L-88-471, Special Rept:Fire Barrier Penetration Not Returned to Functional Status within 7 Days.Util Making Effort to Obtain Required Parts.Compensatory Measures Continue to Be Implemented as Applicable
| ML17345A499 | |
| Person / Time | |
|---|---|
| Site: | Turkey Point |
| Issue date: | 10/31/1988 |
| From: | Conway W FLORIDA POWER & LIGHT CO. |
| To: | NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM) |
| References | |
| L-88-471, NUDOCS 8811070076 | |
| Download: ML17345A499 (7) | |
Text
ACCELERATED DIAiIBUTION DEMONSTRKON SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:8811070076 DOC.DATE: 88/10/31 NOTARIZED: NO DOCKET FACIL:50-250 Turkey Point Plant, Unit 3, Florida Power and Light C 05000250 50-251 Turkey Point Plant, Unit 4,.Florida Power and Light C 05000251 AUTH.NAME AUTHOR AFFILIATION CONWAY,W.F.
Florida Power
& Light Co.
RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
SUBJECT:
Special rept:on 881031,fire barrier penetration not returned to functional status within 7 days.
DISTRIBUTION CODE:
IE22D COPIES RECEIVED:LTR 3 ENCL
(
SXZE:
TITLE: 50.73 Licensee Event Report (LER), Incident Rpt, etc.
NOTES r
D S
RECIPXENT ID CODE/NAME PD2-2 LA EDISON,G INTERNAL: ACRS MICHELSON ACRS WYLIE AEOD/DSP/TPAB DEDRO NRR/DEST/CEB 8H NRR/DEST/XCSB 7
NRR/DEST/MTB 9H NRR/DEST/RSB 8E NRR/DLPQ/HFB 10 NRR/DOEA/EAB 11 NRR/DREP/RPB 10 NUDOCS-ABSTRACT RES/DSIR/EIB RES/DSR/PRAB EXTERNAL: EG&G WILLIAMS,S H ST LOBBY WARD NRC PDR NSIC MAYS,G COPIES LTTR ENCL 1
1 1
1 1
1 1
1 1
1 1
1 1
1 1
1 1
- 1 1
1 1
1 1
1 2
2 1
1 1
1 1
1 4
4 1
1 1
1 1
1 RECIPIENT ID CODE/NAME PD2-2 PD ACRS MOELLER AEOD/DOA ARM/DCTS/DAB NRR/DEST/ADS 7E NRR/DEST/ESB 8D NRR/DEST/MEB 9H NRR/DEST/PSB 8D.
NRR/DEST/SGB 8D NRR/DLPQ/QAB 10 NRR/DREP/RAB 10 S. SIB 9A RE FILE 02 SR EPY RGN2 FILE 01 FORD BLDG HOY,A LPDR NSIC HARRIS,J COPIES LTTR ENCL 1
1 2
2 1
1 1
1 1
0 1
1 1
1 1
1 1
1 1
1 1
1 1
1 1
1 1
1 1
1 1
1 1
1 1
1 D
NOTE 'I0 ALL "RIDS" RECIPIENTS:
PIZASE HELP US I0 REDUCE WASTE CONIACT THE DOCUMENI CONIBOL DESKS ROOM Pl-37 (EXT. 20079) m ZXZGZATE KKR NAME FROM DISTRIKTZIGN LISTS H)R DOCMERZS YOU DON'T NEEDf D;
TOTAL NUMBER OF COPIES REQUIRED:
LTTR 43 ENCL 42
P.
OX 14000, JUNO BEAGH, FL 33408 0420 OCTOBER 5 1
)S88 L-88-471 U. S. Nuclear Regulatory Commission Attn:
Document Control Desk Washington, D.
C.
20555 Gentlemen:
Re:
Turkey Point Units 3 and 4
Docket Nos.
50-250 and 50-251 Special Report Breached Fire Barriers and Other Fire Protection S stem Im airments In accordance with Technical Specification 6.9.3.c.,
the attached Special Report is provided for your information.
Should there be any questions on this information, please contact us
~
Very truly yours, figpCCC Cia'.
F.
Con y
Senior Vice President Nuclear WFC/RHF/gp Attachment cc:
Malcolm L. Ernst, Acting Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant g'ii01 >07' 050A02!='0
<<(
7g Sai03i pDR AQOOK
- pD'='.
9
)
P P
SPECIAL REPORT OCTOBER 31, 1988 FIRE PROTECTION SYSTEM IMPAIRMENTS REQUIRING NRC NOTIFICATION cirrose:
Technical Specification (TS) 3.14.5.b requires the submission of a report to the NRC if a non-functional fire barrier penetration is not returned to functional status within 7 days.
TS 3.14 also states that certain other conditions require NRC notification.
In accordance with the above requirements, this special report is being generated in order to notify the NRC.
Event:
Fire Protection Impairment (FPI) Numbers 1882 and 1886 were issued for detectors'hich were required to be placed out of service in order to replace a Component Cooling Water Heat Exchanger.
FPIs 1902 and 1928 were issued for two fire doors.
One fire door was being replaced, and the other one had an inoperable lock.
FPI 1901 was issued for a detector which was placed out of service due to repair of its air regulator.
FPI 1926 was issued for the installation of a conduit.
The duration of the work which requires the above impairments extended beyond the Technical Specification limits thus requiring the filing of this Special Report.
Please see Attachment 1 for details.
Cause and Corrective Actions:
FPI 1882 1886 Cause Duration of the work required to replace one of the Component Cooling Heat Exchangers.
14 days is not sufficient to complete this effort.
1902 Parts to complete the repairs were not available or the scope of the 1928 repairs expanded.
1901 1926 Rebar was found during the conduit installation.
This increased the work which was required and extended the schedule.
As corrective action, the plant is making every effort to obtain the required parts.
Those impairments which are not yet closed are being. handled in an expeditious manner to complete the required work.
The plant continues to implement the compensatory measures as applicable.
Attachment 2 identifies impairments which are now closed but were previously reported as open.
ATTACHMENT L SPECIAL REPORT FIRE PROTECTION SYSTEM IMPAIRMENTS WHICH HAVE EXCEEDED TECH SPEC LIMITS SINCE PREVIOUS REPORT FPI ¹ FEATURE TYPE II OPENED CLOSED 1882 1886 1901 1902 1926 1928
- DETECTOR, HEAT 25-1 DETECTOR ALARM POINT 22 DETECTOR ALARM POINT 45 DOOR 094-1 PENETRATION 045E-M007 DOOR 58-2 09/17/88 09/18/88 09/23/88 09/24/88 09/30/88 09/30/88
/ /
/ /
/ /
/ /
/ /
/ /
ATTACHMENT 2 FIRE PROTECTION SYSTEM IMPAIRMENTS PREVIOUSLY NOT REPORTED CLOSED FPI ¹ FEATURE TYPE OPENED CLOSED
, 1523 BARRIER 108A 03/29/88 10/05/88