LER-1976-007, /01T-0:on 760624,investigation of RO 76-06 Revealed That Assumed Boron Concentration of LOCA Analysis Was Exceeded During Hydrostatic Leak Test of Reactor Vessel. Caused by Personnel Error.Personnel Reinstructed |
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LER 76-07/01T EVENT DESCRIPTIGN During normal operation an investigation uns initiated into the details of Reportable Occurrence 76-06, Personnel Error.
The in-vestigation discovered that during the hydrostatic leak test of the reactor vessel and portions of the Physics Testing program for Core XII startup the assteed baron concentration, of the IDCA Analysis was exceeded.
Amendment No. 21, Enclosure A to the Technical Specifications asstned maximum boron concentration limits for the main coolant, safety injection tank and safety injection accumulator to minimize Se effects of boren precipitation following a loss of coolant accident.
i With the boron concentrations in excess of those assumed 'on the analysis the post LOCA sump and core concentration would have exceed that assined in the analysis.
This incident is reported as Reportabic Occurrence 50-29/76-07.
CAUSE DESCRIPTION Based on a Post IDCA sump and core concentration of 2314 ppm (from analysis)
Hot Leg Injection would be required in 20 to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to preclude flow channel blockage.. A reanalysis perfonned with the higher boron concentration during Core XII startup (2407 ppm) indicated that the i
time required to hot leg injection would not have changed.
Therefore, it is concluded that this incident wuuld not have been inimical to the public health and safety.
. Personnel have been reminded of their responsibilities to review accident analysis assumptions.
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IIR 76-07/01T ADDITIOXAL FACIORS The 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> report of June 28, 1976 reported that the main coolant boron exceeded that assumed in the accident analysis by approximately 75 ppm during initial power operation.
Further eyaluation of the data revealed that the actual worst case occurrdd during the main coolant system hydrostatic test when the boron concentration reached 2420 ppm.
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| 05000029/LER-1976-001, Forwards LER 76-001/03L-0 | Forwards LER 76-001/03L-0 | | | 05000029/LER-1976-001-03, /03L-0:on 760204,slight Leakage from Charging Pump 3 Found in Two Areas,Relief Valve Discharge Flange & Pump Suction Tee to Valve Line Welds.Caused by Vibration Induced Fatigue Failure.Flange & Tee Replaced | /03L-0:on 760204,slight Leakage from Charging Pump 3 Found in Two Areas,Relief Valve Discharge Flange & Pump Suction Tee to Valve Line Welds.Caused by Vibration Induced Fatigue Failure.Flange & Tee Replaced | | | 05000029/LER-1976-002, Forwards LER 76-002/03L-0 | Forwards LER 76-002/03L-0 | | | 05000029/LER-1976-002-03, /03L-0:on 760210,auxiliary Operator Noted Leak in Weld on Reducer Discharge Header of Charging Pump 3.Caused by Vibration Induced Fatigue Failure,Due to Continuous Operation of Displacement Charging Pump | /03L-0:on 760210,auxiliary Operator Noted Leak in Weld on Reducer Discharge Header of Charging Pump 3.Caused by Vibration Induced Fatigue Failure,Due to Continuous Operation of Displacement Charging Pump | | | 05000029/LER-1976-003, Forwards LER 76-003/01T-0 | Forwards LER 76-003/01T-0 | | | 05000029/LER-1976-003-01, /01T-0:on 760513,review of ECCS Analysis Found Error in Accident Analysis.Caused by Error in Assumption of Accident Analysis.Reanalysis Performed.Proposed Change to Tech Specs Submitted | /01T-0:on 760513,review of ECCS Analysis Found Error in Accident Analysis.Caused by Error in Assumption of Accident Analysis.Reanalysis Performed.Proposed Change to Tech Specs Submitted | | | 05000029/LER-1976-004, Forwards LER 76-004/03L-0 | Forwards LER 76-004/03L-0 | | | 05000029/LER-1976-004-03, /03L-0:on 761216,during Monthly Test,Hpsi Pump 1 Shaft Housing Seal Was Found to Leak Lightly.Caused by Cut in Gasket.Defective Gasket Replaced | /03L-0:on 761216,during Monthly Test,Hpsi Pump 1 Shaft Housing Seal Was Found to Leak Lightly.Caused by Cut in Gasket.Defective Gasket Replaced | | | 05000029/LER-1976-005-03, /03L-0:on 760520,auxiliary Operator Noted Slight Leakage from Weld on Inlet Charging Pump 3 Relief Valve. Caused by Pullback Gap Not Allowed During Installation of Pipe & Vibration Induced Fatigue Failure | /03L-0:on 760520,auxiliary Operator Noted Slight Leakage from Weld on Inlet Charging Pump 3 Relief Valve. Caused by Pullback Gap Not Allowed During Installation of Pipe & Vibration Induced Fatigue Failure | | | 05000029/LER-1976-005-30, /030-1:on 760520,weld on Inlet to Charging Pump 3 Relief Valve Found Leaking.Caused by Error in Installation of Pipe in Which Full 1/16 Inch Pullback Not Allowed | /030-1:on 760520,weld on Inlet to Charging Pump 3 Relief Valve Found Leaking.Caused by Error in Installation of Pipe in Which Full 1/16 Inch Pullback Not Allowed | | | 05000029/LER-1976-005, Forwards LER 76-005/03L-0 | Forwards LER 76-005/03L-0 | | | 05000029/LER-1976-006, Forwards LER 76-006/01T-0 | Forwards LER 76-006/01T-0 | | | 05000029/LER-1976-006-01, /01T-0:on 760624,during Normal Operation,Routine Safety Injection Tank Makeup Was Performed Per Plant Procedure.Acceptance Criteria Not Met.Caused by Change 117, Suppl 3,requiring Limits on Boron Concentration | /01T-0:on 760624,during Normal Operation,Routine Safety Injection Tank Makeup Was Performed Per Plant Procedure.Acceptance Criteria Not Met.Caused by Change 117, Suppl 3,requiring Limits on Boron Concentration | | | 05000029/LER-1976-007-01, /01T-0:on 760624,investigation of RO 76-06 Revealed That Assumed Boron Concentration of LOCA Analysis Was Exceeded During Hydrostatic Leak Test of Reactor Vessel. Caused by Personnel Error.Personnel Reinstructed | /01T-0:on 760624,investigation of RO 76-06 Revealed That Assumed Boron Concentration of LOCA Analysis Was Exceeded During Hydrostatic Leak Test of Reactor Vessel. Caused by Personnel Error.Personnel Reinstructed | | | 05000029/LER-1976-007, Forwards LER 76-007/01T-0 | Forwards LER 76-007/01T-0 | | | 05000029/LER-1976-008, Updated LER 76-008/010-0:on 760730,review of Rod Ejection Accident Analysis Revealed Error in Method Used for Core 11 Analysis.Caused by Error in Methods & Application of Analysis Codes.Sys of Documentation Control Initiated | Updated LER 76-008/010-0:on 760730,review of Rod Ejection Accident Analysis Revealed Error in Method Used for Core 11 Analysis.Caused by Error in Methods & Application of Analysis Codes.Sys of Documentation Control Initiated | | | 05000029/LER-1976-010, Forwards LER 76-010/01T-0 | Forwards LER 76-010/01T-0 | | | 05000029/LER-1976-010-01, /01T-0:on 760830,during Review of Core 12 Analysis,Error Found in Figure 8-1 of Tech Specs.Caused by Gamma Heating Correction Omitted by Error in Application of Computer Codes | /01T-0:on 760830,during Review of Core 12 Analysis,Error Found in Figure 8-1 of Tech Specs.Caused by Gamma Heating Correction Omitted by Error in Application of Computer Codes | | | 05000029/LER-1976-011, Forwards LER 76-011/03L-0 | Forwards LER 76-011/03L-0 | | | 05000029/LER-1976-011-03, /03L-0:on 760907,slight Leakage Noted from Welded Nipple on Charging Pump 3 Discharge Heater Line.Caused by Failure to Allow 1/16-inch Pull Back Gap During Installation of Weld.Pump Isolated & Nipple Replaced | /03L-0:on 760907,slight Leakage Noted from Welded Nipple on Charging Pump 3 Discharge Heater Line.Caused by Failure to Allow 1/16-inch Pull Back Gap During Installation of Weld.Pump Isolated & Nipple Replaced | | | 05000029/LER-1976-012-01, /01T-0:on 761119,safety Injection Accumulator for Boron Was 30 Ppm Over Tech Specs & 80 Ppm Over Administrative Limits.Investigation Revealed That Std Sodium Hydroxide Titrant Had Concentrations Lower than Predicted | /01T-0:on 761119,safety Injection Accumulator for Boron Was 30 Ppm Over Tech Specs & 80 Ppm Over Administrative Limits.Investigation Revealed That Std Sodium Hydroxide Titrant Had Concentrations Lower than Predicted | | | 05000029/LER-1976-012, Forwards LER 76-012/01T-0 | Forwards LER 76-012/01T-0 | | | 05000029/LER-1976-013-01, /01T-0:on 761128,following Plant Trip from Power, Main Collant Pump 3 Inadvertently Restarted During Scram Recovery.Caused by Jammed Trip Mechanism on Air Circuit Breaker.New Trip Coil Installed | /01T-0:on 761128,following Plant Trip from Power, Main Collant Pump 3 Inadvertently Restarted During Scram Recovery.Caused by Jammed Trip Mechanism on Air Circuit Breaker.New Trip Coil Installed | | | 05000029/LER-1976-013, Forwards LER 76-013/01T-0 | Forwards LER 76-013/01T-0 | | | 05000029/LER-1976-014-03, /03L-0:on 761216,during Performance of OP-4204, Monthly Test of Safety Injection Pumps,High Pressure Safety Injection Pump Shaft Housing Seal Found Leaking.Caused by Cut in Gasket.Defective Gasket Replaced | /03L-0:on 761216,during Performance of OP-4204, Monthly Test of Safety Injection Pumps,High Pressure Safety Injection Pump Shaft Housing Seal Found Leaking.Caused by Cut in Gasket.Defective Gasket Replaced | |
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