On Friday, April 20, 2018 at 1042
CDT, Braidwood Station Unit 1 was at 0 percent power in Mode 6. The 1A Diesel Generator (
DG) was
inoperable with troubleshooting in progress. The 1B
DG was being run for a normal monthly run in accordance with 1 BwOSR 3.8.1.2-2, 'Unit One 1B Diesel Generator Operability Surveillance,' and subsequently tripped. The trip was due to a failure of the
overspeed butterfly valve actuator and springs, and not an actual
overspeed condition. The unit entered
Technical Specification (TS) 3.8.2, '
AC Sources - Shutdown,' Condition B for required
DG inoperable. All required TS actions were met at the time of the 1B
DG inoperability. The offsite power source remains available. At no time was
residual heat removal lost.
This event is reportable under 10 CFR 50.72(b)(3)(v)(B) for any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to remove residual heat.
The licensee has notified the NRC Resident Inspector.