GO2-03-096, May 2003 Monthly Operating Report for Columbia

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May 2003 Monthly Operating Report for Columbia
ML031710554
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 06/11/2003
From: Oxenford W
Energy Northwest
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
GO2-03-096
Download: ML031710554 (3)


Text

ENERGY NORTHWEST P0. Box 968 Richland, Washington 99352-0968 June 11, 2003 G02-03-096 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555-0001

Subject:

COLUMBIA GENERATING STATION, DOCKET NO. 50-397 MONTHLY OPERATING REPORT MAY 2003

Dear Sir or Madam:

Transmitted herewith is the Monthly Operating Report for the month of May 2003 as required by Technical Specification 5.6.4.

Respectfiully, Ws Plant General Manager Mail Drop 927M Attachment cc:

TP Gwynn - NRC RIV BJ Benney - NRC NRR NRC Senior Resident Inspector - 988C TC Poindexter - Winston & Strawn INPO ANI Library Utility Data Institute RN.Sherman - BPA /1399

-w

OPERATING STATUS REPORT for Columbia Generating Station Date: June 1, 2003

1.

Docket: 50-397

2.

Reporting Period: May 2003

3.

Utility

Contact:

Patricia Campbell (509) 377-4664

4.

Design Electrical Rating (Net MWe): 1153

5.

Maximum Dependable Capacity - summer (Net MWe): 1107 MONTH YEAR CUMULATIVE

6.

Hours Re-ctr Critical 72.6

--- 2,641.1l---

122,336.6

7.

Hours Generator On-Line 72.6 2,616.8 118,988.3

8.

Unit Reserve Shutdown Hours 0.0 0.0 3,274.7

9.

Net Electrical Energy (MWH) 70,591 2,865,205 118,117,984 Challenges to safety/relief valves are no longer required per Technical Specification Amendment # 182.

I UNIT SHUTIDOWNS DOCKET NO.: 50-397 UNIT NAME:

Columbia Generating Station DATE: June 1, 2003 COMPLETED BY: P. Campbell TELEPHONE: (509) 377-4664 REPORT PERIOD: May, 2003

SUMMARY

The plant began the month at full power. A Forced Outage began May 4th due excursion. The plant commenced the Refueling Outage on May 9th, one (1) REASON A - Equipment Failure B - Maintenance or Test C - Refueling D - Regulatory Restriction E - Operator Training &

License Examination F - Administration G - Operational Error H - Other (2) ME OD 1 - Manual 2 - Manual Trip/Scram 3 - Auto Trip/Scram 4-Continuation 5 - Other (Explain) ito a reactor coolant water chemistry day earlier than planned.

Type Method of CJuse / Corrective Actions F: Forced Duration Shutting No.

Date S: Scheduled (Hours)

Reason (1)

Down (2)

Comments03-002 5/4/03 F

119.4 A

1 Shutdown because of reace r coolant chemistry that was impacted by a condenser tube leak.

03403 5/9/03 S

552.0 C

5 From the Forced Outage, ediately went into the Planned Refueling and I

Maintenance Outage R-16.