ML18085A942
| ML18085A942 | |
| Person / Time | |
|---|---|
| Site: | Salem |
| Issue date: | 02/19/1981 |
| From: | Steele W Public Service Enterprise Group |
| To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| Shared Package | |
| ML18085A938 | List: |
| References | |
| LER-81-012-03L, LER-81-12-3L, NUDOCS 8102270723 | |
| Download: ML18085A942 (1) | |
Text
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (7-;t7l __ -- ;;.
-LICENSEE EVENT REPORT
- C::ON,TRO,L J
I BLOCK: ~1_..__,__....___...__........__.6~ IIi" (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) fB:D *IN- IJ 7 8 9 Is I LICENSEE CODE GI sl1 Kvl 01 oj 14 15
-I ol ol ol ol ol -1 ol olG)l4 LICENSE NUMBER 25 26 I 1l 1l 1l 1l©I LICENSE TYPE JO I
57 CAT 58 10 CON'T
~ =~~~~~ LlJ©I ol sl olo I ol 2l 1l 21G)lo 1210 l4 ls t1l@I012111918111@
7 8 60 61 DOCKET 'llUMBEA 68 69 EVENT DATE 74 75 REPORT DATE BO _
EVENT DESCRIPTION AND PROBABLc CONSEQUENCES@
I During normal operation on 2/4/81, the #2 Fire Pump in the Fire Suppression Water
((JI] I System was declared inoperable in order to repair a leaking inlet cooling water line.I
~ Action Statement 3.7.10.l(a) was entered at 1625 hours0.0188 days <br />0.451 hours <br />0.00269 weeks <br />6.183125e-4 months <br />.
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ITID
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7 8 9 80 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUB CODE SUBCOOE
[ill] IA I Bl@ L!J@ L!..J@) I PII I Pl El XI x1@ ~ ~@
7 8 9 10 11 12 13 18 19 20 SEQUENTIAL OCCLJRAENCE REPORT REVISION r.-:;-. LE A-Ao CV ENT YEAR REPORT NO. CODE TYPE NC.
\;.:.; REPORT NUMBER I 8 11 I l==1 10 11 12 I I/I Io 13 I L!J L=J LQJ 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN t::::::i ATTACHMENT NPR0-4 PRIME COMP. COMPONENT TAKEr.i ACTION ON PLANT METHOD HOURS ~ SUBMITTED FORM SUB. SUPPLIER MANUFACTURER w@W@) ~@ ~ 10 10 10 1° 40I~@ ~ ~@ I Al 3js1 Bl@
33 34 35 36 37 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @
IJJ]J I A corrugated stainless steel hose that connects the common cooling water piping shared by the pump and its starting diesel was leaking. The hose was replaced in kind. The Action Statement was terminated at 2140 hours0.0248 days <br />0.594 hours <br />0.00354 weeks <br />8.1427e-4 months <br />.
rrrn 7 B 9 80 FACILITY M~oom ~
STATUS % POWER OTHER STATUS DISCOVERY DISCOVERY DESCRIPTION ~
EJI]8 ~@ 11 I 0 I 012J@I- - 1 3 - - - -N/A ~~._l_O_p_e_r_a_t_o_r_o_b_s_e_r_v_a_t_i_*o_n___________,
7 9 10 -'"--,.---44 45 46 80 ACTIVITY CONTENT ~
RELEASED OF RELEASE AMOUNT OF ACTIVITY ~ LOCATION OF RELEASE @
~~@W@I* N/A N/A 7 8 9 10 11 44 45 BO PERSONNEL EXPOSURES (:;;;.,
NUMBER t::::::i TYPE DESCRIPTION~
EI?]
7 B 9 I 0 .I 0 I 011lL!J@ 12 1._3_ _ _ _
N A
...._~------------------------------8 ...
0 Pl!RSONNEL INJURIES (;"";\
r.;-r;:"'1 NUMBER DESCRIPTION6
~I 1 - 8 9 ol ol oj@).._~~~~~N~A~~~~---:-~----------~------------------
11 12 BO LOSS OF OR DAMAGE TO FACILITY l.iJ\
TYPE DESCRIPTION ~
~
7 B 9 l;J@).__~~~~~~--=N~A~~~~~~~~~~~~~~~~~~~~~~
10 BO PUBLICITY C\
ISSUED/,;;\ DESCRIPTION~ 81 0221 .., NRC USE ONL y .,
I2I£)
7 8 9 L!Ll6l N/A - (} ,;Q3 1 - - - - - - - - - - . = : . . t . . . = . - - - - - - - - - - - - - - - - - - - - - J 6 B 69 11111111JI11 f!
80 ;
0 NAMEOFPREPARER ____ w_._J_._s_t_e_e_l_e__________ PHONE: _ _6_0_9_-_9_3_5_-_0_9_9_B_ _ __ II.
"