ENS 45663
ENS Event | |
---|---|
21:25 Jan 26, 2010 | |
Title | Entry Into Technical Specification Required Shutdown |
Event Description | While operating in mode 1 at 100% power, [the licensee] identified [a] failure to comply with Technical Requirements [TR] Manual 3.7.20, Snubbers, Condition C. [The] required action C.1 requires the performance of an inspection of required snubbers affected by transient in accordance with Table TR 3.7.20-1 within 6 months of the event. WCNOC [Wolf Creek Nuclear Operating Corporation] determined that a portion of the required inspections was not completed for transients that occurred during Refueling Outage 16 (Spring 2008). TR 3.7.20, Snubbers, Condition D requires affected systems to be declared inoperable immediately. No major equipment was out of service prior to the event.
At 1525 CST, TS [Technical Specification] LCO [Limiting Condition of Operation] 3.7.8, Essential Service Water (ESW) System, was declared not met, [and therefore], both trains of ESW [were declared] inoperable. With both trains of ESW inoperable, TS LCO 3.0.3 was entered and preparations for unit shutdown commenced. Additionally, with both trains of ESW inoperable both Emergency Diesel Generators were declared inoperable. TS LCO 3.8.1, AC Sources - Operating, Conditions B and F were entered. Actions to complete required inspections per TR 3.7.20 Table TR 3.7.20-1 have been initiated. Shutdown was commenced at 1618 CST. NRC Senior Resident was notified 1/26/2010 15:30 CST regarding entry into TS LCO 3.0.3.
The licensee completed inspection of Train "B" snubbers, and at 2013 CST, the licensee exited TS LCO 3.0.3 based on restoration of Train "B" of Essential Service Water System to operable status. Licensee is still inspecting Train "A" snubbers. The licensee has notified the NRC Resident Inspector. Notified R4DO (Greg Pick) |
Where | |
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Wolf Creek Kansas (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown | |
Time - Person (Reporting Time:+-3.93 h-0.164 days <br />-0.0234 weeks <br />-0.00538 months <br />) | |
Opened: | Jeff Isch 17:29 Jan 26, 2010 |
NRC Officer: | Joe O'Hara |
Last Updated: | Jan 26, 2010 |
45663 - NRC Website
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Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (98 %) |
WEEKMONTHYEARENS 572842024-08-23T13:00:00023 August 2024 13:00:00
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