ML17333B038

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Responds to NRC 970815 Ltr Re Violations Noted in Insp Repts 50-315/97-09 & 50-316/97-09 on 970505-23.Corrective Actions: Calculation DC-D-1-SI-F101 Was Revised & Approved on 970602 to Address Cited Discrepancies
ML17333B038
Person / Time
Site: Cook  
Issue date: 09/15/1997
From: Fitzpatrick E
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
50-315-97-09, 50-315-97-9, 50-316-97-09, 50-316-97-9, AEP:NRC:1260H, NUDOCS 9709230028
Download: ML17333B038 (19)


See also: IR 05000315/1997009

Text

CATEGORY l REGULATORY

INFORMATION

DISTRIBUTION

SYSTEM (RIDS)DOCKET 05000315 05000316 NOTES: CCESSION NBR:9709230028

DOC.DATE: 97/09/15 NOTARIZED:

YES FACIL:50-315

Donald C.Cook Nuclear Power Plant, Unit 1, Indiana M , 50-316 Donald C.Cook Nuclear Power Plant, Unit 2, Indiana M AUTH.NAME AUTHOR AFFILIATION

FITZPATRICK,E.

Indiana Michigan Power Co.RECIP.NAME

RECIPIENT AFFILIATION

Document Control Branch (Document Control Desk)SUBJECT: Responds to NRC 970815 ltr re violations

noted in insp repts 50-315/97-09

a 50-316/97-09

on 970505-23.Corrective

actions: calculation

DC-D-1-SI-F101

revised a revised safety review incorporating

correct MDAFW pump start time approved.DISTRIBUTION

CODE: IE01D COPIES RECEIVED:LTR

ENCL SIZE-TITLE: General (50 Dkt)-Insp Rept/Notice

of Violation Response INTERNAL: RECIPIENT ID CODE/NAME PD3-3 PD AEOD/SPD/RAB

DEDRO NRR/DISP/PIPB

NRR/DRPM/PECB

NUDOCS-ABSTRACT

OGC/HDS2 COPIES RECIPIENT LTTR ENCL ID CODE/NAME 1 1 HICKMANiJ 1 AEODf&T~1+FILE CEHTE~RQN 1/DRC@HHFB 1 NRR/DRPM/PERB

1 OE DIR 1 RGN3 FILE 01 COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 0 R EXTERNAL LITCO BRYCE g J H NRC PDR 1 1 NOAC 1 1 NUDOCS FULLTEXT 1 1 1 1 D 0 N 0 NOTE TO ALL"RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE.TO HAVE YOUR NAME OR ORGANIZATION

REMOVED FROM DISTRIBUTION

LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD)ON EXTENSION 415-2083 TOTAL NUMBER OF COPIES REQUIRED: LTTR 18 ENCL 18

0

indiana Michigan Power Company 500 Circle Orive Buchanan, Mi 491071395 INDIANA ItrIICHIGAN

PWER September 15, 1997 AEP:NRC:1260H

10'CFR 2.201 Docket Nos.: 50-315 50-316 U.S.Nuclear Regulatory

Commission

ATTN: Document Control Desk Washington, D.C.20555 Gentlemen:

Donald C.Cook Nuclear Plant Units 1 and 2 NRC INSPECTION

REPORTS NO.50-315/97009 (DRP)AND 50-316/97009 (DRP)REPLY TO NOTICE OF VIOLATION This letter is in response to a letter from G~E.Grant, dated August 15, 1997, that forwarded a notice of two violations

of NRC requirements

to Cook Nuclear Plant.The violations

were identified

during the operational

safety team inspection (OSTI)conducted by the NRC from May 5, 1997, to May 23, 1997.The attachment

contains our response to these violations.

Commitments

were made by Cook Nuclear Plant personnel to the NRC OSTI.The inspectors

identified

concerns related to valve descriptions

on labels, drawings, and in procedures, and they had concerns related to our program for sealed valves.The characterization

and detail of these commitments

in the inspection

report reflects our intent.when the commitments

were made.The second violation relates to the issue of design control.While reviewing the OSTI report and preparing this response, Cook Nuclear Plant underwent an NRC architect engineering (AE)team inspection.

The AE inspection

identified

design control issues, some that are similar to those cited in this violation.

Resolution

of the overall design control issue will require action beyond that which is committed to here.Those actions will be defined in the course of addressing

the AE team inspection

issues.The nuclear engineering

organization, along with our entire nuclear generation

group, understands

the importance

of error free human performance

and attention to detail, and to having a design basis that is clear, understandable, and retrievable.

We believe that a first step was taken on September 2, 1997, when standards for technical information

exchange and use in the nuclear engineering

9'709'230028

9709i5 PDR ADQCK 050003%5 8 PDR r.~~0,<iQ ,,s llllllllilllliIIIJlllllllllllliillilf

ill

U.S.Nuclear Regulatory

Commission

Page 2 AEP: NRC: 1260H organization

were formally established.

The objective of the guidance is to provide assurances

that technical information

is accurate, based on sound engineering

principles, properly conveyed, and properly, documented.

Sincerely, E.E.Fitzpatrick

Vice President SWORN TO AND SUBSCRIBED

BEFORE-ME THIS I'5 DAY OF~LV', 1997 Notary Public My Commission

Expires vlb Attachments

JAN WA%0N CAARYPQSC,BBNKNcoWn, e MYCOMMSSOM

EXPtRES FEL 10, 1999 c: A.A.Blind A.B.Beach MDEQ" DW&RPD NRC Resident Inspector J.R.Padgett

ATTACHMENT

TO AEP:NRC: 1260H REPLY TO NOTICE OF VIOLATION:

NRC INSPECTION

REPORT NOS.50-315/97009 (DRP)AND 50-316/97009 (DRP)

Attachment

to AEP:NRC:1260H

Page 1 On May 23, 1997, the NRC completed an operational

safety team inspection (OSTI)of Cook Nuclear Plant units 1 and 2 reactor facilities.

Two violations

of NRC requirements

were identified

during this inspection.

In accordance

with the 60 FR 34381,'General Statement of Policy and Procedures

for NRC Enforcement

Actions", dated June 30, 1995, the violations

and our responses are provided below.NRC Violation I"10 CFR 50, Appendix B, Criterion V,'Instructions, Procedures, and Drawings,'equires, in part, that activities

affecting quality be prescribed

by procedures

of a type appropriate

to the circumstances

and be accomplished

in accordance

with these procedures.

Contrary to the above, On May 10, 1997, the inspectors

identified

that safety related Temporary Modification (TM)1-95-1, which did not require an outage for restoration, had been assigned a (administrative)

date of August 27, 1996, but had not been made a permanent installation

through a design change or been removed as of May 10, 1997 as required by Plant Managers Procedure (PMP)5040.MOD.OO1,'Temporary

Modifications,'evision

7.B.On May 7, 1997, the inspectors

identified

that an activity affecting quality, the deenergization

of the DG2AB inverter, was completed without placing 2-DGAB-INV-CB2

and 2-DGAB-INV-

CB1 to off, contrary to steps 2.1.2 and 2.1.3 of procedure 02-OHP 4021.032.008

'Aligning DG2AB Subsystems

For Standby Operation,'evision

4, Attachment

7.This is a Severity Level IV violation (Supplement

I)." Res onse to NRC Violation I The letter from Mr.Grant, and the notice of viola'on, state that Cook Nuclear Plant's staff provided the NRC with satisfactory

information

regarding the reasons for the violation, and the corrective

actions taken and planned to correct both examples of the violation and prevent recurrence.

The letter goes on to say that, unless our corrective

actions or our position are not accurately

reflected in the inspection

report, we are not required to further respond to this violation.

We have reviewed inspection

report no.50-315/316)-97009

and determined

that it reflects the circumstances

of the examples in the violation as cited, as well as the corrective

actions taken for each.Notwithstanding, for consistency

in understanding, there is information

in the discussion

section of the inspection

report that we wish to clarify.Several condition reports (CRs)are listed as having been reviewed in conjunction

with'he 2AB EDG voltage regulator work.In particular, CR 97-1452 is listed with the title"Partial Clearance Addition Determined

As Root Cause for Blown Fuse On 2AB EDG Inverter." We would like to clarify that the failure to deenergize

the EDG inverter using the appropriate

procedure is not

0

Attachment

to AEP:NRC:1260H

Page 2 considered

to be the root cause for the inverter fuse blowing during reenergization.

Subsequent

investigation

has determined

that the failure to follow'the deenergization

procedure was recognized

before actions were taken to reenergize.

Prior to using the procedure to reenergize

the inverter and place it back in service, the inverter circuit alignment was corrected and the integrity of the fuse was verified.The fuse did blow coincident

with performance

of the procedure to reenergize

the inverter.NRC Violation ZZ"10 CFR 50, Appendix B, Criterion ZZZ, requires, in part, that mdasures be established

to assure that the design basis are correctly translated

into specifications, drawings, procedures, and instructions.

Design control measures shall provide for verifying or checking the adequacy of design.Contrary to the above, design control measures were not adequate to assure that the design basis was correctly translated

into design modification

documents:

b.On May 7, 1997, the inspectors

identified

that calculation

DC-D-1-SZ-F101,'Stress Analysis&Load Generation

for System 1-SI-F101 Per 12-MM-590,'sed

the wrong moment arm and had a missing reaction force and moment.On May 13, 1997, the inspectors

identified

that incorrect and non-conservative

design input was used for the motor-driven

auxiliary feedwater pump start time in the Safety Review Memorandum

f or the Setpoint Values f or the Time Delay Pickup Relays in the AFW Flow Retention Circuits, dated January 15, 1997, for design change package 12-DCP-0817,'Revise Aux.Feedwater Flow Retention Circuit.', On May 13, 1997, the inspectors

identified

that a calculation

for the seismic design adequacy of minor modification

12-MM-337 was not per formed.The design package for 12-MM-337 indicated this calculation

existed as DC-D-12-ES-116.

This is a Severity Level IV violation (Sur,v>lement

I)." Res onse to NRC Violation ZZ 1.Admission or Denial of the Violation We admit to violation ZI as cited in the NRC notice of violation.

Reasons for the Violation , The examples cited in the violation represent issues in the area of design control.Concurrent

with the review of the OSTI report and preparation

of this response, Cook Nuclear Plant underwent an NRC architect engineering (AE)team inspection.

This inspection

identified

design control issues, some that are similar to those cited in the violation.

Zt is recognized

that the three examples cited in this notice of violation must be

0

Attachment

to AEP:NRC: 1260H Page 3 considered

along with any new issues identified

by the AE team inspection, relative to the overall issue of design control.The circumstances

of each issue cited in this notice of violation are discussed below.Calculation

DC-D-1-SI-F101,"Stress Analysis and Load Generation

for System 1-SI-F101 per 12-MM-590", was performed in support of adding a permanent vent line to the safety injection system (SIS)piping.The inspector's

review of the design change package identified

errors made by the authors and overlooked

by the calculation

reviewers.

The errors are characterized

as insufficient

attention to detail on the part of the engineers performing

and reviewing the design change package.When calculating

reaction forces, the length value of a piping span, used as a moment arm in the calculation, was transcribed

from the input data presentation

to the actual algebraic presentation

incorrectly, from 37-5/8" to 35-5/8".This discrepancy

caused the maximum reaction force result to be incorrect, but in a conservative

direction.

In another section of the package, values for reaction force and moment were omitted from a summary format.These discrepancies

consisted of numbers correctly derived in the body of the calculation

on one page, but omitted from the summary on the following page.This problem was administrative

in nature;no incorrect information

was presented or used as a result.A third discrepancy

related to this design change package was noted in the body of the inspection

report, but not specified in the notice of violation.

The inspector made an observation

that incorrect design information

was stated in the safety review documentation.

Our investigation

concluded there was no discrepancy

in the safety review input information.

The values of design temperature

and pressure used by the safety reviewer were correct for the specific location where the new vent valve was to be installed.

The engineer performing

the design calculation

conservatively

used the highest bounding design temperature

and pressure for the SIS as a whole.This approach is often adopted when the inherent safety margin of a design is such that the more stringent design requirements

can be accommodated.

The thought process involved in taking this approach was not clearly documented

in the calculation

package.Design change 12-DCP-0817

was developed to add a time delay relay to the auxiliary feedwater (AFW)flow retention actuation circuit to prevent spurious actuation from momentary outlet pressure spikes, especially

those that occur when the AFW pumps

0

Attachment

to AEP:NRC:1260H

Page 4 automatically

start.A safety review was performed by the design engineering

organization

for the addition of the time delay pick-up relay to the AFW system circuits.The nuclear safety and analysis section was asked to perform an evaluation

of the setpoint value for the time delay relay.The review performed by this group was intended to demonstrate

that the magnitude of the time delay in the flow retention circuits would not adversely impact related accident analysis assumptions

or safety margins.In order to complete this review, the engineer needed to know how quickly the motor driven AFW pumps would start.An'incorrect

value of thirty seconds was used, based on a telephone conversation

with the AFW system engineer at the plant site.The system engineer communicated

that the turbine driven AFW (TDAFW)pumps start and come up to speed within thirty seconds.Surveillance

data on the TDAFW pumps was available on the system engineers desk at the time.What the system engineer intended was that thirty seconds would bound the start time on the motor driven pumps.Most often, in relation to safety analysis or T/S surveillance, the information

of concern is a time which bounds the pump start, time.However, the safety reviewer understood

that the thirty seconds would characterize

the start time for the motor driven auxiliary feedwater (MDAFW)pumps.Based on surveillance

measurements, the correct start time for the motor driven pumps is three seconds.Investigation

into the reason for this incorrect input to the safety review concluded that it was poor communications

between the involved engineers, and an incomplete

understanding

on the part of the system engineer as to the intended use of the information.

One engineer believed the bounding start time was needed, while the other was trying to determine the shortest start time for the pumps.Minor modification

12-MM-337 was performed to replace the emergency diesel generator (EDG)starting air system safety valves.The NRC inspector indicated that the calculation

for the seismic adequacy of the new valve type was not performed.

The design change package referenced

calculation

DC-D-12-ES-116.

This referenced

calculation

was not intended to follow the typical format in what was then the calculation

procedure.

DC-D-12-ES-116

was a record-keeping

and retrieval file for a number of individual

reviews prepared for the replacement

of non-identical

valves.The file did contain the final approval letter from the structural

design section documenting

that the valve change had been reviewed.However, we would have expected to find information

in this file related to

Attachment

to AEP:NRC:1260H

Page 5 the decision making process, such as isometric data, weight data, and support location information.

For unknown reasons, this file did not contain the information

that would have been expected pertaining

to the review of the valve replacement

of 12-MM-337.

The information

could not be found.It was reconstructed

and the new review was documented

appropriately.

The file now contains the appropriate

information

and review documentation (performed

in May 1997)that confirmed the conclusion

of the original design approval letter.Whether the file was lost, or the review never documented, this condition is characterized

as insufficient

attention to detail.It resulted in the inability to retrieve design data or design basis related information.

3.Corrective

Action Taken and Results Achieved b.c Calculation

DC-D-1-SI-F101, for the safety injection system stress analysis, was revised and approved on June 2, 1997, to address the cited discrepancies.

On May 29, 1997, a revised safety review, incorporating

the correct MDAFW pump start time was approved by the plant nuclear safety review committee (PNSRC).The conclusions

of the original safety review remained unchanged.

A walkdown and review of the valves installed under 12-MM-337, for the EDG starting air system, was performed on May 13, 1997, and documented

with the related condition report.This review confirmed the original conclusions

of the seismic qualification

review performed in 1992.The review was formally documented

on May 15, 1997.Corrective

Actions Taken to Avoid Further Violations

We understand

the importance

of"attention

to detail", and to having a design basis that is clear, understandable, and retrievable.

Each of the three cited examples in the NRC inspection

report refer to a lack of"attention

to detail", or a lack of clear communication

of design information.

The three examples of design control problems highlighted

in this violation will be considered

again as a part of the larger set of issues identified

by the NRC AE team inspection

of Cook Nuclear Plant.Resolution

of the overall design control issue will require action beyond that which is committed'in this response.Those actions will be defined in the course of addressing

the AE team inspection

issues.The violation examples a.and c.have been characterized

as insufficient

attention to detail.When the errors were identified

by the inspector, discussions

were held with the engineers in the design engineering

organization

who are involved in the development

and

0

Attachment

tq AEP:NRC:1260H

Page 6 documentation

of the calculations.

They were made aware of the inspection

findings and the importance

of attention to detail.This was accomplished

while the OSTI was still in progress.Training will be provided for personnel in the nuclear engineering

organization

who perform, review, and approve engineering

and design calculations.

The session will emphasize the importance

of"attention

to detail" and good calculation

control processes.

This training will be completed by December 31, 1997.In 1990, as a result of design verification

concerns raised during the safety system functional

inspection

of our essential service water system, quality review teams (QRTs)were established

to periodically

review design output documentation

for technical adequacy and procedural

compliance.

These teams were disbanded in 1996.The discrepancies

found under the QRT program had no impact on the conclusions

of the calculations.

Selected calculations

performed during the past year, August 1996, to August 1997, will be reviewed.The review will look for calculation

errors, inconsistencies, proper documentation

of assumptions, and procedure adherence.

Any findings will be addressed and documented

under the corrective

action program.This assessment

will be completed by December 1, 1997.The problem cited in example b.of the violation, incorrect data input to a safety review, has been identified

to be a communication

problem.On August 26, 1997, the nuclear safety and analysis section conducted a tabletop session that discussed the need for precision in the use of technical information

in safety reviews.It stressed that the use of written input is the preferred method, and that if verbal communication

is needed, it must be followed up with a written document.These standards for information

exchange and use were formally established

by procedural

direction issued on September 2, 1997.This document provides requirements

for nuclear engxneering

organization

personnel when providing technical direction.

The objective of the standard is to provide assurances

that the information

is accurate, based on sound engineering

principles, properly conveyed, and properly documented.

5.Date When Full Com liance Was Achieved Relative to the individual

examples cited in the violation, full compliance

was achieved: On June 2, 1997, when calculation

DC-D-1-SI-F101

was reviewed and approved for the safety injection system stress analysis.On May 29, 1997, when the revised safety review for the AFW flow retention time delay relay setpoint was approved by the PNSRC.

I 1

Attachment

to AEP:NRC:1260H

Page 7 On May 15, 1997, when walkdown and review of the seismic qualification

of the EDG starting air system safety valves was documented

and verified.