ENS 49717
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ENS Event | |
---|---|
09:23 Jan 12, 2014 | |
Title | Manual Reactor Trip Following Control Rod Position Deviation |
Event Description | After achieving criticality a deviation between control rods was observed by plant personnel. When attempting to level the control rods, one rod could not insert to the level of the rest of the group. A manual reactor trip was initiated by the operating crew. All tripable control rods fully inserted into the core.
The trip was uncomplicated and the licensee is investigating the cause of the control rod position deviation. The licensee has notified the NRC Resident Inspector.
Report was updated to indicate 8-hour reportable criteria for Valid Specified System Actuation (Reactor Protection System). The licensee will notify the NRC Resident Inspector. Notified the R4DO (Kellar). |
Where | |
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Fort Calhoun Nebraska (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-2.65 h-0.11 days <br />-0.0158 weeks <br />-0.00363 months <br />) | |
Opened: | Scott Moeck 06:44 Jan 12, 2014 |
NRC Officer: | Ryan Alexander |
Last Updated: | Jan 16, 2014 |
49717 - NRC Website
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Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | Yes, Manual Scram |
Before | Startup (0 %) |
After | Hot Standby (0 %) |
Fort Calhoun with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 520332016-06-22T13:41:00022 June 2016 13:41:00
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