This is a non-emergency, information only notification to the
NRCOC. Plant conditions are as follows: Unit 3 is de-fueled and Unit 4 is in Mode 1 [At 100 percent power]. The Unit 3 Startup transformer is
INOPERABLE due to preplanned maintenance. The 3B
Emergency Diesel Generator (
EDG) became
INOPERABLE due to loss of all 480V vital
AC load centers on Unit 3.
With Unit 4 in Mode 1, Technical Specification [TS] 3.8.1.1.c requires a 4-hour report to the NRC due to inoperability of 1 of 3 required EDGs onsite, concurrent with inoperability of a required Startup transformer. This report is for informational purposes only and is not required by 10CFR50.72/73.
Spent Fuel Pool Cooling at Unit 3 remains available via 3B SFP Cooling Pump which is powered from Unit 4.
The loss of the Unit 3 480V AC load centers is still under investigation. TS 3.8.1.1.c requires Unit 4 to exit the TS action statement in 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> or shutdown. To exit this TS, no two battery chargers may be powered from the same motor control center. The 480V vital AC load centers for Unit 3 must be restored since Unit 4 requires at least one train from Unit 3 480V AC load centers. The licensee is in the process of performing those actions.
The licensee notified the NRC Resident Inspector.