IR 05000116/1986001
ML20207B285 | |
Person / Time | |
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Site: | University of Iowa |
Issue date: | 11/05/1986 |
From: | Forney W NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
To: | |
Shared Package | |
ML20207B283 | List: |
References | |
50-116-86-01, 50-116-86-1, NUDOCS 8611110572 | |
Download: ML20207B285 (7) | |
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- U.S. NUCLEAR REGULATORY COMMISSION s
REGION III
Report No. 50-116/86001(DRP) License No. R-59 Docket No. 50-116 Licensee: Iowa State University Ames, IA 50010 Facility Name: Iowa State University UTR-10 Reacto Inspection Conducted: ' October.21-24, 1986 Inspector: C. H. Brown
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Approved By: ne , hi Reactor Projects ll/f/f4
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i Inspection Summary Inspection on October 21-24, 1986 (Report No. 50-116/86001(DRP))
Areas Inspected: Routine. .unannot.nced inspection of records, logs, and .' '
organization; review and audit functions; requalification. training; procedures; surveillance and maintenance; fuel handling activities; fuel shipment; radiation protection; radwaste management control; transportation activities; emergency planning. .
Results: No violations were identified in the areas inspected.
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W s Persons Contacted ' f'
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- Dr. B. I. Spinrad, Chairman, Department of Nuclear Engineering '
- Dr. R. A. Hendrickson, Reactor Manager 7, *Dr. R.' E. Williams, Reactor Supervisor l5
T. Sankoorikal, Reactor Operator-
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D. Hamm, Operator Trainee
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! * Denotes those present 'at thet exit intervie '
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' Ge .eral This inspection, which began at 8:30 a.m. on October 21, 1986, was conducted-to examine the research reactor program at the Iowa State University. The facility has toured shortly after arrival. The inspector observed reactor startup and operation during the inspectio '
The general housekeeping of the, facility remains satisfactor ' Organization,LogsandRecords)
The facility organization wa's' reviewed and verified to be consistent-
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~w ith the Technical Specifications and/or Safety. Analysis Report (SAR).
The minimum staffing requirements kere verified to be present during reactor operations, and fuel. handling or refueling operation ,
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The reactor logs ~ and records were reviswed to verify the followin Records were available'for inspectio '-
s Required entries were made,
' Significant problems or incidents were documente The facility was bein' g[ maintained properl No violations or deviations were identifie . Reviews and Audits The licensee's review and audit program records were examined by the inspector to verify the followin I Reviews of facility changes, operating and maintenance procedures, design changes, and unreviewed experiments had been condu'cted by a safety review committee as required by Technichl Specifications or
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SA l The review committee and/or subcorvnittees were composeo of. qualified
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members and -that quorum requiremerits and frequency of meetings had been me i
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. . Required safety audits had been conducted in accordance with Technical Specification requirements and that any identified -
problems were resolve A revie'w of the Radiation Safety Committee and Reactor Use Committee meeting minutes indicated the committees were meeting all requirement '
No violations or deviations were identifie . Requalification Training The~ inspector-reviewed procedures, logs, and training records; and interviewed personnel to verify that the requalification training program was being carried out'in conformance with the facility's approved plan and NRC regulations. Two R0 license and one SR0 license examinations were administered during 1986 by Region III. The three candidates were successful. This provides the facility-with two SR0s and four R0s. One other SR0 at.the facility whose license has expired is planning, at this time, to regain his SR0 license in the near futur No violations or deviations were identifie .- Procedures The inspector reviewed the licensee's procedures to determine if procedures were issued, reviewed, changed or updated, and approved in accordance with Technical Specifications and SAR requirements. This review also verified the followin Procedure content was adequate to safely operate, refuel and maintain the facilit ~ Responsibilities were clearly define Required checklists and forms were use The inspector determined that the required procedures were available and the contents of the procedures were adequate. The licensee had developed a guideline for fonnat and content of the written procedure No violations or deviations were identifie . Surveillance The inspector reviewed procedures, surveillance test schedules, and test records and. discussed the surveillance program with responsible personnel to verify the following,
~ That, when necessary, procedures were available and adequate to
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perform tests.
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. . That tests were completed within the required time schedul . Test records were availabl The licens~ee's surveillance program appeared to be satisfactor No violations or deviations were identifie . Experiments The inspector verified the following by' reviewing ex~periment records and other reactor logs, Experiments were conducted using approved procedures and under approved reactor condition New experiments or changes in experiments were properly reviewed and approve , The experiments did not involve an unreviewed safety question; i.e.,
10 CFR 50.59 requirements regarding experiments were n:et, f Experiments involving potential hazards or reactivity changes were identified in procedure Reactivity limits were not or could not have been exceeded during an
- . experimen The inyector reviewed the changes to one experiment that had been approved since the last inspectio No violations or deviations were identifie . Fuel Handling The facility fuel handling program was reviewed by the inspecto The review included the verification of approved procedures for fuel handling and their technical adequacy in the areas of radiation protection,. criticality safety, Technical Specification, and security plan requirements. The inspector determined by records review and discussions with personnel that fuel handling operations were carried out in conformance of the licensee's procedures.
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No violations or deviations were identified.
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The inspector reviewed records of radioactive material shipments made
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. . The selection of the proper shipping container The preparation of packages for shippin The records of shipment The inspector reviewed the shipping records since the last inspectio The fuel plates in excess of those required for the reactor operation were required to be shipped to a secure facility. The fuel (35 plates)
was shipped on February 14, 1986, and receipt of shipping cask has been acknor;1 edge No violations or deviations were identifie . Radiation Control The inspector reviewed the ra6iation protection activities since the last inspection. Records were reviewed, personnel were interviewed, and observations were made to verify that radiation controls were being carried out in accordance with license and NRC regulations. The areas covered were as follows: Posting and labeling of restricted areas and radioactive material Control of irradiated sample Calibration of radiation detection instrument Required periodic dose rate and contamination survey Exposure records of personne Posted areas of the facilit Personnel trainin Pool water activit No violations or deviations were identifie . Radwaste Management Liquid Wastes No liquid wastes were discharged from the facility during the inspection period. The routine samples taken of reactor coolant (for chemistry control and class work) were turned over to' the environmental group which disposes of waste under the-University's bi-product materials license. The Health Physics personnel stated only a small quantity of reactor liquid waste had been received by the group for disposal during the last two year , ___ - __ . -. .- _ . _ _ __ ________-______- - _- __ -- __
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. , Solid Wastes Normally solid waste is transferred for disposal under the University's bi-product materials license but the minor amount generated during the inspection period has not necessitated a transfe Gaseous Wastes The gaseous radwaste discha'rge from the reactor'is du~e to air saturated water cooling the reactor in an essentially open poo The average reactor power per operating week was less than 5 kilowatt-hours which results in less than 1% of the allowable
- concentration of' argon-41 determined by the time integration of reactor power.-
No violations or deviations were identifie . Emergency Plannin The inspectors reviewed records and interviewed personnel to determine that the approved emergency plan was being carried out by verifying the following: _ That procedures were in place and required records were being kep b '. That required drills were conducted and evaluated, That required-training was conducte R. E. Williams, the reactor supervisor, was named as the Emergency Plan Coordinato No violations or deviations were identifie . Review of Periodic and Special Reports The inspector reviewed the following reports for timel.iness of submittal and adequacy of information submitted, Annual Report: July 1,1984 to June 30, 1985 Annual Report: July 1, 1985 to June 30, 1986 The Annual Report "a." showed a total of 109 kilowatt-hours of energy produced and the report "b." showed 40 kilowatt-hours of energy produce The energy produced is used to provide data for burn-up calculations, and it is also used to calculate the argon-41 release to the building. The Technical Specification states that reactor operation is limited to 100 kilowatt-hours per week to maintain the argon-41 levels to an average concentration less than 50% of listed.value for a restricted area (Table I, Appendix B of 10 CFR Part 20). The historical weekly energy production average has been about 5 kilowatt-hour y_
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> l The Annual Reports discuss the unscheduled shutdowns and corrective actions taken (5 scrams during the two report periods). No major modifications were performed during the reporting period. The reactor was not operated during the last part of 1985 due to an instrument (inlet coolant temperature controller) failure and time lag to obtain a
' replacement. The instrument and indicator had to be replaced with new, functionally equivalent equipment in January 1986. The required reviews and calibrations were performe No violations or deviations were identifie . Exit Interview The inspector met with the licensee representatives (listed in paragraph 1) at the conclusion of the inspection on October 24, 1986, and summarized the scope and findings of the inspection. The inspector also discussed the likely informational content of the inspection report with regard to documents or processes reviewed by the inspector during the-inspection. The licensee did not identify any documents or processes as proprietar