ML18059A931

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Responds to NRC Ltr Re Unresolved Items & Weakness Noted in Insp Rept 50-255/94-02.Corrective Actions:Evaluation of Appropriate Fouling Factor Assumptions Made in Heat Exchanger Performance Calculations Will Be Completed
ML18059A931
Person / Time
Site: Palisades 
Issue date: 04/08/1994
From: ROGERS D W
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9404150058
Download: ML18059A931 (13)


See also: IR 05000255/1994002

Text

consumers

Power l'OWERINli

MICHlliAN-S

PIUlliRESS

Palisades

Nuclear Plant: 27780 Blu.e Star Memorial Highway, Covert, Ml 49043 April 8, 1994 Nuclear Regulatory

Commission

Document Control Desk Washington, DC 20555 David W. Rogers Plant Safety and Licensing

Director DOCKET 50-255 -LICENSE DPR-20 -PALISADES

PLANT -RESPONSE TO NRC INSPECTION

REPORT 94002, SERVICE WATER OPERATIONAL

PERFORMANCE

INSPECTION, UNRESOLVED

ITEMS AND WEAKNESSES

A Service Water System Operational

Performance

Inspection (SWSOPI) was conducted

at the Palisades

plant over the period from

10 through February 11, 1994. The report addressed

a number of unresolved

issues and weaknesses

for which we were asked to provide a response addressing

eath of these items including

our proposed corrective

actions. A specific

for providing

this response was not requested

in the inspection

report letter. Discussions

with the NRC inspection

team leader resulted in agreemerit

on a response date of April 8, 1994. * A ptoject team has been formed as a followup to the SWSOPI Inspection.

The team is presently

developing

a project plan which will at a

address completibn

of the actions identified

as followup to NRC Inspection

and a margin enhancement

plan for.the service water

Attached to this letter is the individual

responses

to each of the unresolved

items and weaknesses

identified

in the March 4, 1994 inspection

report. David W

Plant Safety and Licensing

Director CC:

Region Ill, USNRC Resident _lnspectori

Palisades

Attachment ('\. ;'"\ ::*, 9404150058

PDR ADOCK 05000255 Q PDR A CMSCNE7?GYCOMPANY

  • ATTACHMENT

Consumers

Power Company Palisades

Plant Docket 50-255 RESPONSE TO NRC INSPECTION

REPORT 94-002 SERVICE WATER OPERATIONAL

PERFORMANCE

INSPECTION

.. . UNRESOLVED

ITEMS ANO WEAKNESSES

April 8, 1994 * .

PERFORMANCE

INSPECTION

UNRESOLVED

ITEMS AND WEAKNESSES

UNRESOLVED

ITEMS Unresolved

Item 50-255/92028-03(DRS)

1 . Use of firewater

to provide backup water supply for auxiliary

feedwater (AFW). The NRC's concern was based on the lack of an analysis or testing to verify the fire water system's capability

to provide backup water to the AFW system. *The licensee committed

to complete an analysis to document the fire water

adequacy under action item request (AIR) A-PAL-92-098.

  • CPCo Response As part of the follbwup to NRC Inspection

Repcirt 92028, we were asked to respond within 60 days of the date of the report, to.Unresolved

Item 3. Our March 29, 1993 lettet to the NRC

our plans for completion

of the follow-up

actions for this unresolved

item. In summary, based on

judgement

we believe that the fire water pumps and interconnecting

system can provide the needed water to the auxiliary

feedwater

pumps suction. Action . Item Record -A-PAL-92-098

was written to provide an analysis demonstrating

the ability of.the fire water system to provide backup to the Auxiliary

Feedwater

Pumps. The target date for completion_of

the analysis is December 1994. Unresolved

Item 50-255/94002-01

  • The team identified

the 1 ack of over-pressure

protection

for CCW heat exchangers (HX) E-54A and E-548. The concern *i nvo 1 ved over-pressure

due to thermal expansion

stemming from service water valve isolation.

Palisades's

ASHE Code of record required each vessel to be protected

from any conditians

specified

in the certified

design specification.

The code further required to document the degree of over.:pressure

protection

in a summary technical

report. The licensee was unable to retrieve the summary technical

report that justified

the lack.of over-pressure

protection

prior to completion

of the inspection.

The licensee committed

to locate the report or perform the * technical

analysis to show Code compliance.

CPCo Response h*ve requested

the original plant architectural

engineer to complete a final search for the code-related

documentation

for the CCW heat exchangers

by May 6, 1994. If the search is

we will review the documentation

for acceptability.

If this search is unsuccessful, a summary technical

report documenting

whether over-pressure

protection

is needed will be

The issue of documentation

for the over pressure protection

of the CCW heat exchanger

will be completed

by June 15, 1994.

    • Unresolved

Item 50-255/94002-02

r The results of tests, ca7Cu7ations

and engineering

evaluations

were inconclusive

and could not be used to determine

if the SWS would fu1fi17 its safety related function at elevated Jake water temperatures

combined .with other adverse design basis conditions.

2 The licensee conc7uded

that the SW and CCW systems were currently

operable because current 7 ake water temp.eratures

were 7 ess than 50"F. This temperature

provided significant

margin to account for a77 issues impacting

the SW operability

margin. The licensee committed

to resolve the following

issues, documented

in DR D-PAL-93-272, by mid April 1994. A. Neither test results or design basis calculations

accounted

for * instrument

uncertainties.

8. The analyses that develop required flow. rates to HXs served by* the SWS used only the original design fouling. No calculations

had been performed

to eva 1 uate degraded HX performance

resu]ti ng from f ou 1 ing beyond the original design value. c. D. The most limiting system lineup may not have been teste.d. The impact of increased

sw*temperatures

and reduced SW f7ow rates on the SW and CCW design pressures

and tempera.tures

and systenis'

operation

was not .evaluated.

  • E. The root cause of declining

flow rates to control room chi77ers VX-10 and VX-11 had not been determined.

  • * F. As discussed

in Section 8.1, the SW pump.IST reference

values and pump degradation

was not coupled to the required system

G. The elevated lake water temperature

was. not incorporated

into the maximum allowable

SW system degradation . . Pending the licensee's

completion

of a77 the actions impacting

SWS margin documented

in DR D-PAL-93-272

and review by the NRC, this is considered

an unresolved

item (50-255194002-02).

CPCo Response We have made an operability

determination, as documented

in D-PAL-93-272, which concludes

that plant operation

up to 50°F lake temperature

is acceptable.

A

of historical

plant records show that the temperature

of Lake Michigan begins to approach a.nominal

temperature

of 50°F during the first part of May.

The lake temperature

limft of SO"F is being tracked on the plant Limiting Condition

for Operations (LCO} control board in the shift supervisors

office which tracks conditions

which effect plant operability.

As the evaluations

listed below progress and issues and uncertainties

are better understood, the operability

determination

may be revised. Such operability

determinations

will be documented

in an engineering

analysis and subjected

to appropriate

technical

reviews. As a result, the target completion

dates to attain a *maximum SWS inlet temperature

may be changed accordingly.

3 A. Action will be taken to account for instrument

uncertainties

associated

with the SWS and-CCW testing in an overall reanalysis*

of the syste_ms through coirective

action D-PAL-93-272.

The target date for completiori

of the

  • is May 8, 1994. ?. An additional

action to evaluate the link between analysis inputs and assumptions

used in testing practices

will also be completed

under corrective

action D-PAL-93-272

and is targeted for completion

by August 1, 1994. B. An evaluation

of

fouling

made in heat exchanger

performance

calculations

will be completed.

The evaluation

will determine

appropriate

fouling factors based on Tubular Exchanger

  • Manufacturers

As_soci at ion (TEMA} recommendat

i ans for existing service conditions, plus a review of existing maintenance

and testing practices

to determine

where degraded fouling assumptions

may be appropriate.

The target date for completion

of the corrective

action is May 8, 1994. C. An

to assure that the most limiting

hydraulic

lineup is considered

in our analysis will* be conducted

under D-PAL-93-272.

The current date for completion

of the corrective

action is May 8, 1994 .. D. An analysis to evaluate the impact of the elevated SWS _and CCW temperatures

on system design ratings and performance

will be completed

as corrective

actions under D-PAL-93-272.

The target date for completion

of this corrective

action is May 8, 1994. E. A corrective

action has been initiated

under D-PAL-93-272

which requires system engineering

to determine

and correct the cause of the reduced flow *to VC-10 and VC-11. The present plan to accomplish

this action includes a boroscope

inspection

of the subject service water piping to verify the piping is not fouled. We will also be looking at the instrumentation

for accuracy issues and tubing silting problems that may be contributing

to . *this apparent low flow scenario.

Based on these results, actions correcting

the deficiencies

will be taken .. These actions will be completed

during the 1995 refueling

outage. F. A corrective

action has been initiated

under D-PAL-93-272

to develop reference

values for SWS pump testing (IST} which are related to the design basis and accident analysis.

The corrective

action includes

    • 4 rev1s1on as necessary

of the appropriate

test procedures.

The target date for completion

of this corrective

action in June 15, 1994. G. Reanalysis

of the SWS performance

will ensure that the appropriate

maximum SWS inlet temperatures

are evaluated

along with the maximum expected system degradation.

This analysis will be completed

as a corrective

  • action under

The target date for completion

of the corrective

action is May 8, 1994. Unresolved

Item 50-255/94002-03

Corrective

actions in response to D-PAL-93-272

wi71 comple{e the development

of SWS pump testing reference

values and

system performance.

Additiona71y, the licensee intended to review the basis for IST reference

values and a77owed degradation

for a71 Section XI pump tests to ensure tha.t they were adequately

coordinated

with safety analysis performance

criteria.

This issue is considered

an unresolved

item pending the licensee's

review to determine

impact on the IST reference

values *and the possible effect on past ESS pump operability.

CPto.Response

As noted in response to

50-255/94002-02

Item F,. a corrective

action has been initiated

under D-PAL-93-272

to develop reference

values for SWS pump testing which are related to the design performance.

A

action was written under D-PAL-93-272

to develop a basis for reference

values for all safety related pumps in the Inservice

Test Program which are directly related to the design basis and accident analysis.

The corrective

action requires revision, as necessary;

of the appropriate

test procedures.

After the ISI pump reference

values are

reviews will be completed

to determine

the affect, if any, on past ESS pump bperability . . The target date for completion

of the corrective

action is August 1, 1994. WEAKNESSES

NRC Identified

Weakness The NRC inspectors

ran several scenarios

on the plant simulator.

The first *scenario

required*

the crew to isolate SWS critical header A to stop a leak. The SWS critical header A leak, .which was located in the CCW pump room, was not isolated until 30 minutes after the event was identified

by the crew. This created the potential

for flooding of the CCW pump room. Because procedure

ONP 6.1, "Loss Of Service Water," Revision 5, did not cont*atn any specific guidance to isolate the leak, operator aid (DA) 136 was

    • used,to determine

which valves should be closed to determine

leak location.

OA 136 was a SWS simplified

schematic

that was attached to the control panel. Although the crew successfu17y

isolated the SWS leak, identified

leak location, and determined

the impact on plant operation, the team considered

the delay to complete leak isolation

actions a weakness.

CPCo Response 5 . The simulator.scenario

consisted

of a service water line leak in the CCW Room on the 'A' Critical Service Water Header. The crew suspected

a service water system leak when the SWS standby pump

and critical service water system header pressures

dropped significantly.

The Shift Supervisor

subsequently

ordered an

down power, however during the down power, the plant was tripped due to voltage regulator

problems.

While the crew commenced

EOP 1.0, "Standard

Post Trip Actions," immediate

actions a LOCA event was

Shartly after completing

EOP 1.0, the LOCA was. identified

and the crew focused their immediate

priorities

on the LOCA since the service water critical header pressures

remained above the Safety Function

Check Acceptance

of 42 psig. After sufficient

action was taken on the LOCA, the crew re-directed

their efforts to isolating

the SWS leak which was approximately

30 minutes later: . -* *The following

actions will be performed

to enhance operator*response

in identifying

SWS leaks: 1. We will enhance ONP 6.1, "Loss of

Water," to effectively

proceduralize

a leak isolation

process. However, the procedure

will be changed only if we are sure that the probability

of

efficient

leak isolation

efforts is low. * 2. Additional

simulator

will be completed

on ONP 6.1, "Loss of Service Water." NRC Identified

Weakness This weakness identified

in the licensee's

operating

SOP 16, Steps 5.1.2 and 7.6 prevented

initiation*

of backup coo-Jing from the SWS to the ESS pumps if norma 1 coo*1 i ng from CCW was 1 ost concurrent

with an SI signal. Procedure

compliance

would prohibit opening the SWS valves to the ESS pumps with the CCW valves open. The CCW valves would remain open until the SI signal could be reset. Current procedural

compliance

results in loss of cooling water to the ESS pumps. The licensee indicated

that the procedure

would be revised to allow opening the SWS valves to the ESS pumps if the CCW valves were open and an SI signal was present. A CAUTION preceding

step 7.6 would also be added to alert the operator that CCW would drain to Lake Michigan with a resultant

loss of CCW

    • * system functions, if SWS coo 1 ing to the ESS pumps was a Ugned with either CCW valve open. CPCo Response 6 SOP 16, "Component

Cooling Water (CCW) System Procedure," Step 7.6 provides an option of supplying

service water to the ESS pumps with a loss of CCW cooling supply. This section required closure of the CCW supply and return valves prior to opening the SWS supply and return valves. A precaution, Step 5.1.2, also noted that the CCW supply and return valves shall not be open when the SWS supply and return valves are open since this would allow CCW system water drainage to the lake. The

could have been interpreted

as *: environmental

issue only. The procedure

also did not

address the* case when an SIAS signal was present and the CCW supply and return valves. could.not

be closed. The fo 11 owing actions wi 11 be performed

to correct this procedural

weakness:.

1. A caution was added to SOP 16, Section 7.6, identifying

the inability

to close the CCW supply and return valves with an SIAS si.gnal. The caution also indicates

that if the

water cooling option is performed, the.* CCW system will drain to the lake and CCW cooling to other plant equipment

would be lost. This action is completed . 2. SOP 16,

was revised to clearly._identify

the result* of draining CCW system to the lake. This actibn was completed.

3. SOP 16, Sections 7.6 and Step 5.1.2 will be revised in accordanc'e

with the* engineering

resolution

for resolving

the single failure

This action will be completed

after engineering

resolution

of the single *

vulnerability

of the CCW system. NRC Identified

Weakness This weakness was identified

in the licensee's

operating

procedures.

SOP 15, "Service Water System," Revision 7, Step 4.1.2 contained

a similar statement

as described

above. The licensee indicated

that this procedure . would be revised. CPCo Response The SOP 15, Revision 7, Step 4.1.2, requirement

coincides

with the requirement

of SOP 16, Step 5.1.2 .. SOP 15, Step 4.1.2 will be revised in

with the engineering

resolution

for resolving

the single failure concern. This action will be completed

after the engineering

resolution

of the single

vulnerability

of the CCW system.

    • 7 NRC Identified

Weakness *This weakness was

in the licensee's

operating

Response Procedure (ARP) 7, Window 29, "Service Water Bay 1 ow Level," did not provide guidance regarding

what level SW pumps should be . tripped if SW bay level was decreasing.

Thfs item was previously

identified

during the licensee's

SSDC conducted

in Hay 1990. The licensee indicated

that the procedure

would be revised. CPCo Response ARP 7, Window 29 will be revised tb provide

directions

to

for tripping the service water pumps. NRC Identified

Weakness This weakness was identified

in the licensee's

operating

procedures.

ONP 6.1, Revision 5, Attachment

1, "Alternate

Method of Supplying

the Intake* Structure," requited tripping the SW pumps if warm water recirculation

pump f P-5) was used to supply water to the intake structure.

This did not coincide *with SOP-14, "Circulating

Water and Chlorination

Systems," Revision 16, step 7.13.1, which provided steps to supply the intake structure

from P-5 but did. not require tripping the SW pumps. The licensee indicated

that'guidance

for tripping the SW pumps would be incorporated

into *the appropriate

ARP and removed from ONP 6.1, Attachment

1. No revisions

to SOP 14 were deemed necessary.

  • CPCo Response ONP 6.1, Revision 5, Attachment

1, was developed

on the assumption

of a collapsed

intake piping or crib. The result of such a collapse would be an immediate

emptying of the intake pump bay, therefore, the procedure

ensured that the SWS and dilution water pumps were tripped off. SOP 14, Step 7.13.1 was developed

as a warm water supply to melt ice off the traveling

screens, which does not necessarily

tripping of the SWS or dilution water pumps. The following

actions will be performed

to correct this procedural

weakness:.

1. ONP 6.1 has been revised to require tripping of the dilution water pumps only based on water cohservation

for the SWS system. 2. The ARP 7 will be revised to provide direction

when the SWS and dilution water pumps should be tripped off.

8 NRC Identified

Weakness The team identified

non-seismica11y

constructed

scaffolding, insta11ed

in the. west safeguards

room over safety-related

equipment.

The licensee performed

an engineering

analysis, which concluded

that the scaffolding

did not meet the * requirements

of procedure

HSH-H-43, "Scaffolding,".

Revision O, but was not a

concern. The licensee removed the scaffolding

and initiated

a revision to HSH-H-43 that provided additional

instructions

for scaffotding

in related areas. The revision would include walkdown inspections, supervisor

sign-off for installation, clarification

of requirements, and approval and justification

by the system or assigned engineer for deviations

from the procedure.

The team considered

this action acceptable.

  • CPCo Response On January 20, 1994, NECO Civil

performed

an analysis for scaffolding

and concluded

the scaffolding

did not

the requirements

of Procedure

MSM-M-43.

However, the scaffolding

did not reflect a safety concern. On January 21, 1994, plant maintenance

personnel

performed

a walkdown and found only one qther scaffold installed

in the plant. The installed

scaffold met the installation

requirements

of procedure

MSM-M-43 and there was no safety-related

equipment

involved.

On January 22, 1994, plant maintenance

repair workers dismantled

and removed the scaffolding

from the. West Engineering

Room. * As a result of this event the following

corrective

actidns will be taken: . . . 1. Procedure

MSM-M-43 will be revised to include (1) instructions

for walkdown inspection

for scaffolding

installed

in safety-related

areas; (2) a supervisor

sign-off for scaffolding

installed

in safety-related

areas; and (3) to clarify requirements (for free-standing, separation

_distances, braced scaffold, etc.) as they relate to requirements

for scaffolds

installed

in safety-related

,\ 2. Responsible

maintenance

supervisors

will be informed of the requirement

that any deviations

from the Procedure

MSM-M-43, with regard to general scaffolding

requirements

and requirements

for scaffolds

in safety-related

areas, require approval and justification

by engineering

before the scaffolding

can be accepted for use. 3. Training will be provided for Plant Maintenance

Supervisors

on their

ities

permanent

Maintenance

Procedure

MSM-M-43.

NRC Identified

Weakness The team identified

that a ground strap was not connected

on an recently replace containment

spray pump motor. DR D-PAL-94-017, evaluated

the problem . and co.ncluded

that the work package instruction

lacked the detail necessary

to ensure the ground strap connection.

The package also contained

other minor ;

discrepancies

as we17. The.licensee

the ground strap and was *developing

corrective

actions for the other minor deficiencies.

The team* considered

this attion acceptable.

CPCo Resoonse 9 The root cause of the condition (unconnected

ground strap) described

on . Deviation

Report (DR) D-PAL-94-017

can be attributed

to an inadequate

job plan on Work Order (WO) 24202957.

This WO plan did not contain sufficient

detail to ensure that the work would be

properly.

A procedure

exists (ESS-E-36)

that contains detailed steps concerning

the re-connection

of the ground strap on the motor, EMA-1114.

While.there

is no requirement

to use this procedure

for the replacement

of the motor, the WO plan should c6ntain an equivalent

amount of detail. * While reviewing

the WO package and related documentation, the following

discrepancies

were also noted and corrective

actions will be assigned to" address them as well. 1. The WO plan called for motor removal,

for refurbishment, and. reinstallation

of same motor. The spare motor from stock was used to problems

refurbishment

of the

motor and the WO plan was not. revised to reflect the subtle differences

between the spare motor and the one that had been removed from the pump. 2. The Work Instruction (WI) WI-SPS-E-02

data sheet was not

filled out, in that the motor serial number was not listed as required.

3. Procedures

ESS-E-36 and MSE-E-5

the procedure

and all* attachments

to be filed in DCC

filmed). The WO package was purged of these

prior to closeout and therefore

this requirement

was not met. 4.' Several entries on the WO summary as well as a *signature

in FHS-M:.23

did not contain dates. -I 5. The WO package did not contain the issue ticket for the Raychem cable splices used during the reconnection

of the motor.* 6. The equipment

database has not been revised to reflect the serial number of spare motor that was installed . . ]. The radiation

hot work permit does not provide a box to be checked that

the use of a torch for heating. * 8. Torquing of the motor hold down bolts was signed as performed

on July 10, 1993 and verified on July 11*, 1993. This activity was in fact performed

on July 11, 1993. 9. * Step 9 of the WO plan contained

a double verification

that the WO summary shows was performed

on July 8, 1993 but was signed July 19, 1993.

10 Corrective

Actions 1. The evaluation

of this investigation (D-PAL-94-017)

and its associated

WO will be reviewed with members of the maintenance

department

specifically

addressing

items 1, 2, 4, 5, 8, and 9 listed above. 2. The practice and control used to revise the database

when a spare motor is installed

will be evaluated

to determine

if current practice is acceptable

or if the method should be modified to ensure timely database update. 3. An assessment

will be completed

to

the need to revise. the hot wbrk permit form to include a box to be checked to address heating with a torch. 4. All'permanent

maintenance

procedures

will be reviewed to determine

which .ones

the filming of all attachments.

Those permanent

maintenance

procedures

whose filming requirements

need to be clarified, will be revised following review. NRC Identified

Weakness The team found that the licensee had not fully evaluated

the susceptibility

of SWS instrument

line fouling. Specific flushing requirements

had only been implemented

for instruments

that had been clogged in the past; however, walkdowns

of SWS pump discharge

lines found that instrument

lines to pressure switches for standby pump starting had long stagnant.horizontal

runs that might be subject to fouling. These lines were.not checked by periodic maintenance

or surveillance.

Also omitted were stagnant 11nes to and from the former control room air conditioners.

This was not consistent

with the GL intent, which reconunended

licensees

establish

routine maintenance

of. SWS piping and components

to ensure that silting and bio-fouling

could not degrade system performance.'

The licensee conunitted

to review the.maintenance

of these and other instrument

lines. CPCo Response It is apparent that the original Generic Letter 89-13 effort did not address all instrument

lines. During the Palisades

SWOPI inspection

the NRC Information

Notice 94-003 was issued. The Information

Notice entitled, "Deficiencies

Identified

During *service Water System Operational

notifies licensees

of concerns regarding

instrument

tubing becoming fouled with silt and. acknowledges

that this issue should have been better addressed

by the Generic Letter 89-13 implementation.

We will review the specific issues in the Information

Notice to see how those issues apply to Palisades,

.. ** 11 and incorporate

actions as need&d in our preventative

maintenance

program to ensure that tubing doesn't become fouled. The review of the Information

Notice and any corrective

needed will be completed

by the end of the 1995 refueling

outage. An AIR, A-PAL-94-009, initiated

to assure that the -issue of the stagnant lines to and from the former control room air conditioners

is addressed

under the Generic Letter and Information

Notice 94:004 guidelines.