05000446/LER-2011-003

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LER-2011-003, UNIT 2 EDG 2-02 INOPERABLE DUE TO FUEL OIL LEAK
Comanche Peak Nuclear Power Plant (Cpnpp) Unit 2
Event date: 06-21-2011
Report date: 08-22-2011
Reporting criterion: 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

10 CFR 50.73(a)(2)(v), Loss of Safety Function
4462011003R00 - NRC Website

I. DESCRIPTION OF THE REPORTABLE EVENT

A. REPORTABLE EVENT CLASSIFICATION:

This event is reportable per 10CFR50.73(a)(2)(i)(B) as a condition that was prohibited by the plant's TS and 10CFR50.73(a)(2)(v) as any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to: (B) Remove residual heat; or (D) Mitigate the consequences of an accident.

B. PLANT CONDITION PRIOR TO EVENT:

On May 11, 2011 at 1326, Comanche Peak Nuclear Power Plant (CPNPP) Unit 2 was in Mode 1 at 100% power.

C. STATUS OF STRUCTURES, SYSTEMS, OR COMPONENTS THAT WERE

INOPERABLE AT THE START OF THE EVENT AND THAT CONTRIBUTED TO THE

EVENT

During the period from April 15, 2011 to May 12, 2011, there were two occasions where both Unit 2 EDG trains were inoperable. This condition occurred from April 15, 2011 at 1130 to April 19, 2011 at 1733, and again on April 27, 2011 from 0923 to 1302.

D. NARRATIVE SUMMARY OF THE EVENT, INCLUDING DATES AND APPROXIMATE

TIMES:

On April 15, 2011, at 1130 hours0.0131 days <br />0.314 hours <br />0.00187 weeks <br />4.29965e-4 months <br />, Unit 2 was in Mode 6, approximately two weeks into the twelfth refueling outage (2RF12), when a 12 drop-per-minute (dpm) fuel oil leak was discovered on a Schedule 80 carbon steel fuel oil crossover header of the Train B Emergency Diesel Generator (EDG 2-02) [EIIS: (EK) (DG)]. No attempt was made to fix the leak at the time of discovery due to EDG 2-02 being under a Defense in Depth (DID) for work on the Unit 2 Train A EDG (EDG 2-01).

The EDG System Engineer (Utility, Non-licensed) evaluated the Schedule 80 carbon steel pipe leak and provided an operability determination. After a close visual inspection, the System Engineer determined the leak to be through the threads of the pipe fitting and that it did not constitute a structural failure. Furthermore, the 12 dpm leak did not impede the EDG 2-02 from accomplishing its designed function.

The EDG System Engineer provided the results of his evaluation as his input to an operability report. That report resulted in the Operations Department determining EDG 2-02 remained operable.

A Work Order (WO) was initiated on April 15, 2011 to repair the fuel oil leak. Work could not immediately start due to EDG 2-01 being out-of-service at the time. Repairs to EDG 2-02 would have rendered it inoperable for the duration of the repair.

This condition would have been prohibited by Technical Specifications (TS) 3.8.2, "AC Sources - Shutdown" since the LCO for Modes 5 and 6 requires one EDG to be operable.

Since it was concluded that the EDG 2-02 fuel leak did not affect its operability, addressing it was not an immediate high priority for the Outage Manager (Utility, Non-licensed). The repair of the fuel leak was placed on the Outage Control Center's (OCC's) emergent tracking board until a suitable outage work window became available. The WO was subsequently assigned a 2RF13 work code. That assignment effectively removed it from any future consideration by the at-power Work Schedulers.

At 2304 hours0.0267 days <br />0.64 hours <br />0.00381 weeks <br />8.76672e-4 months <br /> on May 10, 2011, a 24-hour run of EDG 2-02 was commenced to satisfy an 18- month TS Surveillance Requirement (SR). At the start of the run, the fuel leak was the previously recorded 12 dpm. Over the course of the run, the leak worsened, until at the 13-hour point it exceeded 1 liter per minute. EDG 2-02 was secured and deemed inoperable at 1326 on May 11, 2011. Repairs were completed at 0425 hours0.00492 days <br />0.118 hours <br />7.027116e-4 weeks <br />1.617125e-4 months <br /> on May 12, 2011 and EDG 2-02 was declared operable.

Offsite power was never inoperable during this event.

Until the EDG 2-02 was declared inoperable during the 24-hour run of EDG at 2304 on May 10, 2011, the minor thread leak was not considered a challenge to the structural integrity of the pipe and the size of the leak, 12 dpm, did not impede the EDG 2-02 from accomplishing its designed function.

On June 21, 2011, based on subsequent conclusion that EDG 2-02 was inoperable since the leak was identified, this condition was determined to be reportable per 10CFR50.73(a)(2)(i)(B) as a condition that was prohibited by the plant's TS for exceeding the Completion Times. This event is also reportable under 10CFR50.73(a)(2)(v) as any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to: (B) Remove residual heat; or (D) Mitigate the consequences of an accident" for the period of time when both trains of EDGs were inoperable.

E. THE METHOD OF DISCOVERY OF EACH COMPONENT OR SYSTEM FAILURE, OR

PROCEDURAL PERSONNEL ERROR

On April 15, 2011, at 1130, Unit 2 was in Mode 6, approximately two weeks into the twelfth refueling outage (2RF12), when a 12 drop-per-minute (dpm) fuel oil leak was discovered on a fuel oil crossover header of the EDG 2-02. No attempt was made to fix the leak at the time of discovery due to EDG 2-02 being under a DID for work on EDG 2-01.

At 2304 May 10, 2011, a 24-hour run of EDG 2-02 was commenced to satisfy an 18-month TS SR. At the start of the run, the fuel leak was the previously recorded 12 dpm. Over the course of the run, the leak worsened, until at the 13-hour point it exceeded 1 liter per minute. EDG 2-02 was secured and deemed inoperable at 1326 on May 11, 2011. Repairs were completed at 0425 hours0.00492 days <br />0.118 hours <br />7.027116e-4 weeks <br />1.617125e-4 months <br /> on May 12, 2011 and EDG 2-02 was declared operable. Upon disassembly for repair, the Schedule 80 carbon steel fuel oil piping failed due to vibration induced stresses causing circumferential cracking at the leaking threaded connection.

II. COMPONENT OR SYSTEM FAILURES

A. CAUSE OF EACH COMPONENT OR SYSTEM FAILURE

The cause of the EDG 2-02 fuel oil system failure was the failure of a fuel oil pipe due to fatigue failure because of long term vibrational stress.

B. FAILURE MODE, MECHANISM, AND EFFECTS OF EACH FAILED COMPONENT

Not applicable — No component failures were identified during this event.

C. SYSTEMS OR SECONDARY FUNCTIONS THAT WERE AFFECTED BY FAILURE OF

COMPONENTS WITH MULTIPLE FUNCTIONS

Not applicable — No component failures were identified during this event.

D. FAILED COMPONENT INFORMATION

Not applicable — No component failures were identified during this event.

III. ANALYSIS OF THE EVENT

A. SAFETY SYSTEM RESPONSES THAT OCCURRED

Not applicable — No safety system responses occurred as a result of this event.

B. DURATION OF SAFETY SYSTEM TRAIN INOPERABILITY

On April 15, 2011 at 1130 hours0.0131 days <br />0.314 hours <br />0.00187 weeks <br />4.29965e-4 months <br />, Unit 2 was in Mode 6 and EDG 2-01 was inoperable. On April 15, 2011 at 1130 hours0.0131 days <br />0.314 hours <br />0.00187 weeks <br />4.29965e-4 months <br />, Unit 2 was in Mode 6 when the fuel leak was discovered on EDG 2-02. If an event occurred and EDG 2-02 was required to start and run, the leak would have worsened as it did on May 11, 2011. Consequently, EDG 2-02 would not have the required amount of fuel to run seven days and therefore, would have been inoperable per TS. On April 19, 2011 at 1733 hours0.0201 days <br />0.481 hours <br />0.00287 weeks <br />6.594065e-4 months <br />, EDG 2-01 was restored operable. As a result, from April 15 at 1130 to April 19 at 1733 hours0.0201 days <br />0.481 hours <br />0.00287 weeks <br />6.594065e-4 months <br />, Unit 2 would have entered TS 3.8.2, "AC Sources — Shutdown," Condition B since one EDG is required to be operable and both EDGs were inoperable.

Unit 2 reached Mode 4 on April 24, 2011 at 0518 hours0.006 days <br />0.144 hours <br />8.564815e-4 weeks <br />1.97099e-4 months <br />. However, with Unit 2 in MODE 4 and EDG 2-02 still inoperable Unit 2 would have entered TS 3.8.1, "AC Sources Operating" since two EDGs are required and EDG 2-02 is inoperable.

On April 27, 2011 from 0923 to 1302 hours0.0151 days <br />0.362 hours <br />0.00215 weeks <br />4.95411e-4 months <br />, the 2-01 EDG was declared inoperable for a TS SR test while Unit 2 was in MODE 1. Since both EDGs were now inoperable during 0923 to 1302 hours0.0151 days <br />0.362 hours <br />0.00215 weeks <br />4.95411e-4 months <br />, Unit 2 would have entered TS 3.8.1, Condition E for two EDGs inoperable.

Since EDG 2-01 was declared operable at April 27, 2011 at 1302 and EDG 2-02 was still inoperable, TS Condition E would have been exited and Condition B would have been entered since one EDG is inoperable in Mode 1.

EDG 2-02 was restored on May 12, 2011 at 0425 hours0.00492 days <br />0.118 hours <br />7.027116e-4 weeks <br />1.617125e-4 months <br /> and Condition B would have been exited since both Unit 2 EDGs were operable.

C. SAFETY CONSEQUENCES AND IMPLICATIONS OF THE EVENT

The safety function of the CPNPP EDGs is to automatically start and provide power in emergency mode whenever an under-voltage condition is experienced on their respective emergency bus or an SI signal is received. As noted in the event description, the Unit 2 Train B EDG was subsequently considered inoperable from April 15, 2011 to May 12, 2011. During the period of time from April 15, 2011 to May 12, 2011, both of the required offsite power sources were operable and available and no events occurred requiring the EDGs to start and perform their safety function of providing power to the safety related buses. Based on the above, there were no actual safety consequences and the health and safety of the public was not affected.

During the period from April 15, 2011 to May 12, 2011, there were two occasions where both Unit 2 EDG trains were inoperable. This condition occurred from April 15, 2011 at 1130 to April 19, 2011 at 1733, and again on April 27, 2011 from 0923 to 1302. For the period of time that both Unit 2 EDGs were inoperable, the condition meets the definition of a safety system functional failure per 10CFR50.73(a)(2)(v).

However, during this period of time, the non-safety Alternate Power Diesel Generators were available and had the capacity and capability of supplying the necessary equipment for safe shutdown and long term cooling for Unit 2.

IV. CAUSE OF THE EVENT

The cause of the EDG 2-02 fuel oil piping failure was fatigue failure caused by long-term vibration stresses. In addition, it was not recognized that the leak was of a condition where subsequent degradation could occur and could impact the EDG's mission time. Therefore, the repair was not scheduled in an expeditious manner consistent with the EDG's safety significance.

V. CORRECTIVE ACTIONS

The EDG 2-02 crossover piping was repaired and the EDG 2-02 was declared operable. The other EDGs (EDG 1-01, 1-02, and 2-01) crossover piping and piping connections were inspected and no leaks were identified. Additionally, no other leaks of the Schedule 80 carbon steel crossover header piping were identified during inspections for the OPT-214 runs for the other EDGs. Further evaluation of flow induced vibration for the EDG fuel systems, including base excitation is being performed and tracked in the corrective action program. As part of the corrective action program, the process for conducting operability evaluations of similar degraded conditions is being reviewed for additional improvements.

VI. PREVIOUS SIMILAR EVENTS

There have been no previous similar reportable events at CPNPP in the last three years.