ML17216A813

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Forwards NPDES Discharge Monitoring Rept for Nov 1985. Outfall 071 Exceeded Monthly Average Total Iron Limit for Nov.Caused by High Levels of Iron in Susquehanna River.On 851105,excursion of Free Chlorine in Blowdown Occurred
ML17216A813
Person / Time
Site: Susquehanna  Talen Energy icon.png
Issue date: 12/26/1985
From: Fields J
PENNSYLVANIA POWER & LIGHT CO.
To: Koval P
PENNSYLVANIA, COMMONWEALTH OF
Shared Package
ML17216A814 List:
References
PLE-7895, NUDOCS 8601060269
Download: ML17216A813 (2)


Text

Pennsylvania Power 8 Light Company Two North Ninth Street

~ Allentown, PA 18101

~ 215 I 770.5151 December 26, 1985 Mr. Paul Koval Chief, Operations Section Bureau of Water Quality Management Pennsylvania Department of Fnvironmental Resources 90 East Union Street, Second Floor Wilkes-Barre, PA 18701-3296 SUSQUEHANNA STEAM ELECTRIC STATION DISCHARGE MONITORING REPORT NPDES PERMIT NO.

PA 0047325/NOVEMBER 1985 CCN 741326 FILE 012-4 PLE-7895

Dear Mr. Koval:

Enclosed is a copy of the November 1985 Discharge Monitoring Report for Permit No.

PA 0047325.

The following information details data and/or non-compliances for some of the permitted outfalls:

Outfall 071:

Cooling Tower Blowdown Flows are currently, being estimated.

The monthly average total iron limit of 6.8 mg/1 was exceeded in November (12.18 mg/l).

The cause of this violation can be attributed to high levels of iron in the Susquehanna River.

See Note 84 of DMR 071.

The daily maximum of 1 mg/1 for total zinc was exceeded (1.1 mg/1). It is assumed the cause for this excursion is also the river.

'I There was a short excursion of free chlorine in the blowdown on November 4.

The free chlorine was above 0.5 ppm from 0940 to 1110 (about 90 minutes).

The highest level was 0.85 ppm at 0950.

The excess chlorine was due to a shut down of Unit 1 reactor and the subsequent reduction of chlorine demand by reduced heat load and makeup.

See Note i/6 of DMR 071.

Outfall 072:

Service and Administration Building Sump The total suspended solids (TSS) average monthly limit of 30 mg/1 was exceeded (56.0 mg/1), however, the daily maximum of 100 mg/1 was not for TSS.

See Note 83 of DMR 072.

Sb010b02b9 85122b PDR ADQCK 05000387 R

PDR gEA

December 26, 1985 PLE-7895 CCN 741326 FILE 012-4 Outfall 271:

Waste Filter Bypass The TSS limit of 30 mg/1 was exceeded (323 mg/1).

This violation will be corrected"in 1986.

If you have any questions, please call me at (215) 770-7889.

Respectfully yours, (g,4

~

Jerome S. Fields Senior Environmental Scientist-Nuclear JSF/amc jsfltk004033o cc:

. EPA, Region III E.

Adensam