ENS 53745
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ENS Event | |
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05:00 Nov 19, 2018 | |
Title | Emergency Diesel Generator Actuation Due to Low Voltage Signal |
Event Description | On 11/19/2018, at 1916 EST, with unit 2 in Mode 5 at 0 percent power, an actuation of the 'B' [Emergency Diesel Generator] EDG occurred during troubleshooting activities with the opposite train protected. The reason for the 'B' EDG auto-start was low voltage on the E-2 bus due to its supply breaker opening. The 'B' EDG automatically started as designed when the low voltage signal was received. Following the EDG start, required loads sequenced on as designed including the 'B' [Motor Driven Auxiliary Feedwater Pump] MDAFW Pump.
This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the Emergency AC Electrical Power System (Emergency Diesel Generator) and Auxiliary Feedwater System (Motor Driven Auxiliary Feedwater Pump). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified." |
Where | |
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Robinson South Carolina (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+18.07 h0.753 days <br />0.108 weeks <br />0.0248 months <br />) | |
Opened: | Nick Roh 23:04 Nov 19, 2018 |
NRC Officer: | Ossy Font |
Last Updated: | Nov 19, 2018 |
53745 - NRC Website
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Unit 2 | |
---|---|
Reactor critical | Not Critical |
Scram | No |
Before | Cold Shutdown (0 %) |
After | Cold Shutdown (0 %) |
WEEKMONTHYEARENS 565852023-06-22T14:35:00022 June 2023 14:35:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Occured During Protection System Testing ENS 542122019-08-11T12:40:00011 August 2019 12:40:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Turbine Trip ENS 537452018-11-19T05:00:00019 November 2018 05:00:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generator Actuation Due to Low Voltage Signal ENS 526622017-04-04T01:55:0004 April 2017 01:55:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Actuation of Auxiliary Feedwater System During Surveillance Testing ENS 522902016-10-08T17:17:0008 October 2016 17:17:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to Loss of Offsite Power ENS 521982016-08-24T17:38:00024 August 2016 17:38:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due Automatic Turbine Trip from 100 Percent Power ENS 497082014-01-10T03:34:00010 January 2014 03:34:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Turbine Trip ENS 495062013-11-05T23:00:0005 November 2013 23:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Momentary Loss of 4 Kv Buses and Safety System Actuation ENS 495022013-11-05T05:41:0005 November 2013 05:41:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Actuation of the Auxiliary Feedwater System Due to Main Feed Pump Trip ENS 477812012-03-28T19:03:00028 March 2012 19:03:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Steam Generator High Water Level Condition ENS 472932011-09-26T15:45:00026 September 2011 15:45:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to One Loop Low Flow Signal ENS 463132010-10-07T04:13:0007 October 2010 04:13:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to a One Loop Reactor Coolant Low Flow ENS 462382010-09-09T18:37:0009 September 2010 18:37:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Overtemperature Delta-T Signal ENS 457992010-03-28T22:52:00028 March 2010 22:52:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Alert Declared Due to Fire Affecting Safety Related Equipment ENS 454832009-11-07T03:02:0007 November 2009 03:02:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Feed Reg Valve Closure ENS 446602008-11-17T10:51:00017 November 2008 10:51:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to High Turbine Vibration ENS 433642007-05-15T15:16:00015 May 2007 15:16:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip on Turbine Trip Due to Differential Generator Protection ENS 429332006-10-25T06:48:00025 October 2006 06:48:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip After a 100% Load Rejection 2023-06-22T14:35:00 | |
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