LER-1979-014, Forwards LER 79-014/03L-0 |
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| 4091979014R00 - NRC Website |
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e D.tIItYIanND 1*0WEli C00PEftATIVE Ba Crosu, 0%,isirr 54601 August 6, 1979 In reply, please re f e r to LAC-6 4 41 DOCKET NO.40-409 Mr. James G.
Keppler, Regional Director U.
S.
Nuclear Regulatory Commission Directorate of Regulatory Operations Region III 799 Roosevelt Road Glen Ellyn, IL 60137 SUBJ ECT:
DAIhYLAND POWER COOPERATIVE LA CROSSE BOILING WATER REACTOR (LACBWR)
PROVISIONAL OPERATING LICENSE NO. DPR-45 REPORTABLE OCCURRENCE NO. 79-14 REFE RENCES :
(1)
LACBWR Technical Specificati.ons, Section 3. 9. 2.b. (2 )
(2)
LACBWR Technical Specifications, Section 4.2.4.2.3 (3)
LACBWR rechnical Specifications, Section 4.2.4.2.1 (4)
LACBWR Technical Spacifications, Section 4.2.4.2.4
Dear Mr. Kepple r :
In accordance with Re fe rence (1), this is to notify you of conditions leading to operation which conservative surveillance specifications indicated would be a degraded mode permitted oy a limiting condition for operation.
Reference (2) establishes Minimum Critical Power Ratio (NCPR) values as a function of core flow and fuel assembly type for
> 15% of ra ted thermal power.
operation at The surveillance specification 5.2.17.3 conservatively reouires that MCPR shall be determined to be equal to or greater U ar. the limit
-- by verifying that each control rod is within the control rod pattern and withdrawal sequence requirements - -.
65G039
_ 1 _
7 908150 / E
I Mr. James G.
Kepaler, Regional Director LAC-6441 U.
5.
Nuclear Regulatory Commission Aucust 6, 1979 The specified control rod withdrawal sequence for the startup of LACuWR requires that after the Group C rods are fully withdrawn, and all other rods are at 16 dial inches, rods 8 and 12 will be withdrawn as a 2-rod bank.
During the reactor startup on July 8, 1979, control rod 10 was inadvertantly withdrawn instead of rod 12.
When this ou t-o f-se quen ce condition was recognized at 0700 hours0.0081 days <br />0.194 hours <br />0.00116 weeks <br />2.6635e-4 months <br />, the reactor power was 22% of Rated Thermal Power, control rods 8 and 10 were at 27 dial inches, and control rod 12 was at 16 dial inches.
The action requirements of T.S.
4.2.4.2.3 were followed -
adjus tments were initiated immediately and the control rods were re tu rned to the required pattern within approximately 20 minutet.
Subsequent conservative calculations of the reactor thermal-hydraulic conditions during this event showed that the limiting MCPR was not violated (actual MCPR was at least 2.1 times greater than the LCO value for each fual type).
Conservatively calculated values of APLHGR and LHGR were also compared with the LCO values of their respective Technical Specifications (References (3) and (4)) even though these specifications are not applicable
> 25% of rated thermal power.
The until the reactor power is calculated maximum APLHGR was 32.5% of the LCO value, and the maximum LHGR was 36.3% of the LCO value.
The importance of maintaining control rod position within the requirements of the control rod program will be emphasized to all opcrations personne1. No further corrective action is deared necessary.
A Licensee Event Report (Reference:
Appendix A, Regulatory Guide 1.16, Revision 4) is enclosed.
If you have any questior.s concerning this report, please contact us.
Very truly yours, DAIRYLAND POWER COOPERATIVE Prank Linder, General Manager FL: SJ R: abs Encloscres CC:
Director, Office of Inspection and Enforcement (30)
U.
S.
Nuclear Regulatory Commission Washington, D.
C.
20555 Director, Office of Management Information and Progran Control (1)
U.
S.
Nuclear Regulatory Commission Washington, D.
C.
20555 U56MO
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| 05000409/LER-1979-001-01, /01L-0 on 790103:fuel Oil Samples from Tanks Indicated Water & Sediment Concentrations of 0.1%.Similar Occurrence RO-76-15.Tanks Resampled at 3 Elevations Prior to Partial Purging W/Levels Below 0.2% | /01L-0 on 790103:fuel Oil Samples from Tanks Indicated Water & Sediment Concentrations of 0.1%.Similar Occurrence RO-76-15.Tanks Resampled at 3 Elevations Prior to Partial Purging W/Levels Below 0.2% | | | 05000409/LER-1979-001, Forwards LER 79-001/01L-0 | Forwards LER 79-001/01L-0 | | | 05000409/LER-1979-002-01, /01T-0 on 790115:periodic Leakage Rate Testing Revealed Electrical Penetration Units 3,4 & 6 Did Not Meet Type C Test Criteria.Imbrittlement of Epoxy Sealant Contributed to Leaks.Repaired W/Reapplication of Epoxy | /01T-0 on 790115:periodic Leakage Rate Testing Revealed Electrical Penetration Units 3,4 & 6 Did Not Meet Type C Test Criteria.Imbrittlement of Epoxy Sealant Contributed to Leaks.Repaired W/Reapplication of Epoxy | | | 05000409/LER-1979-002, Forwards LER 79-002/01T-0 | Forwards LER 79-002/01T-0 | | | 05000409/LER-1979-003-01, /01T-0 on 790118:indicated Leakage Rate for Seal Injection Sys Makeup Valve Was 0.684 Std Cubic Ft/H.Cause Unknown.Valve Repaired,Now Complies W/Type C Test Criteria | /01T-0 on 790118:indicated Leakage Rate for Seal Injection Sys Makeup Valve Was 0.684 Std Cubic Ft/H.Cause Unknown.Valve Repaired,Now Complies W/Type C Test Criteria | | | 05000409/LER-1979-004-01, /01T-0 on 790119:indicated Leak Rate for Demineralized Water Isolation Valve Was 0.597 Std Cubic Ft/H.Caused by Normal Surface Wear.Valve Repaired & Now Complies W/Type C Test Criteria | /01T-0 on 790119:indicated Leak Rate for Demineralized Water Isolation Valve Was 0.597 Std Cubic Ft/H.Caused by Normal Surface Wear.Valve Repaired & Now Complies W/Type C Test Criteria | | | 05000409/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000409/LER-1979-008-03, /03L-0 on 790429:during Periodic Type C Leakage Rate Testing,Containment Isolation Did Not Meet Tech Spec Criteria.Caused by Damper Disc Shaft Packing.Replaced W/Chevron Type Asbestos Composition Shaft Packing | /03L-0 on 790429:during Periodic Type C Leakage Rate Testing,Containment Isolation Did Not Meet Tech Spec Criteria.Caused by Damper Disc Shaft Packing.Replaced W/Chevron Type Asbestos Composition Shaft Packing | | | 05000409/LER-1979-009-03, /03L-0 on 790507:while Reactor Plant 125 Volt Dc Battery Was Removed for Maint,Control Power Key Switch Turned On.Procedural Change Will Be Initiated Requiring Use of Info Tag on Key Switch | /03L-0 on 790507:while Reactor Plant 125 Volt Dc Battery Was Removed for Maint,Control Power Key Switch Turned On.Procedural Change Will Be Initiated Requiring Use of Info Tag on Key Switch | | | 05000409/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000409/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000409/LER-1979-010-03, /03L-0 on 790522:during Reactor Shutdown,Gross Alpha Activity of Primary Coolant Exceeded Tech Specs.Caused by Irradiated Fuel Matl in Rcs.Primary Purification Resins Replaced & Concentration Reduced | /03L-0 on 790522:during Reactor Shutdown,Gross Alpha Activity of Primary Coolant Exceeded Tech Specs.Caused by Irradiated Fuel Matl in Rcs.Primary Purification Resins Replaced & Concentration Reduced | | | 05000409/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000409/LER-1979-011-03, /03L-0 on 790601:upscale Scram Setpoint on Power Range Nuclear Instrument Channel 6 Exceeded 120% Limit of Rated Thermal Power by 1.8%.Caused by Setpoint Drift of Undetermined Origin.Scram Setpoint Reset | /03L-0 on 790601:upscale Scram Setpoint on Power Range Nuclear Instrument Channel 6 Exceeded 120% Limit of Rated Thermal Power by 1.8%.Caused by Setpoint Drift of Undetermined Origin.Scram Setpoint Reset | | | 05000409/LER-1979-012-03, /03L-0 on 790702:during Operation,Test Revealed Pump A1 Failed to Start Upon Manual Actuation of Control Room Switch.Caused by Electrical Short Causing Diodes to Burn Out & Fuel Valve to Remain Closed.Diodes Replaced | /03L-0 on 790702:during Operation,Test Revealed Pump A1 Failed to Start Upon Manual Actuation of Control Room Switch.Caused by Electrical Short Causing Diodes to Burn Out & Fuel Valve to Remain Closed.Diodes Replaced | | | 05000409/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000409/LER-1979-013-03, /03L-0 on 790704:during Reactor Power Escalation, Piston Rod Seal Failure on Turbine Main Steam Bypass Valve Operating Cylinder Resulted in Loss of Hydraulic Oil.Caused by Normal Wear of Seal.Seals & Oil Replaced | /03L-0 on 790704:during Reactor Power Escalation, Piston Rod Seal Failure on Turbine Main Steam Bypass Valve Operating Cylinder Resulted in Loss of Hydraulic Oil.Caused by Normal Wear of Seal.Seals & Oil Replaced | | | 05000409/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000409/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000409/LER-1979-014-03, /03L-0 on 790708:during Power Escalation,Control Rod 10 Was Withdrawn Rather than Control Rod 12,placing Rods in out-sequence Condition.Caused by Operating Personnel Error.Compliance W/Program to Be Emphasized | /03L-0 on 790708:during Power Escalation,Control Rod 10 Was Withdrawn Rather than Control Rod 12,placing Rods in out-sequence Condition.Caused by Operating Personnel Error.Compliance W/Program to Be Emphasized | | | 05000409/LER-1979-015, Forwards LER 79-015/03L-0 | Forwards LER 79-015/03L-0 | | | 05000409/LER-1979-015-03, /03L:on 790822,during Normal Operation,Auxiliary Operator Commenced Pumping Retention Tank 1B to River,Rather than Sampling 4,500 Gallon Waste Tank.Pumping Stopped & Tank Sampled.No Radiological Release Limits Exceeded | /03L:on 790822,during Normal Operation,Auxiliary Operator Commenced Pumping Retention Tank 1B to River,Rather than Sampling 4,500 Gallon Waste Tank.Pumping Stopped & Tank Sampled.No Radiological Release Limits Exceeded | | | 05000409/LER-1979-016-01, /01T-0:on 790907,during Low Recirculation Flow Scram,Bypass Key Switches Were Not Turned to Normal Position as Required by Tech Specs.Caused by Personnel Error.Addl Training Administered | /01T-0:on 790907,during Low Recirculation Flow Scram,Bypass Key Switches Were Not Turned to Normal Position as Required by Tech Specs.Caused by Personnel Error.Addl Training Administered | | | 05000409/LER-1979-016, Forwards LER 79-016/01T-0 | Forwards LER 79-016/01T-0 | | | 05000409/LER-1979-017-01, /01T-0:on 791109,reactor Vessel Cooled Down at Rate Exceeding Tech Specs During Reactor Scram.Caused by Turbine Governor Problem Resulting in Power to Flow Scram. Turbine Governor Sys Inspected & Flushed | /01T-0:on 791109,reactor Vessel Cooled Down at Rate Exceeding Tech Specs During Reactor Scram.Caused by Turbine Governor Problem Resulting in Power to Flow Scram. Turbine Governor Sys Inspected & Flushed | | | 05000409/LER-1979-017, Forwards LER 79-017/01T-0 | Forwards LER 79-017/01T-0 | | | 05000409/LER-1979-018, Forwards LER 79-018/01T-0 | Forwards LER 79-018/01T-0 | | | 05000409/LER-1979-018-01, /01T-0:on 791214,util Notified by Allis-Chalmers That Containment Isolation Dampers Require Repositioning to Ensure Full Closure.Cause Not Stated.Dampers Closed Pending Allis-Chalmers Analysis.Ler to Be Updated | /01T-0:on 791214,util Notified by Allis-Chalmers That Containment Isolation Dampers Require Repositioning to Ensure Full Closure.Cause Not Stated.Dampers Closed Pending Allis-Chalmers Analysis.Ler to Be Updated | | | 05000409/LER-1979-019, Forwards LER 79-019/01T-0 | Forwards LER 79-019/01T-0 | | | 05000409/LER-1979-019-01, /01T-0:on 791223,periodic Leakage Rate Test for Emergency Airlock Did Not Meet Type B Test Criteria Specified by Tech Specs.Caused by Flattened O Rings & Shaft Packaging in Shaft Seal.Seal Replaced | /01T-0:on 791223,periodic Leakage Rate Test for Emergency Airlock Did Not Meet Type B Test Criteria Specified by Tech Specs.Caused by Flattened O Rings & Shaft Packaging in Shaft Seal.Seal Replaced | |
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