AEP-NRC-2017-41, Follow Up Notification of Ph Non-Compliance for Turbine Room Sump

From kanterella
Jump to navigation Jump to search
Follow Up Notification of Ph Non-Compliance for Turbine Room Sump
ML17195A248
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 07/11/2017
From: Scarpello M
Indiana Michigan Power Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
AEP-NRC-2017-41
Download: ML17195A248 (6)


Text

s IN DIANA MICHIGAN POWER A unit of American Electric Power July 11, 2017 Docket Nos.: 50-315 50-316 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555-0001 Donald C. Cook Nuclear Plant Units 1 and 2 Indiana Michigan Power Cook Nuclear Plant One Cook Place Bridgman, Ml 49106 lndianaMichiganPower.com AEP-NRC-2017-41 10 CFR 50.4 FOLLOW UP NOTIFICATION OF PH NON-COMPLIANCE FOR TURBINE ROOM SUMP

References:

1. Letter from M. K. Scarpello, Indiana Michigan Power Company, to Nuclear Regulatory Commission, "Notification of PH Non-Compliance for Turbine Room Sump," dated May 25, 2017 (AEP-NRC-2017-35).
2. Letter from J. H. Harner, Indiana Michigan Power Company, to J. Sanders, Michigan Department of Environmental Quality, "Donald C. Cook Nuclear Plant Groundwater Permit GW 1810102," dated June 23, 2017.

By Reference 1, Indiana Michigan Power Company (l&M), the licensee for Donald C. Cook Nuclear Plant (CNP) Units 1 and 2, submitted to the Nudear Regulatory Commission (NRC), a notification of pH non-compliance for Outfall OOD (Turbine Room Sump).

On April 2, 2017, a discharge occurred from Outfall OOD that was below the minimum pH permit limit of 6.5. Approximately 26,000 gallons of water were discharged to the on-site absorption pond with a pH value between 6.4 and 6.1. The next discharge, which occurred on April 3, 2017, had returned within proper pH limits.

By Reference 2, l&M submitted to MDEQ a follow up to Reference 1. Internal evaluation of the cause for the pH lower limit to be exceeded identified that the actuator showed that it was worn/dirty, causing it to malfunction when an alarm signal was provided. This would have allowed the discharge valve to remain open with the pH of the discharge outside of the alarm limits. The valve actuator has been cycled/cleaned and verified to be operational. The replacement of the discharge isolation valve switch (as stated in Reference 1) did not occur, as the evaluation identified it was not malfunctioning.

The exceedance occurred for approximately 13 minutes. The outfall pH was resampled on the next pump out and had returned to within permit limits. Two follow up samples of downgradient wells were taken and indicated pH was within normal values. CNP has not observed any environmental impact from the discharge.

U. S. Nuclear Regulatory Commission Page 2 AEP-NRC-2017-41 Reference 2 is provided, as an enclosure to this letter, in accordance with CNP's Environmental Protection Plan, Section 5.4.2, "Non-Routine Reports."

This letter contains no new or revised commitments. Should you have any questions please contact Jon H. Harner, Environmental Manager, at (269) 465-5901, extension 2102.

&?b~rd-Michael K. Scarpello Regulatory Affairs Manager

Enclosure:

KMH/dmb Letter from J. H. Harner, Indiana Michigan Power Company, to J. Sanders, Michigan Department of Environmental Quality, "Donald C. Cook Nuclear Plant Groundwater Permit GW 1810102," dated June 23, 2017.

c:

R. J. Ancona - MPSC J. K. Rankin, NRC Washington D.C.

NRC Resident Inspector, w/o enclosure C. D. Pederson - NRC Region Ill A.J. Williamson - AEP Ft. Wayne

ENCLOSURE TOAEP-NRC-2017-41 Letter from J. H. Harner, Indiana Michigan Power Company, to J. Sanders, Michigan Department of Environmental Quality, "Donald C. Cook Nuclear Plant Groundwater Permit GW 1810102," dated June 23, 2017.

Indiana Michigan Power Cook-Nuclear Plant One Cook Place Aunit of American Electric Power Bridgman, MI 49106 IndianaMichiganPower.com Mr. Jerrod Sanders - District Supervisor Michigan Department of Environmental Quality Surface Water Quality Division 7953 Adobe Road Kalamazoo, MI 49009-5026 June 23, 2017

Subject:

Donald C. Cook Nuclear Plant Groundwater Pennit GW 1810102 Dear Mr. Sanders This letter is a follow-up letter to our previous notification dated May 10, 2017. The lower limit for pH for Outfall OOD (Turbine Room Sump) was exceeded during a pump-out on April 2, 2017. Approximately 26000 gallons of pH range 6.1 - 6.4 was discharged to the on site absorption pond, As required by Part 1.11.c, the on-line pH meter-data recorded a pH value of7.l on April 3, 2017 at 0221 hrs during the next discharge period.

The fOllowing is a summary of an internal evaluation of the cause for the pH-lower limit to be exceeded:

The TRS (Outfall OOD) effluent is continuously monitored by an on line pH meter. Alarms are set for low pH at 7.0, and High-pH at 8.5. When the pH meter alarms, a signal is sent to a valve controller that will send a signal to the discharge valve to shut off the flow. An alarm is also sent to the control rooms, and subsequently the sump recirculation alarm light illuminates at the make-up plant panel.

On May 5, 2017, TRS pH data was downloaded for preparation of the monthly Discharge Monitoring report. It was noted that there was-a period oftime where-the pH ofthe discharge was below the limit of6.5, and during the following pump out the pH had returned to 7.1.

Cause investigatiOn showed that both the calibration checks for the pH meter and the alarm function was satisfactory before and after the exceedance.

A review of the automatic pump outs showed that it was a routine pump out due to a level signal, so this was not due to a human performance issue as a manual pump out.

Inter-views with operations personnel concluded that manual operation of the discharge valve is not a common occurrence.

Inspection of the valve actuator showed that it was worn/dirty, causing it to malfunction when an alarm signal was provided. This would have allowed the discharge valve to remain open with the pH of the discharge outside of the alarm limits. The valve actuator has been cycled/cleaned and verified to be operational.

The exceedence occmTed for approximately 13 minutes; the outfall pH was resampled on the next pump out and had returned to 7.1 pH (within permit limits).

Two follow up samples of downgradient wells were taken and indicate normal values.

June 23, 2017 GW Permit GW1810102 Page2 Date/time 4/4/2017 0940 4/4/2017 1052 5/10/2017 0900 5/10/2017 1030 Monitorin oiht HResults WellEW-lA 7.28 Well EW-12 7.83 WellEW-lA 6.94 Well EW-12 7.73 We inspect the on-site absorption pond on a weekly basis and-have not observed any environmental -impact from this discharge. Based on the dilution oftbe effluent by a 6 million gallon settling pond, and additional groundwater dilution, there is no impact to the surrounding groundwater from this event. With this notification we have met parts a through d of the pennit requirements.

If you have any questions, please contact me at (269) 465-5901, ext. 2102.

Sincerely, JonH. Hamer Environmental Manager c:

Ms Christina Bauer - MDEQ Kalamazoo Ms Laurelin Martin - MDEQ Kalamazoo USNRC per app. B TS.

June 23, 2017 GW Permit GW1810102 Page 3 be:

J. -P: Gebbie J. D. Ross J. H. Hamer B. D. Newton Q.S. Lies M. K. Scarpello W. H. Schalk J.C. Krieger B. K. Zordell NDM MDEQFile