ML20153D508

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Confirms Telcon Rept of 880827 Oil Spill During Operator Attempt to Dewater Oil/Water Separator,Resulting in Discharge to Outfall 004.Operators to Exercise More Caution During Dewatering Until Chiller Operation Curtailed
ML20153D508
Person / Time
Site: North Anna  Dominion icon.png
Issue date: 08/29/1988
From: Marshall B
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To: Kregloe W
VIRGINIA, COMMONWEALTH OF
References
NUDOCS 8809020231
Download: ML20153D508 (2)


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.% Glen Allen, Virgtnia 23060 August 29, 1988 6 w- m Mr. William L. Kregloe State Water Control Board Valley Regional Office 116 North Main Street P.O. Box 268 Bridgewater, Virginia 22812

Dear Mr. Kregloe:

Re: OIL SPILL AT NORTH ANNA POWER STATION This letter is to confirm our report of an oil spill on Saturday, August 27, 1988. The s Office (Roberts) pill was hours.

at 1122 reported by telephone to the Valley Regional The spill occurred at 0900 hours0.0104 days <br />0.25 hours <br />0.00149 weeks <br />3.4245e-4 months <br />, August 27, 1988 as an operator

' attempted to dewater che oil / water separator. Over the past several weeks the separator has been operating at full capacity due to condensate from the steam cF.ellers entering turbine building sumps. These chillers are only used 'n hot weather. As the operator initiated dewatering some 10-20 gal of oil were carried over, discharging to the discharge caral at Outfall 004. The operator imediately terminated dewatering and began cleanup.

A permanent boom around Outfall 004 was adjusted to contain most of the oil and absorbent pads were used to soak up the oil from the water's surface. No oil escaped the boom permanently deployed at the end of the discharge canal. No oil was deposited on the shoreline and no adverse environmental impact was observed.

Operation of the steam chillers will be curtailed in the near future as the weather cools. This will reduce the volume of water entering the sump system and therefore lessen the risk of a reoccurrence of such a spill. Until then operators will exercise even more caution during the dewatering operation.

pQb 8809020231 000829 PDR ADOCK 05000330 ) g P PNU \

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Mr. William L. Kregloe Page 2 August 29, 1988 If you have any questions regarding the incident, please contact my office.

Sincerely, B. M. Marshall, P.E.

Manager Water Quality GRK:ro:1328 cc: U.S. NRC Docket No. 50-338/50-339 101 Marietta St., NW Suite 2900 Atlanta, Georgia 30323 IV.5;2 NRC J!

Attn: Docket Control Desk Docket No. 50-338/50-339 Washington, DC 20555 NRC Senior Resident Inspector Docket No. 50-338/50-339 North Anna Power Station

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