ENS 52888
ENS Event | |
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19:11 Aug 4, 2017 | |
Title | |
Event Description | On August 4, 2017, at 1511 EDT, Unit 1 Secondary Containment was declared inoperable due to a small (i.e., approximately 0.75 inch diameter) hole in Service Water system piping which was found during ultrasonic testing activities. The affected portion of piping penetrates Secondary Containment and flow in the piping creates a vacuum condition; thus bypassing Secondary Containment. The identified hole is being evaluated with respect to its impact on operability of the Service Water system.
This condition is being reported in accordance with 10 CFR 50.72(b)(3)(v)(C), as an event or condition that could have prevented fulfillment of a safety function needed to control the release of radioactive material. This event did not result in any adverse impact to the health and safety of the public. Initial Safety Significance Evaluation: The initial safety significance of this event is minimal. At the time of discovery, Unit 1 was at 100% steady state conditions. Reactor Building Ventilation was in service in a normal alignment. No abnormal radioactivity conditions existed within Secondary Containment. Corrective Actions: Temporary repair of the affected Unit 1 Service Water piping has been completed. This repair was evaluated by Engineering and it has been determined that the repair meets the requirements to maintain Secondary Containment operable. Unit 1 Secondary Containment operability was restored at 1704 EDT on August 4, 2017. The licensee notified the NRC Resident Inspector.
Based upon further evaluation, Duke Energy is retracting Event Notification 52888. The safety objective of Secondary Containment is to limit the release of radioactivity to the environment after an accident so that the resulting exposures are kept to a practical minimum and are within regulatory limits. A bounding engineering evaluation was performed which demonstrates that potential releases from Secondary Containment could not have resulted in offsite or control room doses exceeding regulatory limits. Furthermore, the condition did not impact Technical Specification operability of Secondary Containment in that the ability of Secondary Containment to maintain the required vacuum was not impacted. Therefore, this condition does not represent an event or condition that could have prevented fulfillment of a safety function needed to control the release of radioactive material and is not reportable in accordance with 10 CFR 50.72(b)(3)(v)(C), and the event notification is being retracted. The NRC Senior Resident was notified of this retraction. Notified R2DO (A. Masters). |
Where | |
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Brunswick North Carolina (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material | |
Time - Person (Reporting Time:+-1.77 h-0.0738 days <br />-0.0105 weeks <br />-0.00242 months <br />) | |
Opened: | William Roberts 17:25 Aug 4, 2017 |
NRC Officer: | Donald Norwood |
Last Updated: | Sep 27, 2017 |
52888 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 528882017-08-04T19:11:0004 August 2017 19:11:00
[Table view]10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material Secondary Containment Inoperable Due to Opening in Service Water Piping ENS 500462014-04-20T06:15:00020 April 2014 06:15:00 10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material Loss of Secondary Containment Due to Opening in Reactor Building Roof Drain Piping ENS 499212014-03-17T11:50:00017 March 2014 11:50:00 10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material Secondary Containment Airlock Door Interlock Malfunction ENS 499102014-03-13T13:37:00013 March 2014 13:37:00 10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material Apparent Secondary Containment Airlock Door Interlock Malfunction ENS 498802014-03-06T21:05:0006 March 2014 21:05:00 10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material Secondary Containment Airlock Door Interlock Malfunction 2017-08-04T19:11:00 | |