This
8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> notification is being made in accordance with
10 CFR50.72 (b)(3)(v)(A).
On November 24, 2011, 1N35 and 1N36 Intermediate Range Nuclear Instruments High Flux Trip set points were adjusted while Unit 1 was at approximately 55% reactor power following the 1R21 Refueling outage, On December 11, 2011, at 1258 EST Salem Unit 1 entered Technical Specification 3.0.3, after determining the set points were set incorrectly.
A review of the Reactor Engineering Manual, which contains the trip set points, showed that the trip set points for 1N35 and 1N36 were 2.69E-4 and 2.37E-4 respectively. These values equate to approximately 125% thermal power. The Intermediate Range Trip set point is normally set to 25% thermal power. Both channels were declared inoperable and preparations were made to install the correct set points. At 1628 [EST] 1N35 was declared operable and Technical Specification 3.0.3 was exited following installation of the correct set point and retest of the channel.
There was no out-of-service safety related equipment that contributed to this event. No one was injured as a result of this event.
The licensee will notify the NRC Resident Inspector and local authorities.