IR 05000133/1979002

From kanterella
Jump to navigation Jump to search
IE Insp Rept 50-133/79-02 on 790814-17.No Noncompliance Noted.Major Areas Inspected:Qa Program Annual Review, Procurement,Surveillance,Followup on Lers,Bulletins & Circulars & Independent Insp
ML19254D373
Person / Time
Site: Humboldt Bay
Issue date: 09/21/1979
From: Carlson J, Morrill P, Sternberg D
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML19254D371 List:
References
50-133-79-02, 50-133-79-2, NUDOCS 7910250406
Download: ML19254D373 (6)


Text

.

.-

U. S. NUCLEAR REcULATORY CodDilSSION OFFICE OF INSPECTION AND E!r/ORCEMENT

REGION V

Report No. _ 50 ',3 3/ 79-0,.'

_ 019

_ License No.

DPR-7 Safeguards croup Docket No.

..

L.c.nace:

Icific Gas and clectric Company 77 Beale Street San Francisco, California 94106 Facility Ncme:

Humocidt Bay Unit 3 Insrection at:

Eureka. California Inspection conducted:

August 14-17. 1979 b__.

V[/4/[W Inspecto w

<

Date Signed J. D. Carlson Rea nspect d+- /or,

?f/ Vf79

'

.

~

P. J. Morrill, Reactor Inspe(tor Date Si'gned Date Signed Approved By:

)

9h/ 79

/

,,.

<-

F 6-D. Sternberg, Chief, Reay^oject Section 1

$

D^ SIE"*d Reactor Operations and fiuclear Support Branch Surrma ry :

Inspection on August 14-17,1979 (Report flo. 50-133/79-02)

Areas Inspected:

Routine, unannounced inspection of operations; QA Program Annual Review; Procurement; Surveillance; Followup on Licensee Event Reports; Followup on Bulletins and Cirulars; and independent in-spection. The inspection involved 44 inspector-hours onsite by two !1RC inspectors.

Results: fio items of noncomoliance or deviations were identified.

_

RV Forrn 719 (7)

1209 J38 7910250 y %

.

DETAILS

.

1.

Persons Contacted

"E. Weeks, Plant Superintendent

  • W. Rapp, Power Plant Engineer
  • R. Twiddy, Quality Control Engineer D. Voss, Supervisor of Operations The inspectors also interviewed other licensee employees during the course of the inspection including control operators, shif t foremen,

,mcenoLsem=n, anc office personnel.

  • Denotes those present at the exit interview on August 17, 1979.

2.

Plant Operations The major items remaining to be completed during the outage have been deferred until resolution of the geologic / seismic issues at the plant. No major work was observed to be in progress during this inspection.

The inspectors walked through areas of the plant to observe activities in progress, to inspect the general state of housekeeping, and to check that monitoring instrumentation was reading or recording as required. Temperature and nuclear monitoring indications appeared normal.

The inspectors observed that neutron monitoring was being performed in accordance with Technical Specification requirements.

Normal radiation control practices were in effect including the estabiishment of barrier controls.

No unusual fluid leaks or piping vibrations were observed. The ventilation systems, nuclear instrumentation, component cooling system, and reactor protection systems were in operation during this tour.

Representative samples of the following logs and records from March-July,1979 were examined and discussed with licensee personnel:

Control Operator's Log Shift Foremen's Log Jumper Log Clearance Logs Plant Staff Review Committee Minutes No items of noncompliance or deviations were identified.

_

3.

Annual Review of Quality Assurance Program One personnel change occurred in the QA prograr affecting the Humboldt site. The onsite QA engineer has been withdrawn.

His responsibilities have been transferred in part to the onsite quality control engineer and the remainder to the generel office quality assurance department.

]}Qg9

_2_ . There were several substantial changes to the program made in the par,t year. The inspectors examined these changes and the associated revised procedures and verified that they conform to the appreved program, applicable codes, standards, and regulatory guides. The most significant change was deleting the Qualified Supplier List and endorsing the Coodinating Agency for Supplier Evaluation (CASE) Program. The inspectors discussed the changes and their imple-mentation with the onsite QC engineer.

flo items of noncompliance or deviations were identified.

4.

Surveillance The inspectors reviewed the Control Room Surveillance Schedule and the following surveillance procedures: OTP 8: Refueling Building Leak Rate Test, Gas Treatment System Check, and Refueling Duilding Isolation Monitor Check OTP 9: Liquid Poison System Check OTP 14C: Fire and Low Pressure Core Flood Pump Test All of the completed surveillance tests were accomplished in accordance with approved written procedures.

The test results were in accordance with Technical Specification requirements.

11 0 items of noncompliance or deviations were identified.

5.

Procurement The inspectors toured the warehouse facility to verify safety-related material and spare parts were being handled, stored, and identified in accordance with approved procedures.

In addition, the inspectors reviewed the following: a.

Procedure D-4: Procurement of Safety-Related Equipment, Services and Materials b.

QA Procedure 3.1: Procurement of Items end Services c.

Procurement Document Review Log (8/78-8/79) The above procedures were reviewed to ensure the procurement pro-gram meets the requirements of the Quality Assurance Program.

Implementation of the procurement program was verified by selecting three safety-related items and checking that procurement documents were prepared, tne vendor's qualification was current, ad vendor ' supplied documentation of quality was available.

flo items of noncompliance or deviations were identified.

1209 040

-3- . . Reportable Event Followup 6.

The circumstances and ccrrective action described in the Licensee Event Reports listed below were verified by the inspectors through an examination of selected records, interviews with responsible personnel, and examination of equipment. The events have been reviewed by the licensee and reporting requirements were met.

78-04, Revision 1, Low Flow in Gas Treatment System: Licensee perf ormed a troubleshooting program to determine the cause for the low flow condition. After the ceramic packing in the gas absorption column was replaced, the flow rate returned to normal.

Licensee attributes the cause of the low flow rate to De fouling of Ine packing.

(Ciosec) 79-01, Yearly ILRT Missed: Since Humboldt Bay Unit-3 has been shutdown for seisnic upgrading, the licensee decided to. Smit a Technical Specification char,ge to defer the yearly ILRT requirement until :.tartup. Amendment No.18 to the Technical Specifications was approved on July 13, 1979 making the ILRT deferment effective on January 25, 1979.

The ILRT was due on January 26, 1979; therefore, no noncompliance occurred.

(Closed) 79-02, Late Performance of Surveillance Test: Licensee revised surveillance schedule and placed responsibility for meeting surveillance schedules on the onsite Q.C. engineer.

(Clored) 7.

Followup on IE Circulars and Bulletins The inspectors verified that the plant staff had reciived the IE Circulars and Bulletins listed below. An examination of records and discussions with licensee representatives verified that appro-priate corrective action was identified or taken as follows: a.

Circulars The following Circulars are not applicable to Humbolit Bay Unit-3 and are closed: 79-01, Administration of Unauthori ~f Byproduct Material to Humans.

79-03, Inadequate Guard Training / Qualification and Falsified Training Records.

79-06, Failure to Use Syringe and Bottle Shields 'n Nuclear Medicine.

- 79-07, Unexpected Speed Increase of Reactor Recirculation MG Set Resulted in Reactor Power Increase.

79-08, Attempted Extortion - Low Enriched Uranium.

1209 041

-4- - .. 79-11, Design / Construction Interface Problems.

, 79-12, Potential Diesel Generator Turbocharger Problem.

79-14, Unauthorized Procurement and Distribution of Xenon-133.

The following Circulars are open and are being rev1ewed by licensee personnel for appropriate corrective actions prior to resumption of operations: 78-06, 78-16, 78-17, 78-18, 78-19, 79-02, 79-04, 79-05, 79-10, 79-13.

79-09, Occurrences of Split or Punctured Rect'lator Diaphrams in Certain Contained Breathing Apparatus: L1censee repre-sentatives stated that all Scott regulators were removed from service approximately one and or.e-half years ago and only MSA regulators are being used.

This item will be closed by materials inspector.

(0 pen) 79-15, Bursting of High Pressure Hose and Malfunction of Relief Valve and 0-ring in Certain Self-Contained Breathing Apparatus: Licensee representatives stated that the SurvivAir Mark I equipment is not used at their facility. This item will be closed by materials inspector.

(0 pen) b.

Bulletins 76-01, 76-04, 78-03, 78-09, 78-12,12A,128, 78-14, 79-01, 79-12, 79-03, 79-07, 79-14, 79-18 remain open.

Licensee repre-sentative stated that these open items have been deferred until resolution of the seismic issue and that review and appropriata corrective measures will be taken prior to resumption of plant cperations.

79-04, Incorrect Weights for Saing Check Valves Manufactured by Velan Engineering Corporation: Licensee personnel reviewed purchase order files, and installed equipment logs to determine if this type of check valves were used at Humboldt Bay Unit-3.

It was determined that these valves were not installed; in addi: ion, these check valves were added to the prohibited component list.

(Closed) 79-05, 79-06, 79-13, 79-17, 79-21 were issued for information only, and are closed.

79-08, Events Relevent to BWR Reactors Identified During Three Mile Island Incident: Licensee response commits to some long range actions that will be deferred until after the seismic ' issue is resolved.

Appropriate corrective measures will be taken prior to resumption of plant operations.

(0 pen) 1209 042

- * 79-09, Failures of GE Type AK-2 Circuit Breakers in Safety-Related Systems: Licensee personnel researched installed equipment logs to determine if this type of circuit breaker is used at this facility.

It was determinec that these circuit breakers were not installed and were added to the prohibited equipment list.

(Closed) 79-10, Requalification Training Program Statistics: Licensee provided requested information.

(Closed) 79-11, Faulty Overcurrent Trip Device in Circuit Breakers for Engineered Safety Features: Licensee personnel researched

r.nc.;12
epipmen: '. ;s and de:er+.ef that 'Jestinghouse 03-75 circuit breakers were not installed.

These breakers were added to the prohibited equipment 11st.

(Closed) 79-12, Short Period Scrams at BWR Facilities: Licensee committed to procedure changes and operator training program provided a satisfactory resolution is obtained to the seismic issue.

(0 pen) 79-15, 79-16 and 79-19: Licensee response is in preparation.

(0 pen) No items of noncompliance oc deviations were identified.

8.

Independent Inspection The inspectors toured the facility as part of the turnover inspection for the principal inspectors.

Seismic modifications, augmented off-gas treatment system, and safety-related systems were compre-hensively covered.

It was observed that considerable improvements had been made in housekeeping of Unit 3.

No items of noncompliance or deviations were identified.

9.

Exit Interview The inspectors met with licensee representatives (denoted in Paragraph 1) at the conclusion of the inspection on August 17, 1979.

The purpose and scope of the inspection was summarized.

The licensee was advised that no items of noncompliance or deviations were identified.

~ 1209 043 }}