ENS 40263
ENS Event | |
---|---|
06:00 Oct 21, 2003 | |
Title | Plant Shutdown Required by Technical Specifications |
Event Description | Due to failure of an instrument power inverter (NN11) which supplies vital 120Vac bus NN01, Callaway Plant entered L.C.O. 3.8.7, Electrical Power Systems, Inverters - Operating, Condition A at 0721 on October 20, 2003. The inverter supplying the bus is required to meet the LCO. Since the initiation of the inverter failure, the vital instrument bus has been energized from alternate power supply transformers in accordance with plant design and procedures. It is not an acceptable alternative to meet the LCO OPERABILITY requirement.
Details of the impact on the plant due to this failure are detailed in Corrective Actions Program Report (C.A.R.) 200307636. In summary, the bus voltage was lost momentarily, then restored by operation of the inverter static transfer switch. The failure and subsequent restoration of power to AC Vital Bus caused some control systems responses that were corrected by the control room staff. After the event was stabilized, power remained at 100%. The LCO Action is to restore the inverter to OPERABLE status within twenty four (24) hours, otherwise be in MODE 3 in 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> AND be in Mode 5 in thirty six (36) hours. The twenty four hour period ends at 0721 October 21, 2003. In advance of the action time, a controlled plant shutdown to Mode Three (3) was commenced at 0100 on October 21, 2003 at a rate of ten (10) percent per hour. At the time of this report, maintenance efforts have determined that the problem is internal to the inverter Static Transfer Switch, therefore the reduction of power will continue. No safety system actuations resulted from the control power transfer. The licensee has notified the NRC Resident Inspector. |
Where | |
---|---|
Callaway Missouri (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown | |
LER: | 05000483/LER-2003-009 |
Time - Person (Reporting Time:+-0.67 h-0.0279 days <br />-0.00399 weeks <br />-9.17766e-4 months <br />) | |
Opened: | Charles Sarrow 05:20 Oct 21, 2003 |
NRC Officer: | Mike Ripley |
Last Updated: | Oct 21, 2003 |
40263 - NRC Website | |
Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (70 %) |
WEEKMONTHYEARENS 512532015-07-23T06:15:00023 July 2015 06:15:00
[Table view]10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Initiation of Plant Shutdown Due to Rcs Leakage ENS 448632009-02-19T11:30:00019 February 2009 11:30:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Power Supply Failure Resulting in a Tech Spec Required Shutdown ENS 417812005-06-17T00:02:00017 June 2005 00:02:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Unit Commenced a Tech Spec Required Shutdown Due to an Electrical Problem Affecting a Safety Related Battery ENS 415272005-03-26T09:00:00026 March 2005 09:00:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Inoperable Esw Train. ENS 402632003-10-21T06:00:00021 October 2003 06:00:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Plant Shutdown Required by Technical Specifications 2015-07-23T06:15:00 | |