05000321/FIN-2017002-04
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Finding | |
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Title | Licensee-Identified Violation |
Description | TS 3.6.4.1 requires secondary containment be operable in Mode 1 and during movements of irradiated fuel assemblies in the secondary containment. Contrary to the above, on February 8 at 1035, with Unit 1 operating at 100 percent RTP and Unit 2 conducting refueling operations, secondary containment was made inoperable when Unit 2 reactor building containment was breached for a scheduled refueling outage and a configuration control error on the Unit 2 standby gas treatment system provided a uncontrolled opening into the secondary containment for the Unit 1 reactor building and the common refueling floor. A temporary blind flange had been incorrectly installed on the upstream side vice downstream side of the Unit 2 standby gas treatment inlet isolation valve when the valve had been removed from the system for testing. This configuration rendered secondary containment for the Unit 1 reactor building and the common refueling floor inoperable. A senior reactor operator performing a plant tour noted the incorrect flange configuration and at 2017 on February 17, the blind flange was moved to the downstream side of the Unit 2 standby gas treatment inlet isolation valve to restore compliance. Inspectors screened the finding in accordance with IMC 609 Appendix A The Significance Determination Process (SDP) for Findings at-Power. The finding screened as very low safety significance (Green) because the questions in Appendix A Exhibit 3 for Control Room, Auxiliary, Reactor, or Spent Fuel Pool Building, were answered no. This issue was documented in the licensees corrective action program as CR 10332592. |
Site: | Hatch |
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Report | IR 05000321/2017002 Section 4OA7 |
Date counted | Jun 30, 2017 (2017Q2) |
Type: | NCV: Green |
cornerstone | No Cornerstone |
Identified by: | Licensee-identified |
Inspection Procedure: | |
Inspectors (proximate) | D Hardage D Retterer J Montgomery P Braaten J Munday |
Violation of: | Technical Specification |
INPO aspect | |
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Finding - Hatch - IR 05000321/2017002 | |||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Hatch) @ 2017Q2
Self-Identified List (Hatch)
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