IR 05000332/1980003

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IE Insp Rept 50-332/80-03 on 801015-17.No Noncompliance Noted.Major Areas Inspected:Internal Reviews & Audits,Safety Committees,Ie Bulletins & Independent Effort
ML20002C254
Person / Time
Site: Barnwell File:Allied-General Nuclear Services icon.png
Issue date: 11/18/1980
From: Coryell G, Kahle J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I), NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20002C253 List:
References
50-332-80-03, 50-332-80-3, NUDOCS 8101090802
Download: ML20002C254 (3)


Text

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NOV 181980 Report No. 50-332/80-3 Licensee: Allied-General Nuclear Services Barnwell, SC 29812 Facility Name: Barnwell Nuclear Fuel Plant Docket No. 50-332 License No. CPCSF-4 Inspection at: Barnwell Nuclear Fuel Plant Ex

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Date'

Approved by.

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. Kahle, Actjing Chief, F @l Facility aK Projects Section, Safegu#ds Branch Inspection Summary Inspection on October 15-17, 1980.

Areas Inspected This routine, unannounced inspection involved 17 inspector-hours onsite in the areas of Internal Review and Audits, Safety Committees, IE Bulletins l

and Circulars and independent effort.

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Results l

No apparent items of noncompliance or deviations were identified in the areas inspected.

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1.

Persons Contacted Licensee Employees

  • G. A. Buckham, Executive Vice President
  • G. T. Stribling, Vice President, Marketing and Regulatory Affairs
  • A. K. Williams, Vice President, Operations and Technical
  • M. Hawkins, Manager, Safety and Environmental Controls
  • W. F. Kelly, Manager, Quality Assurance and Compliance
  • C. E. Walker, Specialist, License Compliance
  • W. R. Waltz, Acting Director, Nuclear Technology J. H. Ellis, Manager, Nuclear Material Control L. B. Wilson, Operations Shift Supervisor T. H. Kervin, Operations Shift Supervisor M. L. Rogell, Engineer, Welding and Metallurgy
  • Attended exit interview.

2.

Exit Interview The inspection scope and findings were sumarized on October 17, 1980 with these persons indicated in Paragraph 1 above.

3.

Licensee Action on Previous Inspection Findings Not inspected.

4.

Unresolved Items Unresolved items were not identified during this inspection.

5.

Safety Comittees a.

Operational Safety Comittee (OSC) meeting minutes for meeting #90, conducted on August 28, 1980, were reviewed.

Agenda coverage, quorum requirements and report distribution and followup records were found to be in accordance with proposed Technical Specification 16.6.2.2 and administrative procedures. The inspector was informed that the OSC is currently reviewing revision 5 of the Site Emergency Plan.

b.

The Executive QA Committee's annual audit of the AGNS QA program was conducted in the period September 8 to 19,1980.

The Comittee audit report has not been issued as of this inspection date and will be reviewed at a later dat.. _ _ _

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-2-6.

Internal Review and Audits Selected QA audit and OSC or OSC/ License Compliance Audit a.

records were reviewed for conformance with procedural requirements of QAP-7 " Audit Procedure" and QAP-4 " Quality Assurance Activity Report (QAAR)". No deviation from procedural requirements were noted, b.

Verification was obtained that the FY1980 scheduled audits had been accomplished. QAAR's examination included QA program audits covering specific appendix B criteria, QA training, evaluations of suppliers, and OSC/ License Compliance audits of AGNS divisions.

7.

Facility Status a.

Activities relating to DOE contract tasks such as the AFR spent fuel project, advanced nuclear materials control and accounting and physical protection development are in progress.

b.

Observations made during a tour of the FRSS and Separations Building were that housekeeping is excellent and that Operations Division logbooks and lock and tag records are up-to-date and in conformance with procedural requirements.

8.

IE Circulars and Information Notices Circular 80-14, " Radioactive Contamination of Plant Demineralized a.

Water System and Resultant Internal Contamination of Personnel".

The use of demineralized water for potable purposes is not permitted.

Inspection of water systems by the applicant did identify a " temporary" jumper connecting the recycle water header into the cold chemical service demineralized water line. This was done to prevent excess process water t,cildup during mini-runs. This sink supply line is locked and tagged to prevent usage and is punch-listed for change at conclusion of the mini-runs.

b.

Circular 80-20, " Changes in Safe Slab Tank Dimensions." AGNS has examined the facility Slab Tanks and determined that the original tank calibrations established the relationship of volume versus liquid level. Calibrations are shown to be accurate and repeatable to better than 0.1% accuracy. Thickness changes greater than 0.002" would be detected by recalibration. The tanks are of 3/8" titantam with 102 1-3/8" titaniam tie-bars and all tanks are vented into a large capacity vent system.

Provisions have been made for routine dimensional checks by tank recalibrations.