ML20138N206

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Insp Repts 50-327/85-35 & 50-328/85-35 on 851006-1105. Violation Noted:Failure to Implement Procedures Re Reactor Trip Response Time Testing,Installation of Containment Penetration & Radiation Monitoring Testing
ML20138N206
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 12/06/1985
From: Jenison K, Linda Watson, Weise S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20138N155 List:
References
50-327-85-35, 50-328-85-35, NUDOCS 8512230406
Download: ML20138N206 (15)


See also: IR 05000327/1985035

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                                                                        UNITgD STATES '
                 g               .o                     NUCLEAR REGU'.ATORY COMMISSION
                [[ -                 ,                                    REGION 11.
             . g --                -j                        101 MARIETTA STREET,N.W.
             ~*-                     2                         ATLANTA, GEORGIA 30323

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              ' Report Nos~.: 50.-327/85-35, 50-328/85-35
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                Licensee: Tennessee Valley Authority
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                                     6N11 B Vissionary Ridge Place-
 "-                                 --1101.Ma'rket Street
                                  , Chattanooga, TN 37402-2801
               - Doc ket < No s'. : 50-327'and 50-328                          ' License Nos.: DPR-77 and DPR-79
              ' Facility Name:                Sequoyah Units 1 and 2
              . Inspection Conductea:               Octeer 6 through November 5, 1985
                Inspectors:               6Qd           <W
                                     K. M. Wnisof, Senior Resident Inspector
                                                                                                                   /A/05/B5
                                                                                                               Dat'e Si'gned
                                  .       G 0. nd         .Ww                                                      /G-loS/A5
                                     L. J. W4tson,gResident Irspector                                          Dat'e Signed
                Accompanying. Personnel:             G.   . Pi
                Approved by:                          7/                                                         ~
                                                                                                                           II
                                       S. P. Weise,~ Section Chief
                                            .
                                                                                                               DatE Signed
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                                       Division of Reactor Projects
                                                                        Summary
                Scope: .This routine, announced inspection involv'ed-349 resident inspector-hours
     ,          onsite in the areas of operational . safety verification including operations
              -performance, . system lineups, radiation protection, . security . and housekeeping
               ' inspections; ' surveillance and maintenance observations; review of previous
                inspection findings; followup of events; review of licensee identified items;
                walkdown-of Engineered Safety Features;; and review of inspector followup items.
              :Results: One violation was identified - Failure to implement procedures'in the
                areas of reactor trip response time testing (paragraph 7), installation, of, a
                containment penetration'(paragraph 8), radiation monitor testing (paragraph'10);                                ;
                and, configuration control of a radiation monitor power source (paragraph 10).                                ,
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                B512230406 851210
                PDR- ADOCK 05000327
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                                                REPORT DETAILS
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          - 1.   Licensee Employees
                 Persons Contacted
                 H. L. A'oercrombie, Site _ Director
               *P. R. Wallace, Plant Manager
               *L. M. Nobles, Operations and Engineering Superintendent
               *B. M. Patterson, Maintenance Superintendent
                J._M.- Anthony, Operations Group Supervisor
                 R. W. Olson, Modifications Branch Manager
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                 M. R. Sedlacik, Electrical Section Manager, Modifications Branch
               *H._D. Elkins, Instrument Maintenance Group Manager
                 G. B. Tiner,. Instrument Maintenance Engineer
               *M.   R. Harding, Engineering Group Manager
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               *D. C. Craven, Quality Assurance Supervisor
               *G. B. Kirk, Compliance Supervisor
               , M. L. - Frye, Compliance Engineer
                 D. H.:Tullis, Mechanical-Maintenance Group Supervisor
                J. H. -Sullivan, Regulatory Engineering Supervisor
               *C, E. Bosley, Quality Assurance. Auditor
               -Other licensee employees contacted included technicians, operators, shift
                 engineers, security force members, engineers and maintenance personnel.
               * Attended exit interview
           2.    Exit Interview
                 The inspection scope and findings were summarized with the Plant Manager and
                 members of his staff on November 6, 1985.       A violation with examples
                 described in paragraphs 7, 8 and 10 was discussed.           The licensee
                 acknowledged the inspection findings and identified as proprietary a portion
                 of- the material reviewed by the inspectors- in regard to the negative rate
                 trip application as discussed in paragraph 10. The information in this
                 report 'does not include that proprietary information. During the reporting
               -period, frequent discussions were held with the Site Director, Plant Manager
                 and his assistants concerning inspection findings. At no time during the
                 inspection was written material provided to the licensee by the inspector.
           3.    Licensee A>: tion on Previous Inspection Findings (92702)
                .This subject was not addressed in this inspection.
           4.    Unresolved Items
                 No unresolved-items were' identified during this inspection.
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 '5. ' Operational Safety Verification (71707)
     .a.     Plant Tours
           : The inspectors observed control room operations, reviewed applicable
             logs, conducted discussions with control room operators, observed shift
            . turnovers, and confirmed operability of instrumentation.          The
             inspectors verified the . operability of selected emergency systems.
           -reviewed tagout records, verified compliance- with Technical
           -Specification (TS) Limiting Conditions for Operation (LCO) and verified.
             return to service of affected components. The inspectors verified that
             maintenance.. work orders had been submitted as required and that
             followup activities and prioritization of work was accomplished by the
             licensee.
             Tours of the diesel generator, auxiliary, control, and turbine
             buildings and containment were conducted to observe plant . equipment
             conditions,    including potential fire hazards, fluid leaks, and
             excessive vibrations and plant housekeeping / cleanliness conditions.
             The inspectors walked down accessible portions of the following
             safety-related systems on Unit I and Unit 2 to verify operability and
             proper valve alignment:
                   Residual Heat Removal System (Units 1 and 2)
                   Charging Pump Flowpath (Units 1_ and 2)
                   Control Room Ventilation Chlorine Detection System (Common)
                   Spent Fuel Pool Cooling System (Common)

. b. Security

             During the course of the inspection, observations relative to protected
             and vital area security were made, including access controls, boundary
             integrity, search, escort, and badging.
                    '
             On November 1, 1985, the licensee declared a moderate security
            . degradation as a result of the actions of a security officer posted at
           -the entrance of -the Unit 2 containment hatch on the 690 level.
             Appropriate ' compensatory actions were taken and the licensee's
             personnel administrative process was implemented. The inspector
             reviewed the above incident and had no further questions. .This item
             will be reviewed by NRC specialist inspectors at a later date. No
             violations or deviations were identified,
        c.   Radiation Protection
             The inspectors observed Health Physics (HP) practices and verified
             implementation of radiation protection control. On a regular basia,
             radiation work permits (RWPs) were reviewed and specific work
             activities were monitored to assure the activities were being conducted
             in accordance with applicable RWPs.       Selected radiation protection

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                          : instruments were verified operable and calibration frequencies were
                          . reviewed.
               6.   Engineered Safety Features Walkdown (71710)
                  EThe , inspector verified. operability of the Component Cooling Water system
                    (CCS) on' Units 1'and 2: by continuing a walkdown of the accessible portions
                    of a the systems.~ -Inspection Report 327,328/85-32 documents the previous
                    inspection.of this.' system. The following specifics were : reviewed and/or .
                  ' observed'as_ appropriate:
                   a.    _that the licensee's system lineup procedures. matched plant drawings and
                           the as-built configuration;
 p                 b.     :that equipment _ conditions were sati sfactory and items that might

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                         ' degrade ' performance were identified and evaluated (e.g. hangers and
                           supports were operable, housekeeping etc, was adequate);
                   c.     ~with assistance 'from licensee personnel, the interior of-the breakers
                           and electrical or instrumentation cabinets were inspected for debris,
                           loose material, jumpers, evidence of rodents, etc;
                  ;d.     .that instrumentation was properly valved in and functioning and

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                           calibration ~date's were appropriate;
                   e.      that -valves were in proper position, breaker alignment was correct,
                           power was available, and valves were locked as required; and
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                    f.     local and remote instrumentation was compared, and remote instru-

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                           mentation was functional.
No violations or deviations were identified.
           ' 7' . -Monthly Surveillance Observations (61726)
                   The inspectors observed Technical Specification (TS) required surveillance
                   testing and verified that testing'was performed in accordance with adequate
                   procedures, that test instrumentation was calibrated, that Limiting
                   Conditions for Operation.were met, that test results met acceptance criteria
                   requirements -and were reviewed by personnel other that the individual
                   directing the test, that deficiencies were identified, as appropriate, and
                   that any deficiencies identified during the testing were properly reviewed
                   and resolved by management personnel, and that system restoration was
                   adequate.- For complete tests, the inspector verified that testing                                                          '
                   frequencies were met and tests were performed by qualified individuals.
                   The inspectors witnessed / reviewed portions of the following surveillance
                   test activities:

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                           SI-82.2 Functional Tests for the Radiation Monitoring System
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       .SI-67    . Periodic Calibration of the RPI System
 .The inspectors reviewed the results of reactor trip response time testing.
  The following procedures were reviewed:
       :IMI-99 ' Reactor . Protection System RT 11.6, Response Time Test of
        dT/Tavg Channel II, Rack 6
        IMI-99 Reactor ' Protection System RT 11.8, Response Time Test of
        dT/Tavg Channel 4, Rack 13
        IMI-99 Reactor Protection System RT 7.14 Response Time Test of Loop
        1 Steam Generator Level Channel III (L-518) (L-3-39)
        IMI-99 Reactor Protection System RT 7.17 Response Time Test of Loop
        2 Steam Generator Level Channel III (L-528)
        IMI-99 Reactor Protection System RT 7.20 Response Time Test of Loop

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        3 Steam Generator Level Channel III (L-538)
        IMI-99 Reactor Protection System RT 7.23, Response Time Test of Loop
        4 Steam Generator Level Channel III (L-548)
        IMI-99 Reactor Protection System RT 611A, Response Time Testing
        Engineered Safety Feature Actuation Slave Relay K611
  The inspector observed a. portion of the performance of the response time
  testing for loop 1 steam generator level Channel III under procedure RT
  7.14,    The technician stopped the test when he could not complete step 4.4
  which required that he insure that a test indicator light on the train he
  was testing was -lit. The test indicator light was not lit. The technician
  took the procedure-to his foreman for guidance. The foreman discussed the
  step with an instrument maintenance engineer and determined that the light
  would not illuminate because the reactor trip breakers were not closed. A
  nonintent change was requested to revise the procedure.
  During these discussions, the inspector observed that a piece of scratch
  paper with a note written on it had been inserted into RT 7.14 indicating
  that Step 55, which had not been performed at that point, could not be
 . performed because of plant conditions.      Step 55 requires verification of
  certain block switches by confirmation that the block switch lights were
 -lit.   The technician stated that he had been instructed to place the remark
  N/A (not applicable) adjacent to this step, and to continue with the test;
  however, the technician stopped the procedure performance prior to reaching
  this step.
  The inspector reviewed additional procedures and determined that certain
  steps had been marked N/A. In RT 611A, Step 5.5.6 requires that certain
  equipment be returned to normal position.        This is an independent verifi-
 . cation signoff. Twenty-six of these steps were marked N/A with a note that
  the components were tagged under various hold orders not specified in. the

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        data-sheets. It should be noted that hold orders require independent veri-
        fication of return to service. One additional non-safety-related component
        was marked N/A with no reference to a hold order or other explanation. The
        procedure requires that - if a device cannot be returned to normal, the
        information should be entered as discrepancies on the data cover sheet.
        This_information had not been entered in the data sheet as a discrepancy.
        Additional . steps in procedures RT 7.17 and 7.23 require verification that
        the status and alarm lights are not lit except as allowed by Step 2 of the
        procedure which states that lights marked by an asterisk may be normally lit
        if the unit is offline.      Lights had been verified to be in a status not
        allowed by the procedure and signed off as acceptable due to plant
        conditions.      The licensee stated that the status and alarm light
        verification did not affect test performance in Modes 5 and 6 but was to
        assure that if the test were performed in modes 1 through 4, the reactor
        would not be tripped.
        The failure to follow procedures RT 611A, RT 7.17, and RT 7.23 constitute a
        violation 327,328/85-35-01.
        In addition, the inspector noted that the following steps in procedure
        RT 611A had been marked N/A in the data sheet when it appears that they
       .should have not been marked that way.
              Step 4.1.10 requires that an annunciator window for the low pressure
              indication from the Condensate Storage Tank to the Auxiliary Feedwater
              Pump (AFWP) be cleared.      The pressure switch would automatically
              initiate Essential Raw Cooling Water (ERCW) flow to the AFWP if the
              pressure reached the low setpoint. The step was marked N/A with a note
              that H0 1073 had power off of all ERCW valves. In this case, the reason
              for the annuniciator window indication was clearly indicated in the
              data sheet.
              Step 5.2.1 was marked N/A. This step had a double entry for signing
              off one handswitch position in the data sheet. This entry was clearly
              a typographical error and should be corrected.
    8.  Monthly Maintenance Observations (62703)
        a.    Station maintenance activities of safety-related systems and components
              were observed / reviewed to ascertain that they were conducted in
              accordance with approved procedures, regulatory guides, industry codes
              and standards, and in conformance with TS.
              The following items were considered during this review: LCOs were met
              while components or systems were removed from service; redundant
              components were operable; approvals were obtained prior to initiating
              the work; activities were accomplished using approved procedures and
              were inspected as applicable; procedures used were adequate to control
              the activity; troubleshooting activities were controlled and the repair
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     record accurately reflected what actually took place; functional
     testing and/or calibrations were performed prior to returning
     components ~ or systems to service; quality control records were
     maintained; activities were accomplished by qualified personnel; parts
     and materials used were properly certified; radiological controls were
     implemented; QC hold points were established .where required and were
     observed;-fire prevention controls were implemented; outside contractor
    ' force activities were controlled ir accordance with the approved
     Quality Assurance (QA) program; and housekeeping was actively pursued.
 b.  The inspectors reviewed the modification of feedring J-tubes in the
     four steam generators. The licensee had planned a modification
     involving replacement of the carbon steel J-tubes with Inconel J-tubes
     due to wall thinning in the J-tubes. Upon examination of the tubes and
     feedring after removal of the J-tubes, the licensee determined that the
     carbon steel feedring had been eroded by high velocity flow at the base
     of the J-tube.
     The modification was revised to include oversized boring of the holes
     in the feedring to eliminate the eroded areas and buildup of the J-tube
     wall with Inconel in this area to fit the larger hole.      The inside
     diameter of the J-tube remained the same except that the entrance to
     the tube from the feedring was machined to a smooth rounded edge to
     prevent turbulance. The J-tube was welded to the feedring with Inconel
     weld filler metal.
     The inspector examined J-tubes removed from the steam generators and
     examined a portion of one feedring upon removal of the J-tubes. The
     inspector also observed an inspection of J-tube welds by the vendor's
     QA representative. The inspector reviewed WP 11829 which covered all
     the J-tube replacements in the four Unit 1 steam generators and
     drawings D-246-941-1 and -2.      The licensee will be presenting the
     findings on- the feedring degradation to the Westinghouse Steam
     Generator Owners Group during November,1985.
     No violation or deviations were identified.
 c.  The inspector observed preparation for a leak test of a containment
     penetration which had been replaced to meet environmental qualificaton
     requirements.    The   inspector   reviewed Work Plan 11802, dated
     October 28, 1985, which required that the penetration be assembled and
     tested in accordance with a validated vendor manual. The inspector
     determined that the licensee had not received the updated vendor manual
     describing the assembly of the feed thru tubes for the penetration. The
     vendor manual at the work site did not describe the assembly of the
     feedthru tubes, but did describe the leak test requirements. The
     inspectors determined that the manual used had not been reviewed and
     validated by PORC.    The penetration was installed and assembled based
     on verbal instructions received from the vendor at an earlier date.
     The vendor, subsequent to this inspection providea written instructions
     to the licensee which included requirements for QC hold points not

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                 performed during -installation. Based on ' this new information, the    '
                 licensee reworked the penetration in. accordance with the vendor's
                 instructions and a validated vendor manual. Failure to' implement the
                 work 1 plan for. assembly of containment electrical penetrations is a
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                 further example of violation 327, 328/85-35-01.
           d.    The replacement of electrical relays in.the 6.9KV shutdown boards was
                 observed. The following documents were reviewed:
                        Special Maintenance Instruction SMI-0-202-1
                        Maintenance Instruction'6.20
                      - Maintenance Request A284454
                        Procurement Documents (575) 5886000390, 5886000771
                 The maintenance appeared to be adequate and no violations or deviations
                 were identified.
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     ;9.   Licensee Event Report (LER) Followup (92700)
         'The following LER's were reviewed and closed. The inspector verified that:
           reporting requirements had been met, causes had been identified, corrective
           actions appeared appropriate, generic applicability had been considered, the
           LER forms were complete, the licensee had reviewed the event, no unreviewed
            safety questions were involved, and violations of regulations or Technical
          ' Specification conditions had been identified,
           a.    LER Unit 1
                 327/85021     Control Room Ventilation Isolation
                 327/85023     Auxiliary Building Isolation
                 327/85026     Failure to Obtain a. Noble Gas Sample
                 327/85027     Main Steam Line I:olation
                 327/85029     Reactor Trip on Loss of Power to Main Feedwater Pump
                 327/85030     Auxiliary Feedwater Initiation
                 327/85033     Main Control Room Isolation Due to Failure to Follow
                               Procedure
                 327/85034     Diesel Generator Operability
                 327/85035     Emergency Diesel Generator Start While Trouble Shooting
                               Control Power
                 327/85037     Main Control Room Isolation Due to Spike on Radiation
                               Monitor
                 327/85038     Auxiliary Building Isolation From SFP Rad Monitor During
                               Filter Changeout
           b.    LER Unit 2
                 328/85007     Inadvertent trip 2A-A Shutdown Board Feeder Breaker
                 328/85008     Failuresto Complete Hourly Fire Watch
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         '10. Event Followup-(93702, 62703, 61726)
              a.   On October 1,1985,- the inspectors received a copy of a Westinghouse
                   Technical . Bulletin which dealt with- negative and positive flux rate
                   reactor trip setpoint calibration methodology. Discussions were held
                   with'several levels of plant management including cognizant engineers
                   and technicians. As a result of this process the following documents
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                  .were reviewed:
                   Westinghouse Technical Bulletin NSID-TB-85-13
                   Westinghouse Technical Manual N2M-2-1-X, Nuclear Instrument-System
                   Surveillance Instruction (SI) E0, Power Range Nuclear Flux Channel
                         Calibration and Functional Test
                   Standard Practice SQA26 Attachment 4, Operating Experience Review
                         Recommended Action Sheet
                   Instrument Maintenance Instruction (IMI) 92-PRM-CAL, NIS Power Range
                   Standard Practice SQA26 Attachment 3, Experience Review Evaluation
                         Form
                   Standard Practice SQA26 Attachment 2, from Supervisor, Regulatory
                         Engineering to Supervisor, Instrument Maintenance and Lead
                         Instrument Engineer (D. Elkins, R. Gladney)
                   Standard Practice SQA26 Attachment 1, Operating Experience Review
                         Screening Sheet
                   TVA memo McGriff to Brimer, Sullivan of September 3,1985
                   TVA memo Gibbs to Wilson copy to Sauer of July 17, 1985 (Note: This
                         is a Watts Bar site memo)
                   Technical Specification Change Request 85-122
                   Management A: tion Tracking System (MATS) Assignment Sheet dated June
                         26, 1985
                   TVA memo McCloud to McGriff dated June-25, 1985
                   Precautions, Limitations and Setpoints for Sequoyah Nuclear Plant
                   NRR memo, T. Dunning to Dunenfeld, Westinghouse Neutron Flux Rate
                         Setpoints
                   Sequoyah Nuclear Plant Startup Test 9.5 Evaluation Report
                   WCAP-10297-P-A Westinghouse Dropped Rod Methodology for Negative
                         Flux Rate Trip Plants
                   Technical Specification Table 2.2-1
                   The SNP management and staff were knowledgable of the WTB about the
                   second week in July. The WTB discussed the alignment procedure for the
                   Nuclear Instrumentation system power range positive and negative rate
                   trip bistables and explained that some plants had misinterpretated the
                   procedure as outlined in the Westinghouse Nuclear Instrumentation
                   System Technical manual. The electrical circuit addressed by both the
                   Nuclear Instrumentation Technical manual and the WTB consists of an
                   upper and lower detector whose signals are indicated on nuclear
                   instrument (NI) meters 301 and 302. The signals are added together
                   and averaged through a level and averaging circuit.       A resulting
                   adjusted signal is then read on full percent power meter 303.
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    The adjusted electrical signal passes through two subsections of the
    power range rate and delay circuit (NM311), resulting in a potential
    difference on a downstream operational amplifier. The output of the
   : operational amplifier is fed to the input of a bistable which will trip
    when a given input value-is reached, resulting in a reactor trip.
    The- Westinghouse Nuclear Instrumentation (WNI) Technical Manual
    described the process used to calibrate this power range rate and delay
   ' circuit to ensure that bistable NC301 has the proper TS reactor trip
     setpoint. Surveillance Instruction SI 80 was reviewed and appeared to
    conform with what was indicated in the WNI Technical Manual.
    Performance of the steps described in the WNI Technical Manual and SI
    80 resulted in a stepped potential difference of 3% (negative rate
    trip) and 5*4 (positive rate trip) being applied to the operational
    amplifier in the rate and delay circuit.
    The Westinghouse Technical Bulletin stated that the power range
    detector A test signal is used to create a step signal which is the
     input to the power range rate and delay circuit (NM311) and that the
    detector A test signal should be set numerically equivalent to the
    value of percent full power change given~ in the plant Precautions,
    Limitations and Setpoints(PLS) document. For Sequoyah, the PLS
    document disagrees with the Technical Specifications, and the licensee
    used the Technical Specification values. The WTB also stated that due
    to possible misinterpretation of the Nuclear Instrumentation System
    manual, plants may have doubled the Detector A test signal in order to
    compensate for the summing the level amplifier.
    Additionally, the WTB ~ requires maintenance personnel to set the
    detector A test signal in power units or percent of full power detector
    current, to the value given in the PLS document for tne percent full
    power change for the rate trip. For example, if the PLS document
    requires a rate trip on a 5% change of full power, then the detector A
    test signal should be set to 5 power units or 5% of detector A full
    power current.
    The difference between the Westinghouse Technical Bulletin (WTB) and
    the Westinghouse Nuclear Instrument Technical Manual is in the
    amplitude of the potential applied.       The WTB requires that the
    amplitude be read on the meter after the leveling circuit.
    The initial TVA management review determined that the bulletin could
    not be complied with because the operational amplifier input would have
    to be set to 1.5*. and that this value would not allow sufficient margin
    from' normally present nuclear flux circuit noise (approximately l*s).
    The licensee interpreted that the trip value of the TS should be equal
    to the magnitude of the detector input since this is consistent with
    standard TS trip setpoint methodology.
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         A TS change request was processed through the Plant Operations Review
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         Committee (PORC) on. September 11, 1985 to implement the standard TS
         trip setpoint valves.     It stated that implementing the calibration
         method stated in the WTB would significantly increase the chances of
         inadvertant trip actuations caused by nuclear noise using the current
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         TS valves.
        -The licensee requested Westinghouse to perform a study and determine
         whether the WTB applied to Sequoyah. The TS change request was-
         submitted to the NRC by letter dated October 22, 1985. Westinghouse's
         response addressed the conservatism of the current Sequoyah TS compared
         to the PLS values and performed some calculations on the power range
         rate and- delay circuit.      Although Westinghouse calculations were
         provided for several cases, the results appeared to be only
         conditionally acceptable. Conversations were held between NRC Region
         II and the licensee and NRR personnel. The licensee's interpretation
         on setpoint methodology for testing was consistent with TS intent. In
         light of the WTB, the NRC determined that the TS were in error and that
         this issue appeared to be generic. Resolution of this TS issue prior
         to the startup is an Inspector Followup Item 327, 328/85-35-02.
         On October 30, 1985, The inspector witnessed a surveillance test which
         verified the Digital Rate Circuit time constant on Power Range Monitor
         channels N-41 and N-43.    The work was requested under MR A-539515 and
         A-539516 for channels N-41 and N-43, respectively. The technicians
         utilized Instrument Maintenance Instruction, IMI-92-PRM-CAL steps
         5.2.9.12 through 5.2.9.14 to perform the test and IMI-134 to record the
         data. The test was conducted by inputing a negative three percent
         change in power level and upon reaching the desired level determining
         the decay time to reach 37% of the initial value,       f.e., one time
         constant. The test determined that the time constant for N-41 was 1.31
         seconds for for N-43 was 1.30 seconds. The time constant is required
         per TS table 2.2-1 to be greater than 1 second.
         No violations or deviations were identified.
     b.  On October 26, 1985, the licensee discovered a leak in the reactor
         cavity liner. The cavity was drained and a nozzle cover was repaired
         and reseated and the cavity was refilled. On October 28, 1985, the
         licensee discovered that the cavity liner was again leaking. The
         leakage was going to the keyway sump-under the vessel and through the
         number 2 cold leg penetration to the containment sump. The licensee
         evaluated the leakage, which remained steady at approximately I gpm
         through the end of the report period, and determined that the liner
         itself was probably the source of the leakage. The inspector reviewed
         the procedure for failure of the reactor cavity seal, Abnormal
        Operating Instruction, A0I-290 and discussed the leak rate with the
         cognizant engineer.     The licensee stated that based on the present
         indications that refueling operations would proceed with close
        monitoring of the leakage. At the end of refueling the licensee will
        drain the reactor cavity and repair the leak.
                                                                                  _ _ _ _ - - _ _ -
          F
    .
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        No violations or deviations were identified.
   c.   On October 10, 1985, the licensee conducted Surveillance Instruction,
        SI-82.2 as part of a post modification test to restore radiation
        monitors 2-RM-90-106B and -112B to service. Work plan 11793 had been
        written to incorperate changes descriosd in the Engineering Change
        Notice 5198 and Field Change Request 3785.      The maintenance consisted
        of a modification to an electrical ground point.         The Instrument
        Technician placed switch HS-90-136A in the block position on Unit 2 and
         then inserted a test signal into the Unit I circuit in error.      This
        action resulted in a containment ventilation isolation. Failure to
        adequately implement SI-82.2 is a further example of violation
        327,328/85-35-01,
   d.   On October 31, 1985, while transferring start bus.1B from normal to
        alternate supply, the alternate breaker faiied to latch. This resulted
         in a loss of power to the 1A Shutdown Board and a start signal to the
        diesel generators. Two of the diesel generators started; the other two
        diesel generators were out of service for maintenance. The licensee
        attributed the failure of the alternate breaker to mechanical binding
        at the end of travel resulting in the failure to latch. The breaker
        was subsequently relatched; however, the licensee stated that main-
        tenance would be performed on the breaker to investigate the problem.
         In conjunction with this failure, a "B" Train Auxiliary Building
         Isolation occurred due to loss of power to spent fuel pool monitor
        0-RM-90-103.    This monitor is required to operate to prevent a release
        of radioactive material from the Auxiliary Building in the event of a
         fuel handling accident in the spent fuel pool.       As identified on
        drawing PL J281-53 the monitor should have been powered from a Train B
        power source inside the radiation monitor cabinet. The licensee
        determined that the monitor was plugged into a nonessential power
        source.
        The inspector reviewed MR A-530620, which the licensee identified as
        the latest maintenance involving unplugging of the power source. The
        MR required maintenance to be done in accordance with Instrument
        Maintenance Instruction IMI-134, Configuration Centrol of Instrument
        Maintenance Activities. This procedure required the use of a
        configuration control sheet to assure that equipment was returned to
        its proper orientation. The requirements for use of the configuration
        control sheet were not properly followed in that the sheet did not
         identify the specific plug mold from which the monitor was unplugged
        and returned. Failure to implement configuration control procedures is
        a.further example of violation 327, 328/85-35-01,

11. Inspector Followup Items (92701)

   Based on inspection activities in the affected functional areas the
   following items were determined to require no additional specific followup

,-

              .
        ..
                                             12
        and are closed. Discussions were held with the licensee with regard to the
        tinieliness of corrective actions.
              83-23-04 (units 1 and 2)
              84-11-03 (unit 1)
    12. Review of Part 21 Reports (36100)
        a.    The inspector reviewed a 10 CFR Part 21 report, provided to the NRC in
              a letter dated March 13, 1984, on Brown Bovari Corporation Type ITE-27N
              undervoltage sensing relays. Correction . of the design deficiency
              required replacement of a 100 kilchm resistor with a 200 kilohm
              resister on fourteen relays provided to Sequoyah.        The inspector
              reviewed MRs A-082428, A-082427, A-082426 and A-082424 which replaced
              12 of the resistors on the subject relays which are utilized for
              undervoltage protection on the 6.9 KV shutdown boards. The inspector
              randomly selected six of the relays and verified replacement of the
              resistors. Two additional relays maintained at replacement parts were
              also verified to be modified.       This item, identified as 327,
              328/P21-85-03 is closed.
        b.    The inspector reviewed a 10 CFR Part 21 report, provided to the NRC on
              June 15, 1984, on the use of Crawford Fitting Company Swagelock
              fittings. Crawford Fitting Company determined that this issue was not
              of safety concern as documented in their November 16, 1984 letter to
              the NRC. This item, identified as 327,328/P21-85-02, is closed. Note
              that vendor recommendations on the use of Swagelock fittings was
              reviewed in Inspection Report 327/85-27, 328/85-28 and an Inspector
              Followup Item was left open regarding the licensee's evaluation of high
              pressure seal fitting adequacy.
    13. Refueling Activities (60710)
        Unit 1 began removing fuel from the reactor for the Cycle 4 fuel load on
        October 23, 1985.     Reload of the core was in progress at the end of this
        inspection report period.       The   inspector observed preparations for
        refueling, fuel handling operations in containment and in the spent fuel
        pool, movement of thimble plugs and rod cluster control assemblies in the
        spent fuel pit, and other ongoing activities associated with the rifueling.
        The inspector verified that_ selected Technical Specification requirements
        were met, that appropriate procedures were being utilized, that containment
        integrity was being maintained, that housekeeping and control of materials
        entering containment was adequate and that staffing was in accordance with
        the Technical Specification requirements. The following documer,:s were
        reviewed:
        Fuel Handling Instruction FHI-5, RCC Change Fixture
        Fuel Handling Instruction FH'.-6, Preparation for Refueling
        Fuel Handling Instruction FHI-7, Refueling Operation
  -
                                                                            - .__ __                           _ _ _ _ _ - _ _
    .
 .               .
          ..
  A
                                               13
          Fuel Handling Instruction FHI-13, Burnable Poison Rod Assembly Handling
             Tool
          Fuel Handling Instruction FHI-14, Thimble Plug Handling Tool
          Fuel. Handling Instruction FHI-17, Rod Cluster Control Change Tool
          Administrative Instruction AI-26, Prevention of Foreign Material in the
             Primary System                                  -
          Restart Test Instruction (RTI)-2, Core Loading
          Technical Instruction (TI)-1, SNM Control and Accountability System
          No violations or deviations were identified.

'

      14. Inspection Plan for Followup of Sequoyah Nonconformance Report
          A staff review was conducted, by a team of NRR technical reviewers and
          Region II personnel,.of the management processes involved in the resolution
          of Nonconformance Report (NCR) SQNNEB 8501 and its associated Failure
          Evaluation Engineering -Report (FEER). Attendant to this staff review,
          selected NCRs and FEERs were collected for additional evaluation. As a
          result of this additional review several cases were identified where
          potential safety questions were raised. Safety Evaluations were made by the
          staff for each safety question and required inspection effort was identified
          in a staff memo (Verrelli et al to Denton) dated August 9, 1985.
          An ' inspection plan for followup of the Sequoyah NCR open concerns was
          established by Region II in a staff memo (Weise to Walker) dated
          September 23, 1985, that identified several items which required resident
          inspector followup. The status of those items which required resident
          inspector followup is indicated below:
          a.    NCR SQN CEB 8406 involved two air clean up units that were not welded
                to their steel supports in accordance with TVA. drawing 48N726. The
                welds were later upgraded to the requirements of drawing 48N726 under
                Maintenance Request A236959. The welding discrepancy was an undersized
                weld which was later determined to have been a temporary fit-up weld
                that should have been replaced with a permanent weld after
                installation.    The licensee inspected all applicable welds in the
                mechanical equipment room and identified no other welds which were
                undersized. These particular welds, because of their temporary nature,
                did not have strike numbers or other means with which to identify the
                crew that performed the welds.      The licensee's corrective action
                appeared to be adequate in this instance, and this item is closed,
          b.    NCR SQN EEB 8406 involved some Class 1E 480 volt switchgear breakers
                and motor control center molded case circuit breakers which could be
                subjected to fault currents beyond their design capability. A FEER was
                issued by the licensee identifying this condition as a Category III. A
                Category III indicates that a component is unable to perform its
                required design function unless corrective modifications are made.
                Subsequently a safety evaluation was performed and found that the
                condition did not impact the safety of the plant and that no
                operational limitations were required. As a result of staff review it
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        was determined that certain aspects of the FEER were deficient and the
         licensee committed to revise the NCR. The inspector obtained a copy of
       -the revised NCR 'and transmitted it to the appropriate Region II
        personnel. -In addition, it appeared that the original NCR was written
        before a calculated load study was completed and there was. no

i statistical validity for the assumptions made in the FEER. As a result

        of the~ revised NCR, this item was reduced. in condition to a Category I,
        acceptable for all modes of operation and design conditions. For the
       . purpose of this. inspection, this item is considered closed.
    c.  NCR SQN NEB 8407 involved eight Class IE radiation monitors which had
        been miswired or had their identification tags interchanged. This item
        was the subject of ' Region II enforcement action (327,327/84-38). The
        . licensee's response to this enforcement action was reviewed by the
         inspector. A team inspection is planned to address the NRC order EA
        85-49 which will include a review of the licensee's NCR corrective
       ' actions. After the team inspection is complete the inspector. will
        review the licensee's corrective actions for the previous violation.
        For the purposes of this review plan, this item is closed.
    d.  NCR SQN NEB 8408 involved a relative humidity control component which
        could fail as a result of high radiation during a reactor accident.
        The licensee's resolution to this issue was to allow the relative
        humidity heater to energize when the fan starts and reaches full speed.
        The relative humidity control component would be used for alarm
        purposes only. A ' review - of the adequacy of .TS surveillance was
        conducted by reviewing Surveillance Instructions SI-141 and -142 and
       . Technical Instruction TI-9.         The surveillances conducted on the
        Emergency Gas Treatment System appear to be adequate.. This issue is
        closed.
    e.  NCR SQN EEB 8412 involved Bettis Actuators with potential deficiencies.
        This issue was resolved in Inspection Report 327,3P8/85-26.
    f.  NCR SQN NEB 8413 involved a discrepancy between the as found spent fuel
        pool alignment and that alignment described in the FSAR. A review of
        the reportablity aspects of this issue was conducted, and the issue was
        determined not to be reportable. An update was made on the most recent
        FSAR amendment submittal by the licensee to reflect current spent fuel
       . pool alignment. A review of the established makeup sources and
        applicable procedures, System Operating Instructions 501-70.1 and -78.1
        and Abnormal Operating Instruction A0I-15, was conducted. The
        procedures and system alignments appear to be adequate and in
        compliance with TS. This issue is closed.
 _.

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