ENS 46457
ENS Event | |
---|---|
10:18 Dec 6, 2010 | |
Title | Tech Spec Required Shutdown Due to Exceeding Allowed Outage Time on the 'A' Emergency Diesel Generator |
Event Description | (KKJ01A) 'A' Emergency Diesel Generator (EDG) was removed from service and declared inoperable [on] 11/29/2010 at 0500 (CST) for a scheduled 7 day Technical Specification equipment outage to perform various scheduled maintenance items. Technical Specification 3.8.1 Condition B was entered for one Diesel Generator inoperable, utilizing Action B.4.2.2, 'Restore the Diesel Generator to OPERABLE within 7 days AND 10 days from discovery of failure to meet LCO'.
On 12/06/2010, it was discovered during the Operability Run Surveillance, STS KJ-015A, utilized to restore the EDG to service, the Engine Analyzer Data Acquisition [software] indicated the No. 12 cylinder is 'out of balance' and will require a clearance order and maintenance repair. On 12/06/2010 [at] 0350 hrs., it was determined that the work required to restore the EDG to service would cause the Tech Spec 3.8.1 Action B.4.2.2 Completion Time requirement of 7 days to be exceeded, requiring a Plant Shutdown per TS 3.8.1 Condition H, with Action H.1, 'Be in Mode 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />', and Action H.2, 'Be in Mode 5 within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />'. Plant Shutdown to Mode 3 was commenced [on] 12/06/2010 at 0418 (CST). The [NRC] Resident Inspector has been contacted. The licensee indicated that required repairs should be completed within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> and expects restart to occur on 12/06/2010. |
Where | |
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Wolf Creek Kansas (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown | |
Time - Person (Reporting Time:+-4.6 h-0.192 days <br />-0.0274 weeks <br />-0.0063 months <br />) | |
Opened: | Preston Lawson 05:42 Dec 6, 2010 |
NRC Officer: | Howie Crouch |
Last Updated: | Dec 6, 2010 |
46457 - NRC Website
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Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (85 %) |
WEEKMONTHYEARENS 572842024-08-23T13:00:00023 August 2024 13:00:00
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