On March 8, 2018, an invalid system actuation occurred while preparations were underway to perform Safety Features Actuation System (SFAS) integrated response time surveillance testing during the recent Davis Besse Nuclear Power Station refueling outage. Several minutes after connecting a data recorder to monitor the
Emergency Diesel Generator (
EDG) 1 start signal, at
1323 hours0.0153 days <br />0.368 hours <br />0.00219 weeks <br />5.034015e-4 months <br /> [EST], the
EDG started with no valid actuation signals or test inputs present. The
EDG successfully came up to speed and voltage as expected. The associated essential 4160 volt electrical bus remained energized from the normal power supply, therefore, the
EDG output breaker did not close to supply power to the bus. Troubleshooting determined the inadvertent actuation was due to a short in the test lead wires at the recorder connection caused by a faulty test lead. The test lead was replaced and the SFAS surveillance testing completed satisfactorily.
This event is being reported as an invalid system actuation per 10 CFR 50.73(a)(2)(iv)(A); this 60-day optional telephone notification is being made per 10 CFR 50.73(a)(i) in lieu of submitting a written Licensee Event Report.
The NRC Resident Inspector was notified of the inadvertent
EDG start at the time of the event and has been notified of this invalid specified system actuation notification.