L-89-203, NPDES Monitoring Rept for Apr 1989
| ML17223A169 | |
| Person / Time | |
|---|---|
| Site: | Saint Lucie |
| Issue date: | 04/30/1989 |
| From: | Barrons J, Woody C FLORIDA POWER & LIGHT CO. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| L-89-203, NUDOCS 8906130167 | |
| Download: ML17223A169 (4) | |
Text
A.C CELE RATED D1$1BUTION DEMONSTRQ ON SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:8906130167 DOC.DATE: 89/04/30 NOTARIZED:
NO FACIL:50-335 St. Lucie Plant, Unit 1, Florida Power
& Light Co.
50-389 St. Lucie Plant., Unit 2, Florida Power
& Light Co.
AUTH.NAME AUTHOR AFFILIATION BARRONS,J.H.
Florida Power
& Light Co.
WOODY,C.O.
Florida Power
& Light Co.
RECIP.NAME RECIPIENT AFFILIATION DOCKET 05000335 05000389
SUBJECT:
"NPDES Monitoring Rept for Apr 1989.<<
W/890607 ltr.
DISTRIBUTION CODE:
IE23D COPIES RECEIVED:LTR ENCL SIZE:
TITLE: Environmental Event Report (per Tech Specs)
NOTES RECIPIENT ID CODE/NAME PD2-2 LA NORRIS,J INTERNAL: ACRS AEOD/PTB NRR/DREP/EPB 10 NRR/PMAS/ILRB12 OGC/HDS2 RGN2 'ILE 01 EXTERNAL: LPDR NSIC COPIES LTTR ENCL 4
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P.O. Box 14000, Juno Beach, FL 33408-0420 FRL JUNE 7
1989 L-89-203 U.
S. Nuclear Regulatory Commission Attn:
Document Control Desk Washington, D.
C.
20555 Gentlemen:
Re:
St. Lucie Units 1 and 2
Docket Nos.
50-335 and 50-389 Environmental Protection Plan Report National Pollutant Dischar e Elimination S stem NPDES Re ortable Event In accordance with Section 3.2.1. of the St. Lucie Units 1 and 2
Environmental Protection Plans, attached is a copy of the Discharge Monitoring Report (DMR) required by the St.
Lucie Plant NPDES Permit with respect to a
reportable event.
Additionally, a
description of the event is provided.
Very truly yours, C.
O.
Woo Acting S or Vice President Nuclear COW/MSD/gp Attachments cc:
Stewart D. Ebneter, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, St. Lucie Plant ePO(~ g 3Ai67 8+0<'-"0
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0 I3 PERMIT S E c CUPt EN'I S l,LLQ+ REQUIREMENT NAME(TITLEPRINCIPALEXECUTIVE OFFICER RhhAX TYPED OR PRINTED COMMENTANDEXPLANATIONOF ANYVIOLATION V40V'V CVO VV Icertifyunder penalty of law that this documenl and allattachmenls were prepared unAN my direction or supanrislon In accordance with ~ syslem designed to asswe that quafif>>d peaonnel properly gather and eva4ate the inkemation submillad. Based onmy Inquiryof the person or persons who manage the system.or those persons direatyresponsible lor gathering the information. the information submitted is, lo the bast of my thnowtadge and baliet. true. accurate. and complete. Iam aware that there ~re ~nireant panahlies tor submilling false information. including the possb,hhty ol tine and imprh onment for knovnng violations. VVVVVV SIGNATUREOF PRINCIPALEXECUTIVE OFFICER OR AUTHORIZEDAGFNT NUMSER OAILY AV INS T HX HG/L TELEthHOHE I 4S~ YEAR DATE MO OAY l'=AUX ILIA"Ye i=CI)NOEiuSE < DISCHARGE E R=UNII 1 ~ S=UNII 2 ~ oOIRUh iAQNITOK IN(; KE4UIRE0, W}I N dA7 C Dh'DhhAA(,CS yKUN ihtFUL'Lhhhl'ATLR STDRAGh. TAriK AND NDNAKRATDD RATER HDLDINu TANK FPe p'hnff11%l1lpoo 1nyat PAFvhrhihCfnhfhrhihTIhhhyhhCCh
DESCRIPTION OF THE EVENT On April 27,
- 1989, between 12:45 and 2:45 p.m.,
during a chlorination on Unit 2, the 0.2 ppm average limit for free available oxidation (FAO) was exceeded at the condenser outlet. Multigrab samples for that period averaged 0.24 ppm FAO. This exceedance was due to Plant start-up where only two of the four circulating water pumps were operating, therefore reducing dilution flow. Total residual oxidants (TRO) measured by a continuous monitor at the discharge canal terminus remained less than 0.01 ppm during this period. At the terminus, Unit 2 flow is combined with flow from four circulation water pumps'on Unit 1. To
- date, when three or four circulating water pumps were in operation, average FAO has never exceeded 0.2 ppm.
In the future, sodium hypochlorite injection will be throttled should outlet FAO begin to exceed 0.2 ppm.}}