ML20054K737
ML20054K737 | |
Person / Time | |
---|---|
Site: | |
Issue date: | 06/24/1982 |
From: | Tipps S GEORGIA POWER CO. |
To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
Shared Package | |
ML20054K738 | List: |
References | |
LER-82-063-03L, LER-82-63-3L, NUDOCS 8207060105 | |
Download: ML20054K737 (2) | |
Text
NRC FORM 36A U. S. NUCLE AR REGUL ATORY COMMISSION 87 77)
LICENSEE EVENT REPORT CONTROL BLOCK: l l l l l 1 l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6 7
0 t 8 9 l G l LICENSEE A l E lCODE I l Il l 2 14 l@l 15 0 l 0 l- l 0 LICENSE l 0 l 0NUMBER l 0 l 0 l- l 0 l 025 l@l26 4 l1LICENSE l1 11 l 1 l@l$7 CAT TYPE JO l
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SllR l60L l@l61 015101010131616 DOCK ET NUMBER l@l 68 0 is 11 69 la l n 19 l@l 75nl AREPORT EVENT DATE 74 la 1 2 80l@
19 ItDATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h I O l 2 l l On June 14, 1982, with Unit Two at approximately 97 MNT and incrnasing i 10 l 31 l power in startup modo, performance of procedure "Consip Delphi Model l lo l4 l l K-IV Ilydrogen and Oxygen Analyzer FT and C", discovered that thn "n" l O s l containment 112 O2 Analyzer was out of calibration. Unit Two Tech Specs 1 0 6 l Table 3.3.6.4-1 requires this channel to be operable. Thn vn d u n d a n t- "A" l l 0 l i ] l system was available. Plant operation was not affected. The health nnal 10 ls i I safety of the public was not af fected. This event was not vnnneieiun-
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_ SEQUENTIAL OCCURRENCE REPORT REVISION LE RiRO EVENT YEAR R EPORT NO. CODE TYPE N O.
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43 l44X l 9 l 9 ! 479 lh CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 11 101 lThe cause of this event has benn att-ri burna en incernmnne a ,-i f e This I i i l instrument was recalibrated and returned to service as part nf +- h n I i 2 l functional test and calibration procedure being performed at the timo ofl i 3 l discovery. This instrument is scheduled for replacement with an I i 4 l environmentally qualified instrument, approximatelv June, 1983. I 7 8 9 80 ST S % POWER OTHER STATUS IS O RY 'SCOVERY DESCRIPTION R Wh lO 10 l4 l@l N/A l (.B.j@l Routine zurveillance !
ACTIVITY CO TENT nELEASED OF RELE ASE AMOUNT OF ACTIVITY LOCATION OF RELEASE W [Z_jh 7 8 9 (Z_j@l10 11 N/A 44 l lN/A 45 80 l
PE RSONNEL E XPOSURES NUMBE R TYPE OESCRIPTION y l 0 l 0 l 0 l@l Z l@l N/A l PE RSONNE L INJU IES NUMBE R DESCRIP TION i n l 0 l 0 l 0 l@l N/A l 7 8 9 11 12 80 LOSS OF OR DAMAGE TO F ACILITY h TVfE DESCRIP TION %,/
1 9 (,Z_J@l N/A l T H 9 10 80 PUB LICIT Y isSut o DESCRIPTION
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4 U,N 8207060105 820624 NRC USE ONLY 1.Njbl PDR ADOCK 05000366 %
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NAME OF PREPARER
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LER #: 50-366/1982-063-Licensee: Georgia Power Company Facility Name: Edwin I. Hatch Docket #: 50-366 Narrative Report for LER 50-366/1982-063 On June 14, 1982, with Unit Two-increasing power from approximately 97 MWT, and while performing routine surveillance, per procedure "Consip Delphi Model K-IV Hydrogen and Oxygen Analyzer FT and C",
the "B" containment Hydrogen and Oxygen Analyzer was discovered to be out of calibration. (Analysis for both Hydrogen and Oxygen as indicated was low.) Technical Specificiations Table 3.3.6.4-1 i requires two operable channels. This requirement was not met during f the period the instrument was out of calibration. The last recorded a calibration occurred after maintenance to replace the internal sampling. flow components which was completed June 4, 1982. The redundant "A" Analyzer was operable. This event-has no effect on l the Unit One H2 O2 Analyzer which is supplied by a different manufacturer. Plant operation was not affected. The health and i safety of the public was not affected. This event was not repetitive.
- The cause of this event has been attributed to instrument drift.
The instrument was recalibrated, as part of the functional test and 4
calibration procedure being performed at the time of the discovery, and returned to service.
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