ML22132A121
| ML22132A121 | |
| Person / Time | |
|---|---|
| Site: | Summer |
| Issue date: | 04/12/2022 |
| From: | Lippard G Dominion Energy South Carolina |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| 22-161 | |
| Download: ML22132A121 (33) | |
Text
V.C. Summer Nuclear Station
~ Dominion Bradham Bl vd & Hwy 215. Jen ki nsvil le. SC 29065 Mail ing Addres s:
P.O. Box 88 , Jen kinsville, SC 29065
- iiiiiii" Energy Dominio n En ergy.com April 12, 2022 Document Control Desk Serial No.
- 22-161 U.S. Nuclear Regulatory Commission VCS-LIC/TS RO Washington , DC 20555 Docket No. 50-395 License No. NPF-12 DOMINION ENERGY SOUTH CAROLINA, INC. (DESC)
VIRGIL C. SUMMER NUCLEAR STATION (VCSNS) UNIT 1 REPORTING RELATED TO NATIONAL POLLUTANT DISCHARGE ELIMINATION SYSTEM (NPDES) PERMITS AND STATE CERTIFICATIONS DESC hereby submits a copy of the South Carolina Department of Health and Environmental Control (SCDHEC) Consent Order 22-024-W for NPDES Permit SCG646072 in accordance with VCSNS Operating License Appendix B Section 3.2, Reporting Related to the NPDES Permits and State Certifications. Consent Order 22-024-W covers the violation for not performing Total Residual Chlorine (TRC) analyses by a certified laboratory. The notice of violation for not performing TRC analyses by a certified laboratory as required by South Carolina laboratory certification regulations was provided to the Nuclear Regulatory Commission in a letter dated January 20, 2022 (ML22020A416).
In addition, DESC is providing copies of environmental violations concerning permit limits for NPDES Permits SC0030856 and SCG646072. The violations for NPDES Permit SC0030856 were reported to the SCDHEC via electronic Discharge Monitoring Reports (DMRs) for permit exceedances of the pH Instantaneous Maximum in December 2021 and the Total Suspended Solids Monthly Average in March 2022. The violations for NPDES Permit SCG646072 were reported to SCDHEC via electronic DMRs for permit exceedances of TRC Monthly Average and Daily Maximum in January 2022. The notice of violation for the January 2022 TRC permit exceedances is also included in this submittal.
Should you have any questions, please call Mr. Michael Moore at (803) 345-4752 .
Sincerely,
~
Site Vice President
- pa;d V.C. Summer Nuclear Station Enclosures Comm itments contained in this letter
- None cc:
G. J. Lindamood - Santee Cooper L. Dudes- NRC Region II G. Miller- NRC Project Mgr.
NRC Resident Inspector
Serial No.22-161 Enclosures Page 1 of 32 VIRGIL C. SUMMER NUCLEAR STATION (VCSNS) Unit 1 DOCKET NO. 50-395 OPERATING LICENSE NO. NPF-12 Enclosures Consent Order 22-024-W Permit Number SC0030856 Discharge Monitoring Report DMR Period 12/1/2021 -12/31/2021 Permit Number SC0030856 Discharge Monitoring Report DMR Period 3/1/2022- 3/31/2022 Permit Number SCG646072 Discharge Monitoring Report DMR Period 1/1/2022 -1/31/2022 Notice of Violation Al-0005261 Permit Number SCG646072 v2.1
Healthy People. Healthy Communities.
April 21, 2022 FIRST CLASS and CERTIFIED MAIL - 9214 8969 0099 9790 14214650 48 Mr. George Lippard, VC Summer Site Vice President VC Summer Nuclear Station Off-Site Water System PO Box 88, Mail Code 800 Jenkinsville, SC 29065 Re: Consent Order 22-024-W VC Summer Nuclear Station Off-Site Water System NPDES Permit SCG646072 Fairfield County
Dear Mr. George Lippard:
Enclosed, please find fully executed Consent Order 22-024-W for the above referenced facility.
The Order is considered executed on April 21, 2022.
If you have any questions, please contact me at (803) 898-4262 or by e-mail at taylorhe@dhec.sc.gov.
Sincerely, Harold Taylor Ill, Enforcement Officer Bureau of Water - WP Control Division WP Compliance and Enforcement Section cc: Jacob Oblander, SCDHEC, WP Compliance Kristian Tucker, SCDHEC, WP Compliance SCDHEC Midlands Regional EQC Office Kayse Jarman, SCDHEC, Water Facilities Permitting Adam Cannon, SCDHEC, WP Enforcement Manager Attachment as stated S.C. Department of Health and Environmental Control 2600 £3..ill Street olL1m 1 J '> 2 J2C
THE STATE OF SOUTH CAROLINA BEFORE THE DEPARTMENT OF HEALTH AND ENVIRONMENTAL CONTROL IN RE: DOMINION ENERGY SC, INC VC SUMMER NUCLEAR STATION OFF-SITE WATER SYSTEM FAIRFIELD COUNTY CONSENT ORDER 22-024-1 The South Carolina Department of Health and .Environmental Control (Department) and Dominion Energy SC, Inc. (Dominion) have agreed to the issuance of this Consent Order to include the following Findings of Fact and Conclusions of Law.
FINDINGS OF FACT
- 1. Dominion owns and is responsible for the proper operation and maintenance of the VC Summer Nuclear Station Off-site Water System (VC Summer WWTF) located at 400 Brabham Boulevard, .in Fairfield County, South Carolina. VC Summer WWTF serves Dominion's VC Summer Nuclear Station.
- 2. The Department issued the National Pollutant Discharge Elimination System (NPDES)
Pennit SCG646072, authorizing VC Summer WWTF to discharge filter backwash to the Monticello Reservoir in accordance with effluent limitations, monitoring requirements and other permit conditions contained therein. The NP DES Permit became effective November 2, 2017 and has an expiration ~ate of December 30, 2020. The NPDES Permit is administratively continued due to an application for renewal of the permit being submitted at least one hundred eighty (180) days before the expiration of the permit.
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- 3. On November 9, 2021, Dominion emailed Department staff regarding operations at VC Sumnier WWTF. Dominion explained the laboratory servicing VC Summer WWTF has not been certified to perform total residual chlorine (TRC) since June 2018. Dominion explained the laboratory is in the process of being recertified for TRC, and until recertified, Dominion will use a certified vendor laboratory for TRC analysis.
- 4. On November 18, 2021, Department staff issued a Notice ofViolation (NOV) to Dominion for failure to use a South Carolina state certified laboratory for sampling and analysis of TRC for the June 2018 through September 2019, December 2019 through March 2020, October 2020, December 2020, February 2021, June 2021, and July 2021 monthly monitoring periods. The certified copy was delivered on November 22, 2021. No response w~s required because Dominion submitted an explanation of the violation November 9, 2021.
- 5. On January 6, 2022, Department staff issued a Notice of Alleged Violation. and Enforcement Conference (NOAV/EC) to Dominion via first class and certified mail. The NOAV/EC was delivered January I 0, 2022.
- 6. On January 24, 2022, Department staff held an enforcement conference with Dominion.
Dominion explained the state certification for TRC was purposefully terminated, but the termination of the certification was not communicated with laboratory personnel for Dominion. Dominion further explained laboratory staff were regularly performing quality control testing while in violation and since identification of the violations, Dominion has been using a South Carolina state certified contract laboratory for TRC measurements. The issuance of a Consent Order containing a civil penalty was discussed.
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CONCLUSIONS OF LAW Based upon the above Findings of Fact, the Department reaches the foll owing Conclusions ofLaw:
- 1. Dominion violated the Pollution Control Act, S.C. Code Ann. § 48-1-ll0(d), Water Pollution Control Permits Regulation S.C. Code Ann. Regs. 61-9.122.41(a) and (e)(l), and State Environmental Laboratory Certification Regulations, S.C. Code Ann. Regs 61-68, by failing to submit to the Deparment analytical results for TRC from a South Carolina certified laboratory as required by NPDES Permit SCG646072.
- 2. The Pollution Control Act, S.C. Code Ann. § 48-1-330, provides for a civil penalty not to exceed ten thousand dollars ($10,000.00) per day of violation for any person violating the Act or any rule, regulation, permit, permit condition, final determination, or Order of the Department.
NOW, THEREFORE, IT IS ORDERED, CONSENTED TO AND AGREED, pursuant to the Pollution Control Act, S.C. Code Ann. § 48-1-50 and 48-1-100, that Dominion shall:
I. Within fifteen (15) days of the execution date of this Order, submit to the Department documentation verifying Dominion has contracted with a South Carolina certified laboratory to perform sampling and analysis for TRC.
- 2. Pay to the Department, a civil penalty in the amount of four thousand eighty dollars
($4,080.00) within thirty (30) days of the execution date of this Order.
THE PARTIES FURTHER STIPULATE that Dominion shall pay a stipulated penalty in the amount of four thousand eighty dollars ($4,080.00) should it fail to comply. with any requirement 3
pursuant to this Consent Order. Such penalties shall be due and payable upon written notice to Dominion. The Department's determination that a requirement has not been met shall be final. All penalties due under this paragraph shall be made payable to the South Carolina Department of Health and Environmental Control within thirty (30) days of notification by the Department. The stipulated penalties set forth above shall be in addition to any other remedies or sanctions which may be available to the Department by reason of Dominion's failure to comply with any requirement of this Order.
PURSUANT TO THE ORDER, communications regarding this Order and its requirements, including civil penalty payments, shall be address as follows:
Harold ~i:.m, &fot:cemem Eroject Manager SCDHEC, Bureau of Water- WP Enforcement Section 2600 Bui] Street Columbia, South Carolina 29201 The Order number should be included on all checks remitted as payment of the civil penalty.
IT IS FURTHER ORDERED AND AGREED that failure to comply with any provision of this Order shall be grounds for further enforcement action pursuant to the Pollution Control Act, S.C.
Code Ann. § 48-1-330, to include the assessment of additional civil penalties.
IT IS FURTHER ORDERED AND AGREED that this Consent Order governs only the civil liability to the Department for civil sanctions arising from the matters set forth herein and constitutes the entire agreement between the Department and Dominion Energy SC, Inc, with respect to the resolution and settlement of these civil matters~ The parties are not relying upon any representations, promises, understandings or agreements except as expressly set forth within this Order.
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THE PARTIES UNDERSTAND that the "execution date" of the Order is the date the Order is signed by the Director of Environmental Affairs.
[Signature Page Follows]
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FOR THE SOUTH CAROLINA DEPARTMENT OF HEALTH AND ENVIRONMENTAL CONTROL M~
MyraC. e c_ _ :13-R.e,u _ Date: lf')2 ) I/2()22 Director of Environmental Affairs
~ Q(ef:j~ Date:_ ___.4_-...../_f_-~'Z.D
- ___,;.2_2_
Jeru&erR\lgbes, Chief Bureau of Water Date: '/-/fJ,-2()2,2-Rob Devlin, Assistant Chief Bureau of Water E*
Attorney Office of.Genera) Cmmsel 7="
WE CONSENT:
VC SUMMER NUCLEAR STATION OFF-SITE WATER SYSTEM 0 $ ~ Vice President 6
Digitally signed by:
nCORE test
- DISCHARGE MONITORING REPORT (DMR) Dal Re Facility Name : DOMINION EN ERGY SOUTH CAROLINA INC/V C SUMMER Permit Number : SC0030856 v3 . 5 Loe NUCLEAR STATION Permittee Name: DOMINION ENERGY SOUTH CAROLINA INC DMR Period : 12/1/2021 - 12/31/202 1 Limit Set: 06B1 No Discharge:
QUANTITY OR LOADING QUALITY OR CONCENTRATION NO. FREQUENCY SAMPLE PARAMETER EX. OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS Total Suspended Solids SAMPLE 0 Monthly Grab (00530) ***** ***** ***** 0 0 MEASUREMENT Effluent Gross (1) mg/L PERMIT ***** ***** ***** 30 98 Grab Lab ID: 40572 Monthly REQUIREMENT Monthly Average Dai l y Maximum
!Oil and Grease (00556) SAMPLE 0 Monthly Grab Effluent Gross (1) ***** ***** ***** 0 0 MEASUREMENT
- mg/L La b ID: 23105 PERM I T ***** ***** ***** 15 19 Grab Monthly REQUIREMENT Monthly Average Dai l y Maximum Flow (50050) 0 INSTANTA Effluent Gross (1) SAMPLE Monthly NEOUS MEASUREMENT 0.25800 0.25800 ***** ***** ***** IN Lab ID: 20001 MGD *****
INSTANTA REPORT PE RM IT REPORT ***** ***** ***** NEOUS Monthly Month l y REQUIREMEN T Daily Maximum IN Average DMR Instructions:
DMR Comments: Oil & Grease Method EPA 1664B , PQL 5.0 mg/L , number of times results below PQL one.
TS S Method SM 2540D- 20 1 1 , PQL 1 . 0 mg/L , number of times results below PQL = one .
Limit Set: 0071 No Discharge :
NAME/ TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law t hat thi s document and all attachments w ere TELEPHONE DATE prepared under my direction or supervision in accordance w ith a system designed to assure t hat qualified personnel properly gather and evaluate th e information submitted. Base d on my inquiry of th e person or persons who manage th e system, or those persons directly respon sible for gat hering th e information, t he information subm itted is, to the best of my know ledge and belief, true, accurat e, and compl ete. I am aware th at th ere are significa nt SIGNATURE OF PRINCIPAL EXECUTIVE AREA NUMBER YEAR MO DAY penalties for subm itting false information, including the possibi lity of fi ne and OFFICER OR AUTHORIZED AGENT CODE rTYPED OR PRINTED imprisonment for knowing violation s.
Permit Number: SC0030856 v3.5 Generated : 1/28/2022 5 : 03 PM Page 1 of 9
DISCHARGE MONITORING REPORT {DMR)
Facility Name: DOMINION ENERGY SOUTH CAROLINA INC/V C SUMMER Permit Number: SC0030856 v3 . 5 NUCLEAR STATION Permittee Name: DOMINION ENERGY SOUTH CAROLINA I NC DMR Period: 12/1/2021 - 12/31/2021 QUANTITY OR LOADING QUALITY OR CONCENTRATION NO. FREQUENCY SAMPLE PARAMETER EX. OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS Total Suspended Solids SAMPLE 0 Monthly Grab (00530) ***** ***** ***** 3.5 3 .5 MEASUREMENT
~ffluent Gross (1)
- mg/L PERMIT ***** ***** ***** 30 100 Grab Lab ID: 20001 Monthly REQUIREMENT Monthly Average Daily Maximum Piland Grease (00556) SAMPLE 0 Monthly Grab Effluent Gross (1) ***** ***** ***** 0 0 MEASUREMENT
- mg/L Lab ID: 23105 PERMIT ***** ***** ***** 15 20 Grab Monthly REQUIREMENT Monthly Average Daily Maximum Flow (50050) 0 INSTANTA Three per Effluent Gross (1) SAMPLE NEOUS MEASUREMENT 0.0933 0.144900 ***** ***** ***** Discharge IN Lab ID: 20001 MGD *****
INSTANTA REPORT PERMIT REPORT ***** ***** ***** NEOUS Monthly Monthly REQUIREMENT Daily Max imum IN Average DMR Instructions:
DMR Comments: Oil & Grease Method EPA 1664B , PQL 5.0 mg /L , number of times results below PQL one.
Limit Set: 0011 No Discharge:
QUANTITY OR LOADING QUALITY OR CONCENTRATION NO. FREQUENCY SAMPLE PARAMETER EX. OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS Temperature (F) 0 Cont i nuo u Continue SAMPLE ***** deg F (00011) ***** ***** ***** 76.70 94 . 63 s us MEASUREMENT I I I I I NAME/TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law that this document and all attachments were TELEPHONE DATE prepared under my direction or supervision in accordance with a system designed to assure that qualified personnel properly gather and evaluate the information submitted. Based on my inquiry of the person or persons who manage the system, or those persons directly responsible for gathering the information, the information submitted is, to the best of my knowledge and belief, true, accurate, and complete. I am aware that there are significant penalties for submitting false information, including the possibility of fine and SIGNATURE OF PRINCIPAL EXECUTIVE
~FFICER OR AUTHORIZED AGENT AREA CODE I NUMBER YEAR MO DAY TYPED OR PRINTED imprisonment for knowing violations.
Permit Number: SC0030856 v3.5 Generated : 1/28/2022 5 : 03 PM Page 2 of 9
DISCHARGE MONITORING REPORT (DMR)
Facility Name : DOMINION ENERGY SOUTH CAROLINA INC/V C SUMMER Permit Number: SC0030856 v3 . 5 NUCLEAR STATION Permittee Name: DOMINION ENERGY SOUTH CAROLINA INC DMR Period: 12/1/2021 - 12/31/2021 QUANTITY OR LOADING QUALITY OR CONCENTRATION NO. FREQUENCY SAMPLE PARAMETER EX. OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS Effluent Gross (1)
PERMIT ***** ***** ***** REPORT 113 Continuou Continue Lab ID: 20001 REQUIREMENT Monthly Average Daily Maximum us s
Temperature (F) 0 Continuou Continue SAMPLE 57.23 (00011) ***** ***** ***** 58.49 s us MEASUREMENT Intake from Stream (7)
- deg F Lab ID: 2 0001 PERMIT ***** ***** ***** REPORT REPORT Continuou Continue REQUIREMENT Monthly Average Daily Maximum s us pH (00400) SAMPLE 0 Monthly Grab Effluent Gross (1) ***** ***** 7 . 11 ***** 7 .11 MEASUREMENT
- SU Lab ID : 20001 6.0 8.5 PERMIT ***** ***** ***** Grab Instantaneous Instantaneous Monthly REQUIREMENT Minimum Maximum Flow (50050) 0 Continuou Continue SAMPLE 492.47 492.47 Effluent Gross (1) MEASUREMENT ***** ***** ***** s us MGD *****
Lab ID: 20001 REPORT PERMIT REPORT ***** ***** ***** Continuou Continue Monthly us REQUIREMENT Daily Maximum s Average BROMIDE (71870) SAMPLE 0 Monthly Grab Effluent Gross (1) ***** ***** ***** 0 0 MEASUREMENT
- mg/L Lab ID: 23105 PERMIT ***** ***** ***** REPORT REPORT Grab Monthly REQUIREMENT Monthly Average Daily Maximum DMR Instructions: MLOC 1 - DISCHARGE TEMPERATURE DISCHARGE SAMPLES SHALL BE COLLECTED AFTER THE COMBINATION OF ALL WASTE STREAMS BUT PRIOR TO MIXING WITH THE RECEIVING STREAM . MLOC 7 - INTAKE TEMP= SHALL BE MONITORED ON THE INLET SIDE OF THE MAIN CONDENSER.
DMR Comments : Bromide Method EPA 300 . 0, PQL 0 . 5 mg/L, number of times results below PQL = one.
NAME/TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law that this document and al l attachments were TELEPHONE DATE prepared under my direction or supervi sion in accordance with a system designed to assure that qualified personnel properly gather and eva luate the information submitted. Based on my inquiry of the person or persons who manage th e system, or those persons directly responsible for gath ering t he information, the informatio n submitted is, to th e best of my knowledge and belief, true, accurate, and complete. I am aware th at th ere are significant SIGNATURE OF PRINCIPAL EXECUTIVE AREA NUMBER YEAR MO DAY penalties for submitting fa lse information, including t he possibility of fi ne and OFFICER OR AUTHORIZED AGENT CODE TYPED OR PRINTED imprisonment for knowing violations.
Permit Number: SC0030856 v3 . 5 Generated : 1/28/2022 5 : 03 PM Page 3 of 9
DISCHARGE MONITORING REPORT (DMR)
Faci1ity Name: DOMINION ENERGY SOUTH CAROLINA INC/V C SUMMER Permit Number: SC0030856 v3.5 NUCLEAR STATION Permittee Name: DOMINION ENERGY SOUTH CAROLINA I NC DMR Period: 12/1/2021 - 12/31/2021 Limit Set: 0041 No Discharge:
QUANTITY OR LOADING QUALITY OR CONCENTRATION NO. FREQUENCY SAMPLE PARAMETER EX. OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS Total Suspended Solids SAMPLE 0 Monthly 2.9 2.9 Grab (00530) MEASUREMENT ***** ***** *****
Effluent Gross (1) mg/L PERMIT ***** ***** ***** 30 100 Grab Lab ID: 20001 Monthly REQUIREMENT Monthly Average Daily Maximum K)il and Grease (00556) SAMPLE 0 Monthly Grab Effluent Gross (1) ***** ***** ***** 0 0 MEASUREMENT
- mg/L Lab ID: 23105 PERMIT ***** ***** ***** 15 20 Grab Monthly REQUIREMENT Monthly Average Daily Maximum Flow (50050) 0 Calculat SAMPLE Monthly Effluent Gross (1) 0.189324 0.189324 ***** ***** ***** ion MEASUREMENT MGD *****
Lab ID: 20001 REPORT Calculat PERMIT REPORT ***** ***** *****
Monthl y Monthly ion REQU IREMENT Daily Maximum Ave ra ge DMR Instructions: FLOW= SHALL BE THE SUM OF THE FLOWS FROM EACH CONTINUOUSLY MON ITORED STEAM GENERATOR BLOWDOWN LINE.
DMR Comments : Oi l & Grease Method EPA 1664B , PQL 5 . 0 mg/L, number of times results below PQL = one .
Limit Set: 0141 No Discharge:
QUANTITY OR LOADING QUALITY OR CONCENTRATION NO. FREQUENCY SAMPLE PARAMETER EX. OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS rH (00400)
SAMPLE ***** SU 1 Twice per Grab Efflu ent Gross (1) ***** ***** 8.36 ***** 8.8 Month MEASUREMENT I I I I I NAME/TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law that this document and all attachments were TELEPHONE DATE prepared under my direction or supervision in accordance with a system designed to assure that qualified personnel properly gather and evaluate the information submitted. Based on my inquiry of the person or persons who manage the system, or those persons directly responsible for gathering the information, the information submitted is, to the best of my knowledge and belief, true, accurate, and complete. I am aware that there are significant !SIGNATURE OF PRINCIPAL EXECUTIVE AREA NUMBER YEAR MO DAY penalties for submitting false information, including the possibility of fi ne and K)FFICER OR AUTHORIZED AGENT CODE rrvPED OR PRINTED imprisonment for knowing violations.
Permit Number: SC0030856 v3 . 5 Generated : 1/28/2022 5 : 03 PM Page 4 of 9
DISCHARGE MONITORING REPORT (DMR)
Faci1ity Name : DOMINION ENERGY SOUTH CAROLINA INC/V C SUMMER Permit Number: SC0030856 v3.5 NUCLEAR STATION Permittee Name: DOMINION ENERGY SOUTH CAROLINA INC DMR Period: 12/1/2021 - 12/31/2021 QUANTITY OR LOADING QUALITY OR CONCENTRATION NO. FREQUENCY SAMPLE PARAMETER EX . OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS 6.0 8.5 Lab ID: 20001 PERMIT ***** ***** ***** Grab Instantaneous Instantaneous Monthly REQUIREMENT Minimum Maximum rrotal Phosphorus (as SAMPLE 0 Monthly Grab P) (00665) ***** ***** ***** 0.29 0.29 MEASUREMENT Effluent Gross (1) mg/L PERMIT ***** ***** ***** REPORT REPORT Grab Lab ID: 23105 Monthly REQUI~EMENT Monthly Average _Daily Maximum Flow (50050) 0 Continuou Continue SAMPLE Effluent Gross (1) 0.135732 0.350045 ***** ***** ***** s us MEASUREMENT MGD *****
Lab ID: 20001 REPORT PERMIT REPORT Continue Monthly ***** ***** ***** Continuou us REQUIREMENT Daily Maximum s Average DMR Instructions :
DMR Comments: COMMENT and EXPLANATION of EXCEEDANCE for OUTFALL 014 A grab compliance pH sample of 8 . 8 su was obtained from Outfall 014 and a backup aliquot had the same results from the December 3, 2021 NPDES sampling event . Because the sample results were not indicative of the discharged stream , Chemistry personnel suspected the initial and backup samples were contaminated. Upon investigation , it was determined that the telescoping sample cup was used to check the water quality at Outfall 006B during cleanup efforts for the November 16 , 2021 transformer oil spill. VCS believes the initial pH sample result is due to cross contamination introduced by using the same telescoping sample cup to obtain the monthly sample for Outfall 014 .
A new telescoping sample cup was used an hour later to obtain another sample and another aliquot using what was analyzed using another pH meter . The first sample with the new apparatus was 8 . 36 su and the second aliquot result was 8.39 su . This occurrence has been documented in the station's corrective action program (CR 03611) .
NAME/TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law that this document and all attachments were TELEPHONE DATE prepared under my direction or supervision in accordance with a system designed to assure that qualified personnel properly gather and evaluate the information submitted. Based on my inquiry of the person or persons who manage the system, or those persons directly responsible for gathering the information, the information submitted is, to the best of my knowledge and belief, true, accurate, and complete. I am aware that there are significant $1GNA TURE OF PRINCIPAL EXECUTIVE AREA NUMBER YEAR MO DAY penalties for submitting fal se information, including the possibility of fin e and PFFICER OR AUTHORIZED AGENT CODE rrvPED OR PRINTED imprisonment for knowing violations.
Permit Number: SC0030856 v3 . 5 Generated: 1/28/2022 5:03 PM Page 5 of 9
DISCHARGE MONITORING REPORT (DMR)
Facility Name: DOMINION ENERGY SOUTH CAROLINA INC/V C SUMMER Permit Number: SC0030856 v3.5 NUCLEAR STATION Permittee Name: DOMINION ENERGY SOUTH CAROLINA INC DMR Period : 12/1/2021 - 12/31/2021 Since VCS cannot invalidate the original 8.8 su pH due to the analytical methodology, VCS is reporting this value as an exceedance of the Daily Maximum Limit of 8.5 su. However, the second compliance sample result of 8 . 36 su is being reported as the monthly minimum value since pH values cannot be averaged. The result is within the permit limit of 6.0 su. VCS is not reporting the second aliquots as these were taken for method verification purposes consistent with SCDHEC guidance .
- DMR Value Comments:
- pH , Effluent Gross (1), Limit: 8 .5 Instantaneous Maximum, Reported Value: 8 . 8, Comment: Suspected sample container cross contamination . See General Report Comments for full details.
Limit Set: 0031 No Discharge:
QUANTITY OR LOADING QUALITY OR CONCENTRATION NO . FREQUENCY SAMPLE PARAMETER EX . OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS pH (00400) 0 Once per SAMPLE Grab Effluent Gross (1) ***** ***** 7.42 ***** 7.86 Discharge MEASUREMENT
- SU Lab ID: 20001 6.0 9.0 PERMIT ***** ***** Instantaneous ***** Instantaneous Monthly Grab REQUIREMENT Minimum Maximum Total Suspended Solids 0 Twice per SAMPLE Grab (00530) ***** ***** ***** 0 0 Month MEASUREMENT Effluent Gross (1)
- mg/L Lab ID: 20001 PERMIT ***** ***** ***** 30 100 Grab Monthly REQUIREMENT Monthly Average Daily Maximum Oil and Grease (00556) 0 Twi c e per SAMPLE Grab Effluent Gross (1) ***** ***** ***** 0 0 Month MEASUREMENT
- mg/L Lab ID : 10120 PERMIT ***** ***** ***** 15 20 Grab Monthly REQUIREMENT Monthly Average Daily Max imum NAME/TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law that this document and all attachments were TELEPHONE DATE prepared under my direction or supervision in accordance wit h a system designed to assure that qualified personnel properly gather and evalua te t he information submitted. Based on my inquiry of the person or persons who manage the system, or those persons directly responsible for gathering the information, the information submitted is, to the best of my knowledge and belief, true, accurate, and complete. I am aware that there are significant lslGNATURE OF PRINCIPAL EXECUTIVE AREA NUMBER YEAR MO DAY penalties for su bmitting fa lse information, incl uding the possibi lity of fi ne and loFFICER OR AUTHORIZED AGENT CODE
[TYPED OR PRINTED imprisonment for knowing violations.
Permit Number: SC0030856 v3.5 Generated : 1/28/2022 5 : 03 PM Page 6 of 9
DISCHARGE MONITORING REPORT (DMR)
Faci1ity Name : DOMINION ENERGY SOUTH CAROLINA INC/V C SUMMER Permit Number: SC0030856 v3 . 5 NUCLEAR STATION Permittee Name: DOMINION ENERGY SOUTH CAROLINA I NC DMR Period: 12/1/2021 - 12/31/2021 QUANTITY OR LOADING QUALITY OR CONCENTRATION NO . FREQUENCY SAMPLE PARAMETER EX. OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS Flow (50050) 0 Once per ESTIMATE SAMPLE Effluent Gross (1)
MEASUREMENT 0 . 004 1 8 1 0 . 004200 ***** ***** ***** Discharge ES Lab ID : 20001 MGD *****
REPORT ESTIMATE PERMIT Monthly REPORT ***** ***** ***** Monthly ES REQUIREMENT Daily Maximum Average DMR Instructions:
DMR Comments: Total Suspended Solids Method SM2540D , PQL 1 . 0 mg/L , number of times result less than PQL two .
Oil & Grease Method EPA 1664B , PQL 5.0 mg/L , number of times results below PQL = two .
Limit Set: 0051 No Discharge:
QUANTITY OR LOADING QUALITY OR CONCENTRATION NO . FREQUENCY SAMPLE PARAMETER EX . OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS BOD - 5 DAY (20 0 24 - Hr DEGREES C) (00310) SAMPLE Monthly Composit
- ***** ***** 9.8 9.8 Effluent Gross (1) MEASUREMENT e
- mg/L Lab ID: 40572 24 - Hr PERMIT ***** ***** ***** 30 45 Composit Monthly REQUIREMENT Monthly Average Daily Maximum e Total Suspended Solids 0 24 - Hr (00530) SAMPLE Monthly Composit
- ***** ***** 6.7 6.7 Effluent Gross (1) MEASUREMENT e
- mg/L Lab ID: 40572 24 - Hr PERMIT ***** ***** ***** 30 45 Composit Mo n thly REQUIREMENT Monthly Average Dai l y Maximum e NAME/TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law that this document and all attachments w ere TELEPHONE DATE pre pared under my direction or supervision in accordance with a system designed to assure that qualified personnel properly gather and evaluate t he information submitted . Based on my inquiry of the person or persons who manage the system, or those persons directly responsib le for gathering the information, the informat ion submitted is, to the best of my knowledge and belief, true, accurate, and complete. I am aware that there are sign ificant pena lties for submitting fa lse information, includ ing the possibility of fine and lslGNATURE OF PRINCIPAL EXECUTIVE OFFICER OR AUTHORIZED AGENT AREA CODE I NUMBER YEAR MO DAY TYPED OR PRINTED imprisonment for knowing violations.
Permit Number : SC0030856 v3 . 5 Generated: 1/28/2022 5:03 PM Page 7 o f 9
DISCHARGE MONITORING REPORT (DMR)
Facility Name: DOMINION ENERGY SOUTH CAROLINA INC/V C SUMMER Permit Number: SC0030856 v3.5 NUCLEAR STATION Permittee Name : DOMINION ENERGY SOUTH CAROLINA INC DMR Period: 12/1/2021 - 12/31/2021 QUANTITY OR LOADING QUALITY OR CONCENTRATION NO . FREQUENCY SAMPLE PARAMETER EX . OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS Flow (50050) 0 INSTANTA Effluent Gross (1) SAMPLE Monthly NEOUS 0.00700 0.00700 ***** ***** *****
MEASUREMENT IN Lab ID: 20001 MGD *****
INSTANTA REPORT PERMIT REPORT ***** ***** ***** NEOUS Monthly Monthly REQUIREMENT Daily Maximum IN Average IE. COLI (MPN/l00ML) SAMPLE 0 Monthly Grab (51040) ***** ***** ***** < 10 <10 MEASUREMENT Effluent Gross (1) #/l00mL 126 PERMIT ***** ***** ***** 349 Grab Lab ID : 40572 30 Day Average Monthly REQUIREMENT Daily Maximum Geometric DMR Instructions:
DMR Comments: (none)
Limit Set: 06Al No Discharge:
QUANTITY OR LOADING QUALITY OR CONCENTRATION NO . FREQUENCY SAMPLE PARAMETER EX. OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS Total Suspended Solids SAMPLE 0 Monthly Grab (00530) ***** ***** ***** 0 0 MEASUREMENT Effluent Gross (1) mg/L PERMIT ***** ***** ***** 30 100 Grab Lab ID: 40572 Monthly REQUIREMENT Monthly Average Daily Maximum Oil and Grease (00556) SAMPLE mg/L 0 Monthly Grab
- ***** ***** ***** 0 0 Effluent Gross (1) MEASUREMENT NAME/TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law that this document and all attachments were TELEPHONE DATE prepared under my direction or supervision in accordance with a system designed to assure that qualified personnel properly gather and evaluate the information submitted. Based on my inquiry of the person or persons who manage the system, or those persons directly responsible for gathering the information, the information submitted is, to the best of my knowledge and belief, true, accurate, and complete. I am aware that there are significant penalties for submitting false information, including the possibility of fin e and SIGNATURE OF PRINCIPAL EXECUTIVE loFFICER OR AUTHORIZED AGENT AREA CODE I NUMBER YEAR MO DAY rTYPED OR PRINTED imprisonment for knowing violations.
Permit Number: SC0030856 v3 . 5 Generated: 1/28/2022 5 : 03 PM Page 8 of 9
DISCHARGE MONITORING REPORT {DMR)
Faci1ity Name: DOMINION ENERGY SOUTH CAROLINA INC/V C SUMMER Permit Number : SC0030856 v3 . 5 NUCLEAR STATION Permittee Name: DOMINION ENERGY SOUTH CAROLINA INC DMR Period : 12/1/2021 - 12/31/2021 QUANTITY OR LOADING QUALITY OR CONCENTRATION NO. FREQUENCY SAMPLE PARAMETER EX. OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS Lab ID: 23105 PERMIT ***** ***** ***** 15 20 Grab Monthly REQUIREMENT Monthly Average Daily Maximum Flow (50050) 0 INSTANTA Effluent Gross (1) SAMPLE Monthly NEOUS 0.016500 0.016500 ***** ***** *****
MEASUREMENT IN Lab ID: 20001 MGD *****
INSTANTA REPORT PERMIT REPORT ***** ***** ***** NEOUS Monthly Monthly REQUIREMENT Daily Maximum IN Average DMR Instructions:
DMR Comments : TSS Method SM2540D- 2011 , PQL=lmg/L, number of times results below PQL = one Oil & Grease Method EPA 16648 , PQL 5.0 mg/L, number of times results below PQL = one.
Limit Set: 0081 No Discharge: Y QUANTITY OR LOADING QUALITY OR CONCENTRATION NO . FREQUENCY SAMPLE PARAMETER EX . OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS rrotal Suspended Solids SAMPLE Monthly Grab (00530) MEASUREMENT ***** ***** ***** ***** *****
Effluent Gross (1) mg/L PERMIT ***** ***** ***** 30 100 Grab Lab ID: Monthly REQUIREMENT Monthly Average Dai l y Maximum Pil and Grease (00556) SAMPLE mg/L Monthly Grab Effluent Gross (1) MEASUREMENT ***** ***** *****
NAME/TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law that this document and all attachments were TELEPHONE DATE prepared under my direction or supervision in accordance with a system designed to assure that qualified personnel properly gather and evalua te the information submitted. Based on my inquiry of the person or persons who manage the system, or those persons directly responsible for gathering the information, the inform ation submitted is, to the best of my knowledge and belief, tru e, accurate, and complete. I am aware that there are significa nt penalties for submitting false information, incl ud ing the possibility of fi ne and
!SIGNATURE OF PRINCIPAL EXECUTNE PFFICER OR AUTHORIZED AGENT AREA CODE I NUMBER YEAR MO DAY
!TYPED OR PRINTED imprisonment for knowing violat ions.
Permit Number: SC0030856 v3 . 5 Generated : 1/28/2022 5 : 03 PM Page 9 of 9
DISCHARGE MONITORING REPORT (DMR)
Facility Name: DOMINION ENERGY SOUTH CAROLINA INC/V C SUMMER Permit Number: SC0030856 v3 . 5 NUCLEAR STATION Permittee Name: DOMINION ENERGY SOUTH CAROLINA INC DMR Period: 12/1/2021 - 12/31/2021 QUANTITY OR LOADING QUALITY OR CONCENTRATION NO. FREQUENCY SAMPLE PARAMETER EX . OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS Lab ID: PERMIT ***** ***** ***** 15 20 Grab Monthly REQUIREMENT Monthly Average Daily Maximum Total Copper (01042) SAMPLE Monthly Grab Effluent Gross (1) MEASUREMENT ***** ***** ***** ***** *****
- mg/L Lab ID :
PERMIT ***** ***** ***** 1.0 1.0 Grab Monthly REQUIREMENT Monthly Average Daily Maximum Total Iron (01045) SAMPLE Monthly Grab Effluent Gross (1) MEASUREMENT ***** ***** ***** ***** *****
- mg/L Lab ID:
PERMIT ***** ***** ***** 1.0 1.0 Grab Monthly REQU IREMENT Monthly Average Daily Maximum Flow (50050) INSTANTA Effluent Gross ( 1 ) SAMPLE Monthly NEOUS MEASUREMENT ***** ***** ***** ***** ***** IN Lab ID: MGD *****
INSTANTA REPORT PERMIT REPORT ***** ***** ***** NEOUS Monthly Monthly REQUIREMENT Daily Max imum IN Average DMR Instructions: COPPER & IRON - SAMPLING IS REQUIRED ONLY WHEN CHEMICAL METAL CLEAING WASTES ARE DISCHARGED. REPORT ' CONDITONAL' ON THE DMR FORM WHEN CHEMICAL METAL CLEANING WASTES ARE NOT DISCHARGED DURING THE MONI TORING PERIOD .
DMR Comments: (none)
NAME/TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law that this document and all attachments were TELEPHONE DATE prepared under my direction or supervision in accordance with a system designed to assure that qualified personnel properly gather and evaluate the information submitted. Based on my inquiry of the person or persons who manage the system, or those persons directly responsible for gathering the information, the information submitted is, to the best of my knowledge and belief, true, accurate, and complete. I am aware that there are significant SIGNATURE OF PRINCIPAL EXECUTIVE AREA NUMBER YEAR MO DAY penalties for submitting false information, including the possibility of fi ne and OFFICER OR AUTHORIZED AGENT CODE TYPED OR PRINTED imprisonment for knowing violations.
Permit Number: SC0030856 v3 . 5 Generated : 1/28/2022 5 : 03 PM Page 10 of 9
Digitally signecib
- nCORE test.wind Oat DISCHARGE MONITORING REPORT (DMR) Re Faci1ity Name: DOMINION ENERGY SOUTH CAROLINA INC/V C SUMMER Permit Number: SC0030856 v3.5 Loe a NUCLEAR STATION Permittee Name: DOM I NION ENERGY SOUTH CAROLINA INC DMR Period : 3/1/2022 - 3/31/2022 Limit Set: 06B1 No Discharge:
QUANTITY OR LOADING QUALITY OR CONCENTRATION NO. FREQUENCY SAMPLE PARAMETER EX. OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS
~otal Suspended Solids SAMPLE 1 Monthly Grab (00530) ***** ***** ***** 32 . 6 32.6 MEASUREMENT Effluent Gross (1) mg/L PERMIT ***** ***** ***** 30 98 Grab Lab ID: 23105 Monthly REQUIREMENT Monthly Average Daily Maximum Pil and Grease (00556) SAMPLE 0 Monthly Grab Effluent Gross (1) ***** ***** ***** 5.4 5.4 MEASUREMENT
- mg/L Lab ID: 23105 PERMIT ***** ***** ***** 15 19 Grab Monthly REQUIREMENT Monthly Average Daily Maximum Flow (50050) 0 INSTANTA
~ffluent Gross (1) SAMPLE Monthly NEOUS MEASUREMENT
- 0. 011800 0.011800 ***** ***** ***** IN Lab ID: 20001 MGD *****
INSTANTA REPORT PERMIT Monthly REPORT ***** ***** ***** Monthly NEOUS REQUIREMENT Daily Maximum IN Average DMR Instructions:
DMR Comments: Oil & Grease Method EPA 1664B, PQL 5 . 0 mg/L, number of times results below PQL one .
TSS - Analysis of a grab sample of 06B on 3/7 yielded a TSS value of 32 . 6 ppm . Delays in receiving and reviewing the vendor data resulted in a missed opportunity for additional samples during the month , yielding an exceedance of the monthly average limit of 30mg/l . This higher than normal TSS value is believed to be an anomaly as results from the previous 4 years do not exceed 15 ppm . In addition, the RPO between the sample/duplicate or matrix spike/spike duplicate was not within control limits due to matrix interference .
NAME/TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law that this document and all attachments were TELEPHONE DATE prepared under my direction or supervision in accordance with a system designed to assure that qualifie d personnel properly gather and evaluate the information submitted. Based on my inquiry of the person or persons who manage the system, or those persons directly responsible for gathering the information, the information subm itted is, to the best of my knowledge and belief, true, accurate, and complete. I am aware that th ere are significant SIGNATURE OF PRINCIPAL EXECUTIVE AREA NUMBER YEAR MO DAY penalties for submitting false information, including the possibility of fi ne and bFFICER OR AUTHORIZED AGENT CODE rrYPED OR PRINTED imprisonment for knowing violations.
Permit Number: SC0030856 v3 . 5 Generated: 4/28/2022 9 : 58 AM Page 1 of 9
DISCHARGE MONITORING REPORT (DMR)
Facility Name : DOMINION ENERGY SOUTH CAROLINA INC/V C SUMMER Permit Number : SC0030856 v3.5 NUCLEAR STATION Permittee Name: DOMINION ENERGY SOUTH CAROL I NA INC DMR Period: 3/1/2022 - 3/31/2022 A follow - up analysis of a grab sample of 06B on 4/4 yielded 6.7 ppm.
- DMR Value Comments:
- Total Suspended Solids , Effluent Gross (1) , Limit : 30 Monthly Average , Reported Value : 32 . 6 , Comment : An explanation for this higher than normal TSS value is noted in the General Report Comments Section.
Limit Set: 0071 No Discharge:
QUANTITY OR LOADING QUALITY OR CONCENTRATION NO. FREQUENCY SAMPLE PARAMETER EX. OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS Total Suspended Solids SAMPLE 0 Monthly Grab (00530) ***** ***** ***** 3 3 MEASUREMENT Effluent Gross (1 ) mg/L PERMIT ***** ***** ***** 30 100 Grab Lab ID: 20001 Monthly REQUIREMENT Monthly Average Dai ly Maximum Oil and Grease (00556) SAMPLE 0 Monthly Grab Effluent Gross (1) ***** ***** ***** 0 0 MEASUREMENT
- mg/L Lab ID: 23105 PERMIT ***** ***** ***** 15 20 Grab Monthly REQUIREMENT Monthly Average Daily Maximum Flow (50050) 0 INSTANTA Effluent Gross (1) SAMPLE Monthly NEOUS MEASUREMENT 0.090000 0.090000 ***** ***** ***** IN Lab ID: 20001 MGD *****
INSTANTA REPORT PERMIT REPORT ***** ***** ***** NEOUS Monthly Monthly REQUIREMENT Daily Maximum IN Average DMR Instructions:
DMR Comments : Oil & Grease Method EPA 1664B , PQL 5 . 0 mg/L, number of times results below PQL one .
NAME/ TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law that this document and all attachments were TELEPHONE DATE prepared under my direction or supervision in accordance with a system designed to assure that qualified personnel properly gather and evaluate the information submitted. Based on my inquiry of the person or persons who manage th e system, or those persons directly responsible for gathering the information, the information submitted is, to the best of my knowledge and belief, true, accurate, and complete. I am aware that there are significant SIGNATURE OF PRINCIPAL EXECUTIVE AREA NUMBER YEAR MO DAY penalties for submitting fal se information, including the possibility of fi ne and OFFICER OR AUTHORIZED AGENT CODE TYPED OR PRINTED imprisonment for knowing violations.
Permit Number: SC0030856 v3 . 5 Generated : 4/28/2022 9:58 AM Page 2 of 9
DISCHARGE MONITORING REPORT (DMR)
Faci1ity Name: DOMINION ENERGY SOUTH CAROLINA INC/V C SUMMER Permit Number: SC0030856 v3 . 5 NUCLEAR STATION Permittee Name: DOMINION ENERGY SOUTH CAROLINA INC DMR Period: 3/1/2022 - 3/31/2022 Limit Set: 0011 No Discharge:
QUANTITY OR LOADING QUALITY OR CONCENTRATION NO. FREQUENCY SAMPLE PARAMETER EX. OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS rremperature (F) 0 Continuou Continue SAMPLE (00011)
MEASUREMENT ***** ***** ***** 83 . 56 87.06 s us Effluent Gross ( 1)
- deg F PERMIT REPORT Continue Lab ID : 20001 ***** ***** ***** 113 Co nt inuou us REQUIREMENT Monthly Average Daily Maximum s rremperature (F) 0 Continuou Continue SAMPLE (00011) ***** ***** ***** 58.24 61. 39 s us MEASUREMENT Intake from Stream (7)
- deg F PERMIT REPORT REPORT Continue Lab ID: 20001 ***** ***** ***** Continuou us REQUIREMENT Monthly Average Daily Maximum s pH (00400) SAMPLE 0 Monthly
- 7. 71 Grab Effluent Gross (1) MEASUREMENT ***** ***** ***** 7. 71 Lab ID: 20001
- SU 6.0 8.5 PERMIT ***** ***** ***** Grab Instantaneous Instantaneous Monthly REQU IREMENT Minimum Maximum Flow (50050) 0 Continuou Continue SAMPLE Effluent Gross (1) 738. 72 738 . 72 ***** ***** ***** s us MEASUREMENT MGD *****
Lab ID: 20001 REPORT Continue PERM IT REPORT ***** ***** ***** Continuou Monthly us REQUIREMENT Daily Maximum s Average BROMIDE (71870) SAMPLE 0 Monthly Grab Effluent Gross (1) MEASUREMENT ***** ***** ***** 0 0
- mg/L Lab ID : 23105 PERMIT ***** ***** ***** REPORT REPORT Grab Monthly REQUIREMENT Monthly Average Daily Maximum NAME/TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law that this document and all attachments were TELEPHONE DATE prepared under my direct ion or supervision in accordance with a system designed to assure that qualified personnel properly gather and evaluate the information submitted. Based on my inquiry of the person or persons who manage the system, or those persons directly responsible for gathering the information, the information submitted is, to the best of my knowledge and belief, true, accurate, and complete. I am aware that there are significant SIGNATURE OF PRINCIPAL EXECUTIVE AREA NUMBER YEAR MO DAY penalties for submitting false information, including the possibility of fi ne and OFFICER OR AUTHORIZED AGENT CODE TYPED OR PRINTED imprisonment for knowing violations.
Permit Number: SC0030856 v3 . 5 Generated: 4/28/2022 9 : 58 AM Page 3 of 9
DISCHARGE MONITORING REPORT (DMR)
Faci1ity Name: DOMINION ENERGY SOUTH CAROLINA INC/V C SUMMER Permit Number : SC0030856 v3 . 5 NUCLEAR STATION Permittee Name: DOMINION ENERGY SOUTH CAROLI NA INC DMR Period: 3/1/2022 - 3/31/2022 DMR Instructions: MLOC 1 -D ISCHARGE TEMPERATURE DISCHARGE SAMPLES SHALL BE COLLECTED AFTER THE COMBINATION OF ALL WAS TE STREAMS BUT PRIOR TO MIXING WITH THE RECEIVING STREAM . MLOC 7 - INTAKE TEMP= SHALL BE MONITORED ON THE INLET SIDE OF THE MAIN CONDENSER .
DMR Comments: Bromide Method EPA 300 . 0 , PQL 1 . 0 mg/L, number of times results below PQL = one .
Limit Set: 0041 No Discharge: Y QUANTITY OR LOADING QUALITY OR CONCENTRATION NO. FREQUENCY SAMPLE PARAMETER EX. OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS Total Suspended Solids SAMPLE Monthly Grab (00530) MEASUREMENT ***** ***** ***** ***** *****
Effluent Gross (1)
- mg/L PERMIT ***** ***** ***** 30 100 Grab Lab ID: Monthly REQUIREMENT Monthly Average Daily Maximum Oil and Grease (00556) SAMPLE Monthly Grab Effluent Gross (1) MEASUREMENT ***** ***** ***** ***** *****
- mg/L Lab ID:
PERMIT ***** ***** ***** 15 20 Grab Monthly REQUIREMENT Monthly Average Daily Maximum Flow (50050) Calculat SAMPLE Monthly Effluent Gross (1)
MEASUREMENT ***** ***** ***** ***** ***** ion MGD *****
Lab ID: REPORT Calculat PERMIT REPORT ***** ***** *****
Monthly Monthly ion REQUIREMENT Daily Maximum Average DMR Instructions: FLOW SHALL BE THE SUM OF THE FLOWS FROM EACH CONTINUOUSLY MONITORED STEAM GENERATOR BLOWDOWN LINE.
DMR Comments: (none)
Limit Set: 0141 No Discharge:
NAME/ TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law that this document and all attachments were TELEPHONE DATE prepared under my direction or supervision in accordance with a system designed to assure that qualified personnel properly gather and evaluate the information submitted. Based on my inquiry of the person or persons who manage the system, or those persons directly responsible for gathering the information, the information submitted is, to the best of my knowledge and belief, true, accurate, and compl ete. I am aware that there are significant SIGNATURE OF PRINCIPAL EXECUTIVE AREA NUMBER YEAR MO DAY penal ties for submitting false information, including the possibil ity of fine and OFFICER OR AUTHORIZED AGENT CODE TYPED OR PRINTED imprisonment for knowing violations.
Permit Number: SC0030856 v3.5 Generated : 4/28/2022 9:58 AM Page 4 of 9
DISCHARGE MONITORING REPORT (DMR)
Facility Name: DOMINION ENERGY SOUTH CAROLINA INC/V C SUMMER Permit Number: SC0030856 v3.5 NUCLEAR STATION Permittee Name: DOMINION ENERGY SOUTH CAROLINA INC DMR Period: 3/1/2022 - 3/31/2022 QUANTITY OR LOADING QUALITY OR CONCENTRATION NO . FREQUENCY SAMPLE PARAMETER EX . OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS IPH (00400) SAMPLE 0 Monthly Grab Effluent Gross (1) ***** ***** 7.48 ***** 7 . 48 MEASUREMENT
- SU Lab ID: 20001 6.0 8.5 PERMIT ***** ***** ***** Grab Instantaneous Instantaneous Monthly REQUIREMENT Minimum Maximum Total Phosphor u s (as SAMPLE 0 Monthly 2.2 Grab P) (00665) MEASUREMENT ***** ***** ***** 2.2 Effluent Gross (1)
- mg/L PERMIT ***** ***** ***** REPORT REPORT Grab Lab ID: 23105 Monthly REQUIREMENT Monthly Average Daily Maximum Flow (50050) 0 Continuou Continue SAMPLE Effluent Gross (1) 0 . 0675249 0 . 1240239 ***** ***** ***** s us MEASUREMENT MGD *****
Lab ID: 20001 REPORT Continue PERMIT REPORT ***** ***** ***** Continuou Monthly us REQUIREMENT Daily Maximum s Average DMR Instructions :
DMR Comments: (none)
Limit Set: 0031 No Discharge :
QUANTITY OR LOADING QUALITY OR CONCENTRATION NO. FREQUENCY SAMPLE PARAMETER EX . OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS pH (00400) 0 Once per SAMPLE ***** SU Grab Effluent Gross (1) ***** ***** 6 . 96 ***** 7.86 Discharge MEASUREMENT I I I I I NAME/ TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law t hat thi s document and all attachments were TELEPHONE DATE prepared under my direction or supervision in accordance with a system designed to assure t hat qualified personnel properly gather and evaluate the information submitted. Based on my inquiry of the person or persons who manage the system, or those persons directly responsible for gathering the TYPED OR PRINTED information, the information submitted is, to the best of my knowledge and belief, true, accurate, and complete. I am aware that there are significa nt penalties for submitting false information, including the possibility of fine and SIGNATURE OF PRINCIPAL EXECUTIVE OFFICER OR AUTHORIZED AGENT AREA CODE I NUMBER YEAR MO DAY imprisonment for knowing violations.
Permit Number: SC0030856 v3.5 Generated: 4/28/2022 9 : 58 AM Page 5 of 9
DISCHARGE MONITORING REPORT (DMR)
Facility Name: DOMINION ENERGY SOUTH CAROLINA INC/V C SUMMER Permit Number: SC0030856 v3 . 5 NUCLEAR STATION Permittee Name: DOM I NION EN ERGY SOUTH CAROLI NA I NC DMR Period: 3/1/2022 - 3/3 1 /2022 QUANTITY OR LOADING QUALITY OR CONCENTRATION NO . FREQUENCY SAMPLE PARAMETER EX. OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS
- 6. 0 9.0 Lab ID : 20001 PERM I T ***** ***** ***** Gr ab Inst a ntaneous Instantaneou s Mont h ly REQU I REMEN T Minimum Maximum rrotal Su spended Solids 0 Tw i ce per SAMPLE Grab (00530) ***** ***** ***** 0 0 Discharge MEASUREMENT Effluent Gross (1)
- mg/L Lab ID : 20001 PERMIT ***** ***** ***** 30 100 Grab Monthly REQUIREMENT Month l y Average Daily Maximum Piland Grease (0055 6 ) 0 Twice pe r SAMPLE Grab Effluent Gross (1) ***** ***** ***** 0 0 Month MEASUREMENT
- mg/L Lab ID: 10120 PERMIT ***** ***** ***** 15 20 Grab Monthly REQU I REMEN T Monthly Average Daily Maximum Flow (50050) 0 Once per ESTIMATE SAMPLE Effluent Gross (1) 0 . 004200 0.004200 ***** ***** ***** Disch arge ES MEASUREMENT MGD *****
Lab ID: 2 0001 REPORT ESTIMATE PERMIT REPORT ***** ***** *****
Monthly Mo n thly ES REQUIREMENT Daily Maximum Average DMR Instructions:
DMR Comments : Total Suspended Solids Method SM2540D , PQL 1 . 0 mg/L , number of t imes result les s than PQL two.
Oil & Grease Method EPA 1664B , PQL 5 . 0 mg/L , number of times results below PQL = two.
Limit Set: 0051 No Discharge:
NAME/ TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law that th is document and all attachments were TELEPHONE DATE prepared under my direction or supervision in accordance with a syst em designed to assure that qualified personnel properly gather and evaluate t he information submitted . Based on my inquiry of the person or persons who manage the system, or those persons directly responsible for gathering the information, the information submitted is, to the best of my knowledge and belief, true, accurate, and complete. I am aware that there are sign ificant SIGNATURE OF PRINCIPAL EXECUTIVE AREA NUMBER YEAR MO DAY penalties fo r submitting false informati on, includ ing the possibility of fi ne and OFFICER OR AUTHORIZED AGENT CODE rTYPED OR PRINTED imprisonment for knowing violations.
Permit Number: SC0030856 v3 . 5 Genera t ed : 4/28/2022 9:58 AM Page 6 o f 9
DISCHARGE MONITORING REPORT (DMR)
Faci1ity Name: DOMINION ENERGY SOUTH CAROLINA INC/V C SUMMER Permit Number: SC0030856 v3.5 NUCLEAR STATION Permittee Name: DOMINION ENERGY SOUTH CAROLINA I NC DMR Period: 3/1/2022 - 3/31/2022 QUANTITY OR LOADING QUALITY OR CONCENTRATION NO. FREQUENCY SAMPLE PARAMETER EX. OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS BOD - 5 DAY (20 0 24 -Hr DEGREES C) (00310) SAMPLE Monthly Composit
- ***** ***** 2.6 2.6 Effluent Gross (1) MEASUREMENT e
- mg/L Lab ID: 40572 24 - Hr PERMIT ***** ***** ***** 30 45 Composit Monthly REQUIREMENT Monthly Average Daily Maximum e Total Suspended Solids 0 24 -Hr (00530) SAMPLE Monthly Composit
- ***** ***** 5. 1 5.1 Effluent Gross (1) MEASUREMENT e
- mg/L Lab ID: 40572 24-Hr PERMIT ***** ***** ***** 30 45 Composit Monthly REQUIREMENT Monthly Average Daily Maximum e Flow (50050) 0 INSTANTA Effluent Gross (1) SAMPLE Monthly NEOUS MEASUREMENT 0.005000 0 .005000 ***** ***** ***** IN Lab ID : 20001 MGD *****
INSTANTA REPORT PERMIT Monthly REPORT ***** ***** ***** Monthly NEOUS REQUIREMENT Daily Maximum IN Average E. COLI (MPN/l00ML) SAMPLE 0 Monthly Grab (51040) ***** ***** ***** <10 <10 MEASUREMENT Effluent Gross (1) #/l0OmL
- 1 26 PERMIT ***** ***** ***** 349 Grab Lab ID: 40572 30 Day Average Monthly REQUIREMENT Daily Maximum Geometric DMR Instructions:
DMR Comments: (none)
NAME/ TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law that this document and all attachments were TELEPHONE DATE prepared under my direction or supervision in accordance with a system designed to assure that qualified personnel properly gather and evaluate the information submitted. Based on my inquiry of the person or persons who manage the system, or those persons directly responsible for gathering the information, the information submitted is, to the best of my knowledge and belief, true, accurate, and complete. I am aware that there are significant islGNATURE OF PRINCIPAL EXECUTNE AREA NUMBER YEAR MO DAY penalties for submitting false information, includ ing the possibility of fi ne and OFFICER OR AUTHORIZED AGENT CODE
[TYPED OR PRINTED imprisonment for knowing violations.
Permit Number: SC0030856 v3 . 5 Generated : 4/28/2022 9 : 58 AM Page 7 of 9
DISCHARGE MONITORING REPORT (DMR)
Faci1ity Name : DOMINION ENERGY SOUTH CAROLINA INC/V C SUMMER Permit Number : SC0030856 v3 . 5 NUCLEAR STATION Permittee Name: DOMINION ENERGY SOUTH CAROLINA INC DMR Period: 3/1/2022 - 3/31/2022 Limit Set: 06Al No Discharge :
QUANTITY OR LOADING QUALITY OR CONCENTRATION NO. FREQUENCY SAMPLE PARAMETER EX . OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS
~otal Suspended Solids SAMPLE 0 Monthly Grab (00530) ***** ***** ***** 1. 2 1.2 MEASUREMENT
~ffluent Gross (1 ) mg/L PERMIT ***** ***** ***** 30 100 Grab Lab ID: 40572 Monthly REQUIREMENT Monthly Average Daily Maximum K)il and Grease (00556) SAMPLE 0 Monthly Grab Effluent Gross (1) ***** ***** ***** 0 0 MEASUREMENT
- mg/L Lab ID: 23105 PERMIT ***** ***** ***** 15 20 Grab Monthly REQUIREMENT Monthly Average Daily Maximum Flow (50050) 0 INSTANTA Effluent Gross (1) SAMPLE Monthly NEOUS 0 . 016500 0 . 016500 ***** ***** *****
MEASUREMENT IN Lab ID : 20001 MGD *****
INSTANTA REPORT PERMIT Mo nthl y REPORT ***** ***** ***** Monthly NEOUS REQU IREMENT Daily Maximum IN Avera ge DMR Instructions:
DMR Comments: Oil & Grease Method EPA 1664B , PQL 5 . 0 mg/1, number of times results below PQL one .
Limit Set: 0081 No Discharge: Y QUANTITY OR LOADING QUALITY OR CONCENTRATION NO. FREQUENCY SAMPLE PARAMETER EX. OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS Total Suspended Solids SAMPLE mg/L Monthly Grab (00530) MEASUREMENT I I I I I NAME/TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law t hat this document and all attachments were TELEPHONE DATE prepared under my direct ion or supervision in accordance with a system designed to assure that qualified personnel properly gather and evaluate the information submitted. Based on my inquiry of the person or persons who manage the system, or those persons directly responsible for gathering the information, the information submitted is, to the best of my knowledge and belief, true, accurate, and compl ete. I am aware that there are significant SIGNATURE OF PRINCIPAL EXECUTIVE AREA NUMBER YEAR MO DAY penalties for submitting false information, including the possibility of fi ne and OFFICER OR AUTHORIZED AGENT CODE TYPED OR PRINTED imprisonment for knowing violations.
Permit Number: SC0030856 v3 . 5 Generated: 4/28/2022 9:58 AM Page 8 of 9
DISCHARGE MONITORING REPORT (DMR)
Faci1ity Name : DOMINION ENERGY SOUTH CAROLINA INC/V C SUMMER Permit Number : SC0030856 v3.5 NUC LEAR STATION Permittee Name: DOMINION ENERGY SOUTH CAROLINA INC DMR Period : 3/1/2022 - 3/31/2022 QUANTITY OR LOADING QUALITY OR CONCENTRATION NO . FREQUENCY SAMPLE PARAMETER EX. OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS
!Effluent Gross (1)
PERMIT ***** ***** ***** 30 100 Grab Monthly Lab ID : REQUIREMENT Monthly Average Daily Maximum K)il and Grease (00556) SAMPLE Monthly Grab Effluent Gross (1) MEASUREMENT ***** ***** ***** ***** *****
- mg/L Lab ID:
PERMIT ***** ***** ***** 15 20 Grab Monthly REQUIREMENT Monthly Average Daily Maximum Total Copper (01042) SAMPLE Monthly Grab Effluent Gross (1) MEASUREMENT ***** ***** ***** ***** *****
- mg/L Lab ID:
PERMIT ***** ***** ***** 1. 0 1.0 Monthly Grab REQUIREMENT Monthly Average Daily Maximum rrotal Iron (01045) SAMPLE Monthly Grab Effluent Gross (1) MEASUREMENT ***** ***** ***** ***** *****
- mg/L Lab I D:
PERMIT ***** ***** ***** 1.0 1.0 Grab Monthly REQUIREMENT Monthly Average Dai l y Maximum Flow (50050) INS TANTA Effluent Gross (1) SAMPLE Monthly NEOUS MEASUREMENT ***** ***** ***** ***** *****
IN Lab ID: MGD *****
INS TANTA REPORT PERMI T Monthly REPORT ***** ***** ***** Monthly NEOUS REQUIREMENT Da il y Maximum IN Average DMR Instructions : COPPER & IRON - SAMPLING IS REQU I RED ONLY WHEN CHEMICAL ME TAL CLEAING WASTES ARE DISCHARGED . REPORT ' CONDITONAL ' ON THE DMR FORM WHEN CHEMICAL METAL CLEANING WASTES ARE NOT DISCHARGED DURING THE MONITORING PERIOD .
NAME/TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law that this document and all attachments w ere TELEPHONE DATE prepared under my direction or supervi sion in accordance with a syst em designed to assure t hat qua lified personn el properly gat her and evaluate th e information submitted. Based on my inquiry of th e person or persons who manage t he system, or t hose persons directly responsible for gatheri ng th e information, the information submitted is, t o the best of my knowledge and belief, tru e, accurat e, and complete. I am aware th at th ere are significant !SIGNATURE OF PRINCIPAL EXECUTIVE AREA NUMBER YEAR MO DAY penalt ies fo r submitting fa lse info rm ation, incl uding the possibility of fi ne and OFFICER OR AUTHORIZED AGENT CODE
!TYPED OR PRINTED imprisonment for knowing violations.
Permit Number: SC0030856 v3.5 Generated : 4/28/2022 9 : 58 AM Page 9 of 9
DISCHARGE MONITORING REPORT (DMR)
Faci1ity Name: DOMINION ENERGY SOUTH CAROLINA INC/V C SUMMER Permit Number : SC0030856 v3 . 5 NUCLEAR STATION Permittee Name : DOMINION ENERGY SOUTH CAROLINA INC DMR Period: 3/1/2022 - 3/31/2022 DMR Comments: (none)
NAME/TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law that this document and all attachments were TELEPHONE DATE prepared under my direction or su pervision In accordance with a system designed to assure that qualified personnel properly gather and evaluate the information submitted. Based on my inquiry of the person or persons who manage the system, or those persons directly respon sible for gathering the information, the information submitted is, to the best of my knowledge and belief, true, accurate, and complete. I am aware that t here are significant SIGNATURE OF PRINCIPAL EXECUTIVE AREA NUMBER YEAR MO DAY penalties for submitting false information, including the possibility of fine and OFFICER OR AUTHORIZED AGENT CODE rfYPED OR PRINTED imprisonment for knowing violations.
Permit Number: SC0030856 v3 . 5 Generated : 4/28/2022 9:58 AM Page 10 of 9
Digitally signed by:
nCORE test.wind Oat DISCHARGE MONITORING REPORT (DMR) Re Faci1ity Name: DOMINION ENERGY SC INC VC SUMMER NUCLEAR Permit Number : SCG646072 v2.1 Lo STATION OFF- SITE WATER SYSTEM Permittee Name: DOM I NION ENERGY SOUTH CAROLINA INC DMR Period: 1/1/2022 - 1/31/2022 Limit Set: OSAl No Discharge:
QUANTITY OR LOADING QUALITY OR CONCENTRATION NO. FREQUENCY SAMPLE PARAMETER EX. OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS ri'otal Manganese SAMPLE 0 Monthly Grab (0 1055 ) ***** ***** ***** 0 . 02 0 . 02 MEASUREMENT Effluent Gross (1) mg/L PERMIT ***** ***** ***** REPORT REPORT Grab Lab ID: 23105 Monthly REQUIREMENT Monthly Average Daily Maximum Flow (50050) 0 Once per INSTANTA Effluent Gross (1) SAMPLE Monthly NEOUS MEASUREMENT 0 . 648 0.648 ***** ***** ***** Discharge IN Lab ID: 20001 MGD *****
INSTANTA REPORT PERMIT REPORT ***** ***** ***** NEOUS Monthly Week ly REQUIREMENT Daily Maximum IN Average DMR Instructions: OUTFALL 05A 1 - REVERSE OSMOSIS DISCHARGING TO FRESHWATERS (FW); TREATED FILTER BACKWASH WATER , SEDIMENTATION WASH DOWN WATER AND DECANT WATER.
DMR Comments: (none)
Limit Set: 08Al No Discharge :
QUANTITY OR LOADING QUALITY OR CONCENTRATION NO . FREQUENCY SAMPLE PARAMETER EX . OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS Total Residual SAMPLE 2 Monthly Grab Chlorine (50060) ***** ***** ***** 0.05 0.05 MEASUREMENT Effluent Gross (1) mg/L PERMIT ***** ***** ***** 0 . 011 0 . 019 Grab Lab ID: 40572 Monthly REQUIREMENT Monthly Average Daily Maximum NAME/TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law that this document and all attachments were TELEPHONE DATE prepared under my direction or supervision in accordance with a system designed to assure that qualified personnel properly gather and evaluate the information submitted. Based on my inquiry of the person or persons who manage the system, or those persons directly responsible for gathering the information, the information submitted is, to the best of my knowledge and belief, true, accurate, and complete. I am aware that there are significant SIGNATURE OF PRINCIPAL EXECUTIVE AREA NUMBER YEAR MO DAY penalties for submitting false information, including the possibility of fi ne and OFFICER OR AUTHORIZED AGENT CODE TYPED OR PRINTED imprisonment for knowing violations.
Permit Number: SCG646072 v2 . 1 Generated : 2/28/2022 2 :1 7 PM Page 1 of 2
DISCHARGE MONITORING REPORT (DMR)
Facility Name: DOMINION ENERGY SC INC VC SUMMER NUCLEAR Permit Number: SCG646072 v2 . 1 STATION OFF- SITE WATER SYSTEM Permittee Name: DOMINION ENERGY SOUTH CAROLINA I NC DMR Period: 1/1/2022 - 1/31/2022 DMR Instructions : OUTFALL OBA 1-TOTAL RESIDUAL CHLORIINE (TRC) LIMITS FOR ALL WATER CLASSIFICATIONS (FW, FW sp, SA , SB , SA sp , SB sp ,
or SFH).
DMR Comments : DESC VCS is skeptical of the TRC 0 . 05 mg/L result for the following reasons :
Prior to the discharge sample , VCS personnel obtained multiple samples from both retention basins and obtained results that were less than 0.05 mg/L (nondetectable).
VCS's reverse osmosis system backwash process only contains raw water , which isn't treated with chlorine.
Throughout the Offsite Water System operating history, TRC has never been detected at the outfall.
There is no significant source of chlorine to the retention basins that could result in TRC level of 0 . 05 mg/L .
The occurrence of TRC res~lts above the permitted limit~ has been entered into the stati;n ' ~ correttive action ~rogram (CR1192303) and is under evaluation to determine the source and the validity of TRC 0.05 mg/L result.
- DMR Value Comments:
- Total Residual Chlorine, Effluent Gross (1), Limit: 0 . 011 Monthly Average , Reported Value: 0 . 05 , Comment : DESC is investigating the source of TRC. The results are suspect because TRC was never detected at the discharge previously . See General Report Comments for full details .
- Total Residual Chlorine , Effluent Gross (1), Limit: 0.019 Daily Maximum , Reported Value : 0.05 , Comment: DESC is investigating the source of TRC . The results are suspect because TRC was never detected at the discharge previously. See General Report Comments for ful l details.
Limit Set: 07A3 No Discharge:
QUANTITY OR LOADING QUALITY OR CONCENTRATION NO . FREQUENCY SAMPLE PARAMETER EX. OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS TEMPERATURE DIFFERENCE SAMPLE deg F 0 Monthly Grab
- ***** ***** ***** 58.0 58.0 (FAHRENHEIT) (00018) MEASUREMENT I I I I I NAME/TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law that this document and all attachments were TELEPHONE DATE prepared under my direction or supervision in accordance with a system designed to assure that qualified personnel properly gather and evaluate the information submitted. Based on my inquiry of the person or persons who manage the system, or those persons directly res ponsible for gathering the information, the information submitted is, to the best of my knowledge and belief, true, accurate, and complete. I am aware that there are significant SIGNATURE OF PRINCIPAL EXECUTIVE AREA NUMBER YEAR MO DAY penalties for submitting false information, including the possibility of fine and bFFICER OR AUTHORIZED AGENT CODE il"YPED OR PRINTED imprisonment for knowing viol ations.
Permit Number : SCG646072 v2 . 1 Generated: 2/28/2022 2:17 PM Page 2 of 2
DISCHARGE MONITORING REPORT (DMR)
Faci1ity Name: DOMINION ENERGY SC INC VC SUMMER NUCLEAR Permit Number: SCG646072 v2.l STATION OFF- SITE WAT ER SYSTEM Permittee Name: DOMINION ENERGY SOUTH CAROLINA INC DMR Period: 1/1/2022 - 1/31/2022 QUANTITY OR LOADING QUALITY OR CONCENTRATION NO . FREQUENCY SAMPLE PARAMETER EX . OF TYPE AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS ANALYSIS Effluent Gross (1)
PERMIT ***** ***** ***** REPORT REPORT Grab Monthly Lab ID: 20001 REQUIREMENT Monthly Average Daily Maximum DMR Instructions: OUTFALL 07A 3-ION EXCHANGE AND REVERSE OSMOSIS DISCHARGING TO CLASS FW, FW sp WITH SITE- SPECIFIC STANDARDS , SA , SA sp , SB , SB sp , or SFH WATERS.
DMR Comments: (none)
NAME/TITLE PRINCIPAL EXECUTIVE OFFICER I Certify under penalty of law th at this document and all attachments were TELEPHONE DATE prepared under my direction or supervision in accordance with a system designed to assure that qualified personnel properly gather and eva luate t he information submitted . Based on my inquiry of the person or persons who manage the system, or those persons directly responsible for gathering the information, the information submitted is, to the best of my knowledge and belief, tru e, accurate, and compl ete. I am aware that there are significant SIGNATURE OF PRINCIPAL EXECUTIVE AREA NUMBER YEAR MO DAY penalties for submitting false information, including th e possibility of fine and bFFICER OR AUTHORIZED AGENT CODE TYPED OR PRINTED imprisonment for knowing violation s.
Permit Number : SCG646072 v2 . l Generated : 2/28/2022 2 : 17 PM Page 3 of 2
Healthy People. Healthy Communities CERTIFIED MAIL- 9214 8969 0099 9790 1421 3706 01 April 6, 2022 DOMINION ENERGY SOUTH CAROLINA INC Attn : GEORGE A LIPPARD PO BOX 88 JENKINSVILLE, SC 29065 Re: Notice of Violation AI-0005261 Pennit # SCG646072 v2. l DOMINION ENERGY SC INC VC SUMMER NUCLEAR STATION OFF-SITE WATER SYSTEM Fairfield County
Dear GEORGE A LIPPARD:
A review of the discharge monitoring reports (DMRs) submitted to the Department for the January 2022 monitoring period has revealed the following violations:
PIPE# PARAMETER DATE LIMIT DMR AVG/MAX 08A 50060-Total Residual January 3 l , 0.019 0.05 Daily Maximum Chlorine 2022 08A 50060-Total Residual January 31, 0.01 I 0.05 Monthly Average Chlorine 2022 You are hereby notified that failure to comply with the effluent limits of the NPDES Permit is a violation of the Pollution Control Act, S.C. Code Ann. 48-1-11 0(d) and Water Pollution Control Permits, 3 S.C.
Code Ann. Regs. 61-9.122.4l(a). The violations make DOMINION ENERGY SC INC VC SUMMER NUCLEAR STATION OFF-SITE WATER SYSTEM subject to further enforcement action, which may include assessment of civil penalties as set forth in the Pollution Control Act, S.C. Code Ann. 48-1-330.
You are requested to submit a written response within ten (10) days ofreceipt of this notice. Your response should include an explanation for the violations cited above and measures that have been or will be taken to ensure compliance with permit conditions. This response will not relieve DOMINION ENERGY SC INC VC SUMMER NUCLEAR STATION OFF-SITE WATER SYSTEM ofresponsibility for the violations cited.
If you have any questions concerning this notice, you may contact me at 803-896-2333 or oblandjl@dhec.sc.gov. I will be glad to assist you.
Jacob Oblander Environmental Quality Manager Bureau of Water cc: Midlands EA Columbia