05000259/LER-1980-055-03, /03L-0:on 800708,during HPCI Special Instruction 4.5.E.1.d & E,Pdv 73-43 Failed to Operate Properly.Caused by Valve Stuck Closed Due to Loose Valve Guide.Valve Disassembled & Cleaned & Valve Guide Tightened

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/03L-0:on 800708,during HPCI Special Instruction 4.5.E.1.d & E,Pdv 73-43 Failed to Operate Properly.Caused by Valve Stuck Closed Due to Loose Valve Guide.Valve Disassembled & Cleaned & Valve Guide Tightened
ML19331B624
Person / Time
Site: Browns Ferry 
Issue date: 08/06/1980
From:
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19331B605 List:
References
LER-80-055-03L-01, LER-80-55-3L-1, NUDOCS 8008120505
Download: ML19331B624 (2)


LER-1980-055, /03L-0:on 800708,during HPCI Special Instruction 4.5.E.1.d & E,Pdv 73-43 Failed to Operate Properly.Caused by Valve Stuck Closed Due to Loose Valve Guide.Valve Disassembled & Cleaned & Valve Guide Tightened
Event date:
Report date:
2591980055R03 - NRC Website

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Tennessee Valley Authority Form BF-27 Browns Ferry Nuclear Plant BF 15.2 1/10/79 LER SUPPLEMENTAL INFORMATION BFRO 259 / _ 8055 Technical Specification Involved 3.5.E.2 Reported Under Technical Specification 6.7.2.b (2)

Date of Occurrence 7/8/80 Time of Occurrence 1630 Unit 1 Identification and Description *ct' Occurrence:

While running SI 4.5.E.1.d and e on the HPCI, PCV-73-43 f ailed to operate properly.

Conditions Prior to Occurrence:

Unit 1 - 93% steady state power.

Unit 2 - 96% steady state power.

Unit 3 - cold shutdown Action specified in the Technical Specification Surveillance Requirements met due to inoperable equipment.

Describe.

CS, DIR, RCIC, and ADS logic proven operable.

A_pparent Cause of Occurrence:

The valve was stuck closed due to the main valve guide becoming loose and unthreading.

Analysis of Occurrence:

There was no danger to. the health or safety of the public, no significant resulting chain of events, no release of activity, and no damage to plant or equipment.

Corrective Action

The valve was disassembled aad cleaned and the valve guide tightened. No recurrence control is required due to no previous failure history.

Failure Data:

NA eriod - Lifetpe; Responsibility - Administrative Supervisor

  • Reten tion :

' Revision:

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