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 Discovered dateReporting criterionTitleDescriptionLER
ENS 4875414 February 2013 23:10:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification Due to Release of Amertap Balls Into the Mississippi River

On 2/14/2013, Xcel Energy personnel determined that approximately 44% of the Amertap balls recently used were not recovered. Monticello Nuclear Generating Plant is required to report to the Minnesota Pollution Control Agency (MPCA) when greater than 20% of the Amertap balls are not recovered. This is based on an agreement with the MPCA dated September 12, 2008. The MPCA was notified at 1710 CST on 2/14/2013. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE FROM MICHAEL STIDMON TO HOWIE CROUCH AT 1352 EST ON 2/15/13 * * *

Update for 50.72 non-emergency notification number 48754: The referenced report number was made at 1831 EST on 2/14/2013. This report stated the Minnesota Pollution Control Agency (MPCA) was notified that 44% of Amertap balls recently used were not recovered at 1710 CST on 2/14/2013. Due to a miscommunication between the Monticello Nuclear Generating Plant Chemistry Department and the Xcel Energy Corporate Environmental Services contractor, the actual MPCA notification was not made until 0930 CST on 2/15/2013. This update report is to ensure the correct time of the MPCA notification was documented. The licensee notified the NRC Resident Inspector. Notified R3DO (Pelke).

ENS 488054 March 2013 15:27:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification Due to a Fish KillAt 0927 CST on March 4, 2012, XCEL Energy Environmental Services made a report to the State of Minnesota regarding 475 fish killed from the discharge canal temperature transient following reactor shutdown on March 2, 2013. Monticello was in the process of performing a planned shutdown in preparation for a refueling outage. The NRC Resident Inspector, Wright County Sheriffs Department and Sherburne County Sheriffs Department have been notified by the licensee.
ENS 488096 March 2013 10:01:0010 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual HeatMomentary Loss of Shutdown Cooling

At 0401 CST on 3/6/2013, while in RHR-High (Residual Heat Removal-High) water level the plant experienced a momentary Loss of Shutdown Cooling which resulted in a loss of safety function for Residual Heat Capability. Division 2 RHR shutdown cooling was restored within approximately 90 seconds without issue. No changes were experienced in refuel volume temperature or level during the loss of RHR shutdown cooling. This occurred shortly after a flow adjustment on the system was made utilizing the outboard valve. The inboard valve was reopened and an investigation is in progress. At the time of the valve closure, decay heat removal continued from Reactor Water Cleanup in heat reject mode and fuel pool cooling (with the fuel pool gates removed) is in service. Division 1 RHR (Shutdown Cooling) was available (not Operable) at the time of the loss. It is not currently understood why the injection valve closed. All systems functioned as required except for the spurious closing of MO-2015 (the Div 2 RHR inboard injection valve). The following make-up sources are available: Divisions 1 and 2 RHR, Divisions 1 and 2 Core Spray, CRD (Control Rod Drive), CST (Condensate Storage Tank) via a Core Spray with pressurizing station bypassed. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION AT 1419 EDT ON 4/11/2013 FROM RYAN RICHARDS TO MARK ABRAMOVITZ * * *

On March 6, 2013 (Notification No. 48809) NSPM (Northern States Power Monticello) reported in accordance with 10 CFR 50.72 (b)(3)(v)(B), a momentary closure of valve MO-2015 in the operating Residual Heat Removal (RHR) subsystem as an event or condition that at the time of discovery could have prevented the fulfillment of a safety function. Following the event, the RHR SDC (shut down cooling) subsystem was removed from operation for equipment forensics and troubleshooting. Results validated that valve MO-2015 was operable and no issues were identified with the associated electrical circuitry, or the RHR SDC subsystem. The decay heat removal requirements of LCO 3.9.7, RHR - High Water Level, were met and there was not a loss of safety function. Therefore, NSPM retracts the March 6, 2013 notification for this event. The licensee notified the NRC Resident Inspector, state and local authorities, and may make a press release. Notified the R3DO (Passehl).

ENS 4891913 April 2013 03:00:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionUnanalyzed Condition Due to Isolated Differential Pressure Switch on Safety Relief Valve TailpipeOn April 12th, 2013 at 2200 CDT, investigation into the inability to complete a Safety/Relief Valve (S/RV) discharge line excess flow check valve test determined that a relief valve discharge monitoring instrument valve had been inappropriately closed since late June, 2011. The closed valve isolated two differential pressure switches that impact the operation of 'E' Low-Low Set (LLS) valve. The LLS logic and instrumentation were affected by the loss of two 'E' S/RV tailpipe discharge pressure switches which indicate S/RV open status and start two inhibit timers which prevent plant operators or the LLS S/RV logic from immediately re-opening the valve to allow the water leg in the S/RV discharge line to recede. The LLS logic and instrumentation is designed to mitigate the effects of postulated thrust loads on the S/RV discharge lines by preventing subsequent actuations with an elevated water leg in the S/RV discharge line. It also mitigates the effects of postulated pressure loads on the torus shell or suppression pool by preventing multiple actuations in rapid succession of the S/RVs subsequent to their initial actuation. The valve found closed has been returned to its normal open position. This condition resulted in the 'E' S/RV LLS function being aligned contrary to its design configuration and as such is being reported as an unanalyzed condition as defined by 10 CFR 50.72(b)(3)(ii)(B). The licensee has notified the NRC Resident Inspector.
ENS 490108 May 2013 11:23:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseEmergency Siren Spurious ActuationOn 5/8/2013 at 0623 (CDT) MNGP was informed by Wright County Sheriffs Department of a spurious actuation of one emergency response siren in Wright County (for about 2 seconds). This activation was confirmed by vendor system monitoring. The source of the activation has not been determined. At this time all aspects of the public notification system are functional. The licensee notified the NRC Resident Inspector and will notify the state and local governments.
ENS 4902310 May 2013 14:20:0010 CFR 26.719, FFD Reporting requirementsFitness-For-Duty Report Involving Discovery of Alcohol Container Inside the Protected Area(The licensee) discovered a small bottle of alcohol within the Protected Area. The 50ml bottle was approximately 2/3 full. The seal ring had been broken. The clear liquid smells of alcohol as the label of the bottle indicates. The bottle was discovered beneath a deck structure to a temporary trailer that workers were demolishing. This event is reportable under 10CFR26.719 Fitness-For-Duty. The license informed the NRC Resident Inspector.
ENS 4904817 May 2013 20:27:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessPlant Process Computer Removed from Service for Maintenance and UpgradesThis is a non-emergency 8-hour notification for a planned loss of emergency assessment capability. This event is reportable in accordance with 10CFR50.72(b)(3)(xiii) because the work activities affects the functionality of the Plant Process Computer System. Monticello Nuclear Generating Plant will remove the Plant Process Computer System (PPCS) from service on 5/17/13 at 1527 (CDT) to perform system upgrades and planned maintenance. The PPCS system is planned to be non-functional for less than 4 hours. While the system is out of service, the Emergency Plan can still be implemented as assessment capabilities are available under alternate means and communication of the assessment results using communication equipment. ERDS will be out of service during this period. Compensatory measures for the loss will be implemented. The NRC Resident Inspector has been notified.
ENS 4906624 May 2013 08:34:0010 CFR 50.72(b)(3)(iv)(A), System ActuationAutomatic Start of Emergency Diesel Generator Due to Bus UndervoltageAt 0334 (CDT) on 5/24/2013 MNGP (Monticello Nuclear Generating Plant) experienced a loss of power to Bus 15 (Division 1 4kV Essential Bus) during performance of preoperational testing on the 2R reserve transformer which initiated an Essential Bus Transfer of Bus 15 and automatic start of 12 Emergency Diesel Generator. MNGP was in Mode 5 operations with water level >21 feet 11 inches above the top of the RPV flange and all credited safety systems were lined up to Bus 16 (Division 2 4kV Essential Bus) which was unaffected by this event. Bus 15 was automatically repowered from the 1AR reserve transformer as designed. During this evolution all critical safety functions remained green and all systems responded as expected to the Essential Bus transfer. The cause of the sequence of events that led to the Bus 15 loss of power is being investigated. This event is reportable under 10CFR50.72(b)(3)(iv) as an event that results in a valid actuation of 12 Emergency Diesel Generator. The NRC Resident Inspector has been notified.
ENS 4908531 May 2013 19:00:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionUnanalyzed Condition Concerning Flooding MitigationOn May 31, 2013, during an aggregate review of issues raised during a focused self assessment of external flooding mitigation, it was concluded that the A.6 Acts of Nature procedure may not adequately protect equipment required to maintain safe shutdown from the external probable maximum flood. The plant is currently in Mode 4, Cold Shutdown for refueling. MNGP (Monticello Nuclear Generating Plant) is addressing the inadequacies. This condition is being reported in accordance with 10 CFR 50.72(b)(3)(ii)(B) Unanalyzed Condition. Compensatory measures are being prepared including procedure changes, additional barriers, and contingency actions. The licensee notified the NRC Resident Inspector.
ENS 4911313 June 2013 19:30:0010 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Emergency Diesel Generators StartWhile preparing for an equipment test Thursday afternoon, Monticello Nuclear Generating Plant lost off-site power on its normal off-site power feed. Power for safety related loads was automatically transferred to the alternate off-site power source. The Emergency Diesel Generators started as designed but did not load onto the safety related busses due to the availability of off-site power. Operators stabilized the plant, which is shutdown for a refueling and maintenance outage, in less than an hour and are investigating the cause of the event. The current plant focus is on restoring the normal off-site power feed. The event posed no danger to the public or plant workers, and no one was injured. There was no release of radiation. Plant safety systems continue to be powered by the backup off-site power feed, with the emergency diesel generators available if needed. Event Specifics: At approximately 1430 CDT, during a refueling outage with the plant in Mode 4, reactor level at approximately 200 inches, and a full Scram already inserted, a loss of normal off-site power occurred due to a fault in a non-safety related bus supply breaker. The fault was in the 13.8 KV supply breaker to the #11 bus. This caused the Station 2R transformer to lockout, resulting in a loss of the normal off-site power to Essential Busses 15 and 16. Shutdown Cooling (SDC) was lost for approximately 1 hour due to loss of supply power and isolation of the common suction valves. Both 11 and 12 Emergency Diesel Generators (EDGs) automatically started but did not load onto their respective busses (as designed) due to the 1AR emergency off-site transformer re-energizing both 15 and 16 bus. This essential bus transfer is being reported as a 'Valid actuation of emergency AC electrical power systems' under 10CFR50.72(b)(3)(iv). During the event the decision was made to shut down the EDGs which rendered them inoperable for a short period of time until the Fast Start capability was reset. The period of time that the EDGs were inoperable is being reported as a 'Condition that could have prevented the fulfillment of the safety functions to remove residual heat, control the release of radioactive material, and mitigate the consequences of an accident under 10CFR50.72(b)(3)(v)(B), (C), and (D). Both EDGs have been restored to Automatic Standby Status and are operable. The loss of power resulted in a Group II Containment Isolation signal causing secondary containment to isolate and Standby Gas Treatment and Control Room Emergency Filtration to initiate as well as associated Group II Containment Isolation Valves to close. This is being reported as a 'General containment isolation signal ESF actuation' under 10CFR50.72(b)(3)(iv). The containment isolation has been reset, and SDC and SFPC have been restored. Reactor temperature rose approximately 4 degrees F during the event from 161 degrees to 165 degrees which remained in the prescribed operating band. Reactor level did not change. The licensee has notified the NRC Resident Inspector.
ENS 491818 July 2013 22:00:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification Due to Sodium Hypochlorite SpillOn July 8th, 2013, at approximately 1730 CDT, the Minnesota State Duty Officer was notified of an approximately 50 gallon sodium hypochlorite spill onsite. The spill has been contained and clean-up is in progress. There was no actual or potential impact on the environment and no impact on the health and safety of the public or onsite personnel. The licensee will also be notifying Wright County. The NRC Resident Inspector has been informed.
ENS 4929322 August 2013 01:00:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionUnanalyzed Condition for Emergency Diesel Generator Fuel Oil Pumps Train SeparationOn August 21, 2013 at 2000 CDT, it was determined following receipt and review of an NRC position document, that the design of the Monticello Nuclear Generating Plant diesel fuel oil supply system is not consistent with current and historical licensing and design basis documents. This condition affects fuel oil supply from the diesel fuel oil storage tank to both emergency diesel generators and is being reported pursuant to 10CFR50.72(b)(3)(ii) as an unanalyzed condition that could significantly degrade plant safety. Actions are in progress to address the unanalyzed condition. The NRC Resident Inspector has been notified.
ENS 4931228 August 2013 02:52:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionRecirc Pump Runback and Power Reduction

On August 27, 2013 at 2152 CDT, Monticello Nuclear Generating Plant (MNGP) experienced a runback of (the) 'B' Recirc pump from 87% speed to 71% speed. Operators took action to lock (the) 'B Recirc pump scoop tube. This runback resulted in a power reduction from 100% to 94% RTP (Rated Thermal Power). With the resultant mismatch between total jet pump flows of the two loops greater than required limits, should a LOCA (Loss of Coolant Accident) occur, the core flow coastdown and resultant core response may not be bounded by the LOCA analyses. It has been determined that this is an unanalyzed condition as defined by 10CFR50.72(b)(3)(ii)(8). At 0121 CST on August 28, 2013, MNGP completed reducing power to 88% using 'A' Recirc pump to match total jet pump flows and (the plant) is no longer in an unanalyzed condition. The 'B' Recirc scoop tube remains locked pending investigation. The licensee has notified the NRC Resident Inspector.

  • * * RETRACTION ON 10/11/13 AT 1253 EDT FROM MARK HOESCHEN TO DONG PARK * * *

This is a retraction for ENS 49312: The licensee reviewed the MNGP design basis analysis to determine if the event was bounded. The licensee determined that the Loss of Coolant Accident (LOCA) provides a bounding analysis for this event. The limiting LOCA event for the MNGP as analyzed in accordance with 10CFR50 Appendix K conditions is based upon single failure of the Low Pressure Coolant Injection (LPCI) injection valve, effectively making LPCI inoperable for the event. The large break Design Basis Accident (DBA) with LPCI injection valve failure (which is analytically equivalent to the condition of both LPCI subsystems being inoperable) is the event analyzed for the current Licensing Basis Peak Cladding Temperature (PCT). This analysis bounds the event as a recirculation pump flow mismatch event is less limiting than the LOCA with LPCI injection valve failure analysis. Therefore, this recirculating loop flow mismatched event is less limiting than a previously analyzed event and ENS 49312 may be retracted as an unanalyzed event. The licensee has notified the NRC Resident Inspector. Notified R3DO (Skokowski).

ENS 4931429 August 2013 16:00:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionFailure to Address All the Effects of External Flooding ScenariosOn August 28, 2013, Monticello Nuclear Generating Plant (MNGP) was notified of the NRC's final significance determination for a finding involving the failure to maintain a procedure addressing all of the effects of an external flooding scenario on the plant. Specifically, MNGP failed to maintain flood Procedure A.6, 'Acts of Nature,' such that it could support the timely implementation of flood protection activities within the 12 day timeframe credited in the design basis as stated in the updated safety analysis report. The finding is not a current safety concern. On February 15, 2013, actions were completed to reduce the flood mitigation plan timeline to less than 12 days by developing an alternate plan for flood protection features, pre-staging equipment and materials, improving the quality of the A.6 procedure, and preplanning work orders necessary to carry out Procedure A.6 actions. The NRC Resident Inspector has been notified.
ENS 493161 September 2013 21:10:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionRecirc Pump Runback and Power Reduction

On September 1, 2013 at 1610 CST, Monticello Nuclear Generating Plant (MNGP) experienced a runback of 'A' Recirc pump from 87% speed to 82% speed. Operators took action to lock 'A' Recirc pump scoop tube. This runback resulted in a power reduction from 100% to 98% RTP (Rated Thermal Power). Should a LOCA (Loss of Coolant Accident) occur with the resultant mismatch between total jet pump flows of the two loops greater than required limits, the core flow coastdown and resultant core response may not be bounded by the LOCA analyses. It has been determined that this is an unanalyzed condition as defined by 10CFR50.72(b)(3)(ii)(B). At 2123 CST on September 1, 2013, MNGP completed adjusting recirc flow speed on 'A' and 'B' Recirc pumps to match jet pump loop flows to within the required limits and is no longer in an unanalyzed condition. Both 'A' and 'B' Recirc scoop tubes remain locked pending investigation. The licensee has notified the NRC Resident Inspector.

  • * * RETRACTION ON 10/11/13 AT 1253 EDT FROM MARK HOESCHEN TO DONG PARK * * *

This is a retraction for ENS 49316: The licensee reviewed the MNGP design basis analysis to determine if the event was bounded. The licensee determined that the Loss of Coolant Accident (LOCA) provides a bounding analysis for this event. The limiting LOCA event for the MNGP as analyzed in accordance with 10CFR50 Appendix K conditions is based upon single failure of the Low Pressure Coolant Injection (LPCI) injection valve, effectively making LPCI inoperable for the event. The large break Design Basis Accident (DBA) with LPCI injection valve failure (which is analytically equivalent to the condition of both LPCI subsystems being inoperable) is the event analyzed for the current Licensing Basis Peak Cladding Temperature (PCT). This analysis bounds the event as a recirculation pump flow mismatch event is less limiting than the LOCA with LPCI injection valve failure analysis. Therefore, this recirculating loop flow mismatched event is less limiting than a previously analyzed event and ENS 49316 may be retracted as an unanalyzed event. The licensee has notified the NRC Resident Inspector. Notified R3DO (Skokowski).

ENS 493359 September 2013 19:00:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionHigh Energy Line Break Barrier Improperly Obstructed

At 1400 (CDT) on September 9, 2013, plant personnel found HELB barrier HATCH-1/TB blocked. The hatch is diamond plate steel located on the turbine floor. Pallets, a fan and a gantry were positioned on top of the hatch possibly preventing pressure relief during a HELB event. This issue is being reported as an unanalyzed condition per 10CFR50.72(b)(3)(ii)(B). All items were removed from the hatch by 1800 on September 9, 2013. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION FROM JEREMY TANNER TO JOHN SHOEMAKER AT 1118 EDT ON 10/04/13 * * *

The licensee reviewed the design basis calculations and analyses for HELB events in the area where Hatch-1/TB is located. The review determined that it is acceptable to block or hold Hatch-1/TB down and that the painted markings on the hatch are overly restrictive. In looking at HELB calculation of record, feed water break at the feed water pumps, there is no flow path modeled between the HELB volumes. Therefore, if Hatch-1/TB is blocked, the physical flow path is in accordance with the Gothic model of the HELB volume. Further, the analyses also indicated that no credit is taken for the hatch to relieve as no HELBs are postulated in the room under the hatch. Finally, Hatch 1/TB structural integrity was verified assuming a HELB occurred with the hatch blocked as described in notification 49335 (pallets, fan and gantry) the barrier would function as designed. Licensee initiated a Work Request to remove any markings on Hatch-l/TB that indicate do not block or hold down. The licensee will notify the NRC Resident Inspector. The Region 3 Duty Officer (Valos) was notified.

ENS 4935619 September 2013 03:29:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Both Secondary Containment Access Doors Briefly Opened Simultaneously

While performing the secondary containment airlock door interlock surveillance, the interlock to the main plenum room did not prevent the opening of both doors to the plenum room airlock (DOOR-85 and DOOR-86). The plenum room airlock doors were immediately closed. The time both doors were opened is estimated to be approximately one (1) second. When both doors open, Technical Specification surveillance requirement SR 3.6.4.1.3 was not met and secondary containment was declared inoperable. Secondary containment was declared operable after independently verifying at least one secondary containment access door was closed. There were no radiological releases associated with this event. The NRC Resident Inspector has been notified.

  • * * UPDATE FROM KIM HOFFMAN TO HOWIE CROUCH AT 1753 EDT ON 9/20/13 * * *

This update provides additional information on the initial notification of the event. On 9/18/13, while testing secondary containment airlock doors, the interlocks did not prevent opening of both doors simultaneously. With the outer door to the main plenum room open, the inner door was able to be opened. At this point, Technical Specification SR 3.6.4.1.3 was not met and secondary containment was inoperable. The inner door was closed immediately. While in this condition, the inner door was then opened, and the interlock did not prevent the opening of the outer door. The outer door was closed immediately. Secondary containment was declared operable after verifying at least one of the airlock doors was closed. There were no radiological releases associated with this event. The NRC Resident Inspector has been notified. Notified R3DO (Reimer).

ENS 4936319 September 2013 22:50:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection Inoperable Due to Steam Leak

On 9/19/2013, during the performance of the High Pressure Coolant Injection (HPCI) quarterly pump and valve surveillance, a steam leak was discovered. HPCI had previously been declared inoperable due to planned maintenance. As a result of the steam leak, HPCI remains inoperable. Action taken: 14 days Required Action TS 3.5.1.J.2 remains in effect and corrective actions are in progress. The licensee has notified the NRC Resident Inspector.

* * * RETRACTION FROM RANDY SAND TO PETE SNYDER AT 1546 EDT ON 10/28/13 * * *

The licensee performed an evaluation that determined the minor steam leak from the High Pressure Coolant Injection (HPCI) turbine reported on 9/20/2013 was not significant enough to prevent HPCI from mitigating the consequences of an accident or mitigating a Station Blackout (SBO) event. The licensee performed an engineering evaluation of the HPCI system, the HPCI pump/turbine and the HPCI room environmental conditions assuming conservative leakage conditions existed. The results of this evaluation confirmed that the HPCI system would have been able to perform its design function assuming conservative leakage conditions existed throughout limiting events. The HPCI pump/turbine would not have failed during any accident or SBO event, and sufficient motive (steam) force was available for the HPCI system to perform its design functions. There would have been no unacceptable impact on the HPCI pump/turbine oil system due to the steam leak. The HPCI room environment would not have exceeded allowable limits. For events where AC power is available, the analysis took advantage of the HPCI room cooler that is powered from an essential power source and supplied from a safety related service water system. This cooler was available during the period of the steam leak. The evaluation of room conditions for SBO conditions did not include use of the HPCI room cooler and also showed room conditions would have remained within acceptable values. There would not have been a buildup of fluid sufficient to cause a flood in the HPCI room. Therefore, based on the results of the formal engineering evaluation, the HPCI system was capable of performing its safety function and therefore, this event may be retracted. The licensee will notify the NRC Resident Inspector. Notified R3DO (Daley).

ENS 4938827 September 2013 13:20:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessTechnical Support Center Planned Maintenance

On 9/27/13, Monticello Nuclear Generating Plant's Technical Support Center power supply will be isolated to perform a planned maintenance activity. The maintenance activity may require implementation of compensatory measures to maintain TSC functionality during the activity. The compensatory measures include having the Emergency Director report to the Control Room and co-locating the remaining TSC staff at the EOF should an event be declared requiring ERO activation. The ERO has previously successfully demonstrated the ability to implement these compensatory measures. The maintenance activity is scheduled to be completed with the TSC returned to full functionality by the end of the dayshift on 9/27/13. The Site Emergency Response Organization has been notified of the maintenance activity. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE ON 9/27/13 AT 1916 EDT FROM MARK IHLENFELDT TO DONG PARK * * *

On 9/27/13, Monticello Nuclear Generating Plant's Technical Support Center power supply was isolated to perform a planned maintenance activity. The maintenance activity required implementation of compensatory measures to maintain TSC functional during the activity. Maintenance activity is completed and TSC is fully functional and returned to service. Site Emergency Response Organization has been notified. The licensee has notified the NRC Resident Inspector. Notified R3DO (Dickson).

ENS 4939027 September 2013 18:30:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessLoss of Emergency Assessment Capability Due to Radiation Monitors Out of ServiceOn 9/27/13, Monticello Nuclear Generating Plant personnel identified that when the Service Water Radiation Monitor or the Discharge Canal Radiation Monitors are removed from service for planned maintenance activities, a loss of emergency assessment capability may occur. The adequacy of compensatory measures for when these radiation monitors are removed from service is under evaluation. The Service Water Radiation Monitor is taken out of service weekly for flushing. This last occurred at 0221 (CDT) on 9/26/13. The Discharge Canal Radiation Monitors are taken out of service approximately once a year for cleaning. The last time these monitors were removed from service was at 1250 (CDT) on 9/18/13. In accordance with 10CFR50.72(b)(3)(3)(xiii) these past occurrences are being reported as a loss of emergency assessment capability. The NRC Resident Inspector has been notified.
ENS 4958026 November 2013 10:00:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessDischarge Canal Radiation Monitor Removed from ServicePlanned preventative maintenance on the discharge canal piping will remove the discharge canal radiation monitor from service. This represents a loss of emergency assessment capability under NUREG-1022, revision 3, specific to RU1.1, RU1.2, RA1.1, and RA1.2. The planned maintenance is expected to last 13 hours. The NRC Senior Resident Inspector was notified (by the licensee) prior to removing the discharge canal radiation monitor from service.
ENS 4958627 November 2013 13:40:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessService Water Radiation Monitor Removed from ServicePlanned preventative maintenance on service water piping will remove the service water radiation monitor from service. This represents a loss of emergency assessment capability under NUREG-1022, revision 3, specific to RU1.1, RU1.2, RA1.1, and RA1.2. The planned maintenance is expected to last eight hours. The NRC Resident Inspector was notified prior to removing the service water radiation monitor from service.
ENS 4971411 January 2014 07:00:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification Due to Decreasing Discharge TemperatureAt 0205 CST (on 1/11/14), Xcel Energy Environmental Services made a report to the State of Minnesota due to cooling water return to the Mississippi River via the plants discharge canal dropping by more than 5 degrees F in an hour. The cause of the temperature drop was due to an emergent reduction in reactor power and generator load in response to a degrading condenser vacuum. This notification is being made under 10 CFR 50.72(b)(2)(xi) based on a notification to another Government Agency. The NRC Resident Inspector has been notified.
ENS 4973917 January 2014 23:36:0010 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
Technical Specification Required Shutdown Due to Reactor Pressure Boundary LeakageLeakage into the Reactor Building Closed Cooling Water (RBCCW) system has been determined to be Reactor Pressure Boundary leakage as identified by the plant's Technical Specification (LCO 3.4.4). Based on this, the LCO is not met and a plant shutdown is required. The shutdown commenced at 2029 CST. All of the leakage has been retained within the RBCCW system. There has been no radioactive release from the Monticello plant and all other systems remain operable and available. The unit continues to be operated in a safe and predictable fashion as it is being removed from service. The NRC Resident Inspector has been notified. The leakage rate was 0.12 gallons per minute at power.
ENS 4974118 January 2014 09:38:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification Due to Discharge Canal Temperature Drop

At 0338 CST, Xcel Energy Environmental Services made a report to the State of Minnesota due to cooling water return to the Mississippi River via the plant's discharge canal dropping by more than 5 deg F per hour. The cause of the temperature drop was due to a required time limited reactor shut down. The reactor is currently shut down with all systems responding as expected. This notification is being made under 10 CFR 50.72(b)(2)(xi) based on a notification to another government agency. The NRC Resident Inspector has been notified

  • * * UPDATE FROM JON LAUDENBACH TO VINCE KLCO ON 1/20/14 AT 1259 EST * * *

At 1130 EST on 1/20/2014, XCEL Energy Environmental Services made a report to the State of Minnesota (Minnesota Pollution Control Agency and the Minnesota Department of Natural Resources) due to the recorded total fish loss (207) as a result of the Monticello Plant's discharge canal temperature change per above. This is an update notification only and has no safety significance and no impact on the health and safety of the general public. The licensee notified the NRC Resident Inspector. Notified the R3DO (Skokowski).

ENS 498087 February 2014 16:05:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
Single Drywell to Torus Vacuum Breaker Not Going Fully Closed During Surveillance TestAfter cycling AO-2382A (Drywell to Torus Vacuum Breaker) for surveillance testing, it did not indicate fully closed. The procedure for this condition was entered and after cycling the valve several times, the vacuum breaker indicated full closed. During the approximately eight minutes that the indication showed that it was not closed, the Technical Specification Limiting Condition for Operation (LCO) requirement was not met. After validation that the vacuum breaker had opened as required, and was closed successfully, the safety function was restored. The health and safety of the public was not jeopardized as the plant was in a normal condition and an initiating event was not in progress. The USAR (Updated Safety Analysis Report) assumes all eight vacuum breakers to be closed. This condition therefore put the nuclear power plant in an unanalyzed condition and is reportable per 10CFR50.72(b)(3)(ii)(B). This condition, at time of discovery, could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident and is reportable per 10CFR50.72(b)(3)(v)(D). The licensee notified the NRC Resident Inspector, the State of Minnesota Duty Officer, and the local counties.05000263/LER-2014-002
ENS 4981410 February 2014 22:50:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Single Failure Vulnerability Affecting Emergency Diesel Generator OperabilityThe licensee also reported an additional 8 hour Non-emergency report in accordance with 10CFR50.72(b)(3)(v)(D) On February 10, 2014, (at 1650 CST) Monticello station personnel identified a vulnerability where a single failure could result in the Emergency Diesel Generators (EDGs) picking up load on the essential busses in a time frame longer than what is required by Monticello Technical Specification Surveillance Requirement (TS SR) 3.8.1.12. This surveillance requires that on a simulated or actual loss of off-site power signal in conjunction with an actual or simulated ECCS initiation signal, the Emergency Diesel Generators auto-start from standby condition and energize permanently connected loads in approximately 10 seconds. The single failure vulnerability could result in the EDGs energizing the connected loads in a slightly longer time period based upon actual test data (< 11 seconds). As a result, Technical Specification SR 3.8.1.12 was declared not met and both EDGs were declared inoperable. Monticello has subsequently isolated the single failure vulnerability and declared the EDGs operable. The station remained in a safe condition during the discovery of this vulnerability. Both EDGs remain available and functional (and operable), off-site power remains available, and the plant continues to operate in a normal condition with no initiating events present. The single failure vulnerability was associated with the 1AR 13.8KV transformer logic. The 1AR transformer is one of three off-site power sources. 1R and 2R meet the TS requirements for Off-site power. The licensee notified the NRC Resident Inspector and the State of Minnesota Duty Officer.05000263/LER-2014-004
ENS 4981911 February 2014 20:30:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
Drywell to Torus Vacuum Breaker Failure During Surveillance TestingWhile cycling AO-2382A (TORUS-DW VAC BREAKER) for required surveillance testing, (the vacuum breaker) did not indicate fully closed on all available indicators. The procedure for this condition was utilized to continue to cycle the vacuum breaker to achieve closed indication on all available indicators. The vacuum breaker was cycled a total of four (4) times and dual indications were present for approximately six (6) minutes. During the six (6) minutes that the vacuum breaker indications did not show fully closed, the Technical Specification Limiting Condition for Operation (TS LCO) requirement was not met. The Monticello Safety Analysis assumes all eight (B) vacuum breakers are closed, therefore this condition is being reported per 10CFR50.72(b)(3)(ii)(B) and per 10CFR50.72(b)(3)(v)(D). The vacuum breakers are all capable of performing their design function and all safety related equipment is operable." The NRC Resident Inspector has been notified. The same vacuum breaker failed its surveillance test in a similar fashion on February 7, 2014 (See EN #49808). The surveillance test for this vacuum breaker is due again on February 18, 2014.05000263/LER-2014-003
ENS 4982012 February 2014 14:15:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessService Water Radiation Monitor Removed from Service for Planned MaintenancePlanned preventive maintenance on service water piping will remove the service water radiation monitor from service. As a result, this represents a loss of emergency assessment capability under NUREG 1022, Revision 3, since the radiation monitor is used to assess NUE (Notification of Unusual Event) and Alert thresholds. The planned maintenance is expected to last 8 hours. During this time, the site Chemistry Department will perform sampling at this location every 30 minutes. The sampling is documented in a station procedure and allows the ability to detect NUE levels in a timely manner. As a result of sampling, reasonable assurance exists to monitor and detect rising radiation levels in order to protect the health and safety of the public. The NRC Resident Inspector will be notified prior to removing the service water radiation monitor from service.
ENS 4984621 February 2014 07:30:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessFailed Power Supply Affecting Radiation MonitorsAt 0130 CST, a degraded power supply resulted in multiple Area Radiation Monitors (ARMs) reading erroneously low. As a result, this condition is reportable under 10 CFR 50.72(b)(3)(xiii) as these ARMs are used to assess NUE and Alert thresholds. Portable Radiation Monitors have been placed in identified affected areas as a compensatory measure. The health and safety of the public was maintained as the plant was in a normal condition with no initiating event in progress or signs of elevated radiation on any other unaffected radiation monitors. The NRC Resident Inspector has been notified.
ENS 498765 March 2014 21:00:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 72.75(b)(2), Offsite Notification
Offsite Notification Due to Dry Shielded Canister Test ResultsThis report is being made to provide information to the NRC regarding Monticello Dry Shielded Canister (DSC)-16. On February 17, 2014, dye penetrant examinations were performed on the outer top cover plate (OTCP) to shell weld on dry shielded canister (DSC)-16. This was a re-examination of a linear indication identified on January 24, 2014. The results of the re-examination identified a 1.6 inch linear indication that remained after surface conditioning. This indication had not been previously detected by nonconforming nondestructive examination previously reported by TriVis Inc. Xcel Energy is evaluating the condition and will remedy prior to moving the cask to the ISFSI (Independent Spent Fuel Storage Installation) pad. The associated DSCs loaded during the current campaign successfully passed their helium leak tests. Helium leak checks are performed to demonstrate confinement and boundary integrity. Thus, public health and safety is not affected. Since the licensee communication plan also notified other government agencies, this report is being made pursuant to 10CFR50.72(b)(2)(xi) and 72.75(b)(2). The above referenced dry shielded canister is currently located on the refuel floor in the reactor building. The licensee notified the NRC Resident Inspector.
ENS 4993820 March 2014 15:20:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionAppendix R Fire Door Failed to Close and LatchAt 1020 CDT, door 410B did not automatically close and latch as required. Door 410 B is an Appendix R fire door that is required for divisional separation of safe shutdown equipment. Due to the doors inability to close and latch as required, divisional separation could not be assured in the event of a fire. A continuous fire watch was established once the deficiency was discovered. The door was repaired and verified to be working properly. The door was non-functional for approximately one hour and fifteen minutes from the time of discovery. Health and safety of the public was maintained as the plant was in a normal condition and there has been no actual condition needing the door to close and latch. The NRC Resident Inspector has been notified.05000263/LER-2014-005
ENS 4997028 March 2014 18:58:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Failure of Secondary Containment Door InterlockAt 1358 (CDT) on March 28, 2014, the Control Room was notified that two Secondary Containment doors (DOOR-62 and DOOR-63) were open at the same lime. This occurred while two employees were entering and exiting the Reactor Building at the exact same time. The time that both doors were open was approximately one (1) second. Secondary Containment differential pressure was maintained throughout the event. With both doors open, technical specification surveillance requirement SR 3.6.4.1.3 was not met and Secondary Containment was declared inoperable. Secondary Containment was declared operable after independently verifying at least one Secondary Containment access door was closed. The health and safety of the public was maintained as the plant was in a normal condition with no initiating event in progress or signs or elevated radiation levels within Secondary Containment. The NRC Resident Inspector has been notified.05000263/LER-2014-006
ENS 500057 April 2014 20:00:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessRemoval of Radiation Monitors from Service for Planned MaintenanceBoth Discharge Canal Radiation Monitor Sample Pumps will be removed from service to facilitate planned maintenance activities. This represents a loss of emergency assessment capability under NUREG-1022 Revision 3 since the Discharge Canal Radiation Monitors are used to assess NUE (Notification of Unusual Event) and Alert thresholds. The Sample Pumps are expected to be unavailable for approximately two hours. During this time, Chemistry will be obtaining samples every 2 hours. As a result of the sampling, reasonable assurance exists that rising radiation levels will be able to be detected and monitored in order to protect the health and safety of the public. The NRC Resident (Inspector) has been notified prior to removing the Radiation Monitors from service.
ENS 5002611 April 2014 02:00:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification Due to a Dead Duck Found on SiteMonticello Nuclear Generating Plant personnel discovered the remains of what appeared to be a deceased duck on plant property. The cause of death was not immediately apparent, no work was ongoing within the vicinity at the time. Notifications to the Minnesota Department of Natural Resources and the Division of Fish and Wildlife will be made for this discovery. This event is reported per 10CFR50.72(b)(2)(xi). The licensee has notified the NRC Senior Resident Inspector. Plant personnel could not determine if the duck was an endangered species.
ENS 5004922 April 2014 19:00:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification Due to Deceased Migratory Bird Found on Plant PropertyMonticello Nuclear Generating Plant personnel discovered the remains of a deceased migratory bird on plant property. The cause of death was not immediately apparent, no work was ongoing in the vicinity at the time the bird was found. Notifications to the Minnesota Department of Natural Resources and the Division of Fish and Wildlife will be made for this discovery. This event is being reported per 10CFR50.72(b)(2)(xi). The NRC Resident Inspector will be informed.
ENS 5005223 April 2014 15:00:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification Due to Deceased Migratory Bird Found on Plant PropertyMonticello Nuclear Generating Plant personnel discovered the remains of a deceased migratory bird on plant property. The cause of death was not immediately apparent and no work was ongoing in the vicinity at the time the bird was found. Notifications to the United States Fish and Wildlife Service will be made for this discovery. This event is being reported per 10CFR50.72(b)(2)(xi). The licensee has informed the NRC Resident Inspector.
ENS 500771 May 2014 13:40:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessService Water Radiation Monitor Taken Out of Service for Planned MaintenanceThe Service Water Radiation Monitor will be removed from service to facilitate planned preventative maintenance. As a result, this represents a loss of emergency assessment capability under NUREG 1022 revision 3 specific to RU 1.2 and RA 1.2. The planned maintenance is expected to last 7 hours. During this time, the site Chemistry Department will perform sampling every thirty minutes per procedure. As a result of the sampling, reasonable assurance exists to monitor and detect rising radiation levels in order to protect the health and safety of the public. The NRC Resident Inspector has been informed.
ENS 5011715 May 2014 21:20:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionDegraded Fire BarrierA degraded fire barrier was identified during a walkdown on May 15th, 2014 at 1620 (CDT). The barrier separates Appendix R safe shutdown divisional equipment. A fire watch has been established as a compensatory measure. The health and safety of the public was not jeopardized as a result of this condition as there have been no fires or initiating events. The discovery of this degraded fire barrier is being reported as an unanalyzed condition as defined by 50.72(b)(3)(ii)(B). The licensee has notified the NRC Senior Resident Inspector.
ENS 5013623 May 2014 16:30:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessLoss of Assessment Capability Due to Failed Area Radiation MonitorAt 1130 CDT, an Area Radiation Monitor (ARM) was determined to be non-functional as a result of a failed calibration test. This represents a loss of assessment capability reportable under 10CFR50.72(b)(3)(xiii). A portable radiation monitor has been placed in the affected area as a compensatory measure. The health and safety of the public was protected as the plant was in a normal condition with no initiating event in progress or signs of elevated radiation levels on any other radiation monitors. The NRC Resident Inspector has been notified. The failed ARM is located in the 'A' RHR core spray room.
ENS 501755 June 2014 21:01:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessDischarge Canal Radiation Monitors Removed from Service for Planned MaintenancePlanned preventive maintenance will render the discharge canal radiation monitors inoperable for both A and B trains. As a result, this represents a loss of emergency assessment capability and is reportable under 10 CFR 50.72 (b)(3)(xiii). The planned maintenance is expected to last two hours. During this time, the site Chemistry Department will be perform sampling as a compensatory measure. The health and safety of the public remains protected as the plant is operating in a normal condition. The NRC Resident Inspector was notified prior to removing the discharge canal radiation monitors from service.
ENS 5022525 June 2014 05:00:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessVarious Telecommunication Lines and Erds Outage for Planned Maintenance

Planned preventive maintenance will render parts of telephone system and Emergency Response Data System (ERDS) nonfunctional. As a result, this represents a loss of emergency communications capability and is reportable under 10 CFR 50.72(b)(3)(xiii). The maintenance is scheduled to begin on 6/25/2014 at 00:00 (CDT), and is expected to last approximately 5 hours. During this maintenance window, various communication connections will be intermittently interrupted for short periods of time. Affected communication connections include some local telephone company lines, Federal Telephone System, ERDS, the Monticello's NRC office, and automatic ring down lines to the state of Minnesota's Emergency Operations Center. During the planned maintenance window, communications to offsite will be available via radios, cell phones, and satellite communications. This ensures that the plant can adequately communicate with the NRC, state, and local agencies to ensure protection of the health and safety of the general public. The NRC Resident Inspector has been notified of the planned telecommunications maintenance. Licensee also notified the Minnesota State Duty Officer and the Wright and Sherburne County Sheriff dispatchers.

  • * * UPDATE PROVIDED BY DAMON HESSIG TO JEFF ROTTON AT 1823 EDT ON 06/25/2014 * * *

At 0500 (CDT) on 6/25/2014, planned maintenance on the Monticello telecommunications system was completed. At 1630 (CDT) on 6/25/2014, testing of all telecommunications was completed. All systems are functioning properly. The NRC Resident Inspector has been notified that the telecommunications system is functional. The Minnesota State Duty Officer and the Wright and Sherburne County Sheriff dispatchers have been notified that the telecommunications system is functional. Notified R3DO (Lara).

ENS 5032731 July 2014 12:20:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessService Water Radiation Monitor Out of Service for MaintenancePlanned preventative maintenance on the Service Water Radiation Monitor (SWRM) strainer will remove the SWRM from service. As a result, this represents a loss of emergency assessment capability since the SWRM is used to assess NUE and ALERT thresholds. The activity is expected to last 6 hours. During this time, the site will be monitoring alternate indications to detect leakage and the Chemistry Department will perform grab samples as required to ensure the ability to detect NUE levels of radioactivity in a timely manner and protect the health and safety of the public. The NRC Resident Inspector has been notified prior to removing the SWRM from service.
ENS 503455 August 2014 19:46:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentBoth Trains of Control Room Emergency Filtration System InoperableThe Division 1 Control Room Emergency Filtration System (CREF) was inoperable for scheduled replacement of charcoal. During the scheduled maintenance, Division 2 CREF was placed into service. Approximately 5 minutes after startup (1446 CDT on 8/5/2014), the Division 2 CREF recirculation fan tripped off for unknown reasons. This rendered both trains of CREF inoperable. This required entry into Technical Specification TS 3.0.3. This is being reported pursuant to 10 CFR 50.72(b)(3)(v)(D) as an event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to (D) Mitigate the consequences of an accident. At 1707 CDT on 8/5/2014, the Division 1 CREF train maintenance was completed and the Division 1 CREF was declared operable. TS 3.0.3 was exited at this time. Investigation is in progress to determine the cause of the Division 2 CREF trip. The control room boundary was not challenged during this time period with any change in radiation levels as plant operation was unaffected. Thus, the health and safety of the public was not affected. The licensee notified the NRC Resident Inspector and the State of Minnesota Duty Officer.
ENS 5036414 August 2014 12:55:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessService Water Radiation Monitor Nonfunctional for Planned MaintenanceThe service water radiation monitor system will be rendered nonfunctional during planned preventive maintenance. As a result, this represents a loss of emergency assessment capability and is reportable per 10CFR50.72(b)(3)(xiii). The planned maintenance is expected to last 4 hours. During this time, plant parameters will be monitored and sampling will be performed which will support sustaining the health and safety of the public during this planned maintenance activity. The NRC Resident Inspector will be notified prior to removing the service water radiation monitor from service.
ENS 5041128 August 2014 14:00:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessBoth Discharge Canal Radiation Monitors Removed from Service for Planned Maintenance'Planned preventive maintenance will render both divisions of discharge canal radiation monitors non-functional. As a result, this represents a loss of emergency assessment capability and is reportable under 10 CFR 50.72(b)(3)(xiii). The planned maintenance is expected to last two hours. During this time, alternate plant parameters will be monitored and sampling performed if needed. The health and safety of the public remains protected as the plant is operating in a normal condition. The NRC Resident Inspector was notified prior to removing the discharge canal radiation monitors from service.
ENS 5045614 September 2014 07:26:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionOperation in Unanalyzed Region of the Power to Flow Map

At 0226 CDT on September 14, 2014, MNGP (Monticello Nuclear Generating Station) experienced a trip of the 12 Reactor Recirc Pump. The subsequent power drop and lowering of recirculating water flow resulted in the plant being outside of the analyzed region of the Power to Flow Map. Operators promptly restored operation within the analyzed region per procedural guidance. This event has been determined to be a condition where the plant was in an unanalyzed condition that significantly degrades plant safety and is reportable under 50.72(b)(3)(ii). The plant is in stable condition at 51% power and the health and safety of the public were not affected. The investigation of the cause of this event is in progress. The licensee will notify the NRC Resident Inspector.

  • * * RETRACTION FROM SCOTT CHRISTOS TO HOWIE CROUCH AT 1433 EST ON 11/10/14 * * *

Further analysis has determined that the condition did not significantly degrade plant safety. General Electric Hitachi was requested to review the event and confirm the SIL653 guidance remains applicable for MELLLA+ (Maximum Extended Load Line Limit Analysis) operation. This review was completed and the conclusions of SIL653 remain valid . The SIL states that: 'unplanned events that result in the plant exceeding the licensed upper boundary do not constitute a safety concern. The consequences of such unplanned events are bounded by the GE safety analysis of limiting events initiated from within the licensed operating domain. Stability monitoring and protection using Detection and Suppression Solution Confirmation Density remained available throughout the event (oscillating power range monitors). The NRC Resident Inspector has been notified. Notified R3DO (Hills).

ENS 5049626 September 2014 03:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(xiii), Loss of Emergency Preparedness
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Containment Isolation Declared Inoperable Due to Relay Age

At 2200 CDT on September 25, 2014, the Duty Shift Manager was notified that Agastat relays associated with Primary Containment Isolation valves on the Hydrogen-Oxygen Analyzing System are beyond the analyzed shelf life for relays that are in the normally energized state and are considered INOPERABLE. This affected both primary containment isolation valves for a containment penetration on multiple flow paths. This issue was determined to be reportable under (10 CFR) 50.72 (b)(3)(v)(C) & (D) for an event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to control the release of radioactive material and mitigate the consequences of an accident. Additionally, the required actions involved isolating six flow paths via manual isolation valves. This action rendered the Hydrogen-Oxygen Analyzers non-functional for both trains and constitutes a loss of Emergency Preparedness and Accident Assessment Capability. This is reportable under (10 CFR) 50. 72(b)(3)(xiii). The Primary Containment Isolation Valves have been, and remain, in their closed position to satisfy their Primary Containment Function and protect the health and safety of the public. The NRC Senior Resident Inspector has been notified. The licensee will notify the State of Minnesota. The relays of concern were manufactured 19 years ago and have been in operation for 11 years, versus a manufacturer assumption of a 10 year operational lifespan.

  • * * UPDATE FROM SCOTT CHRISTOS TO DONALD NORWOOD AT 1430 EST ON 11/20/2014 * * *

Partial retraction for EN 50496. This is an update of Emergency Notification System (ENS) report 50496 that was submitted at 0253 EDT on Friday, September 26, 2014. ENS notification was made due to four relays associated with the sampling valves on the Hydrogen-Oxygen Analyzing (HOA) system that perform Primary Containment Isolation Valve (PCIV) functions. These relays were discovered installed beyond their manufacturer qualified service life, which called operability into question. The portions 10 CFR 50.72 (b)(3)(v)(C) & (D) are being retracted after subsequent bench testing and investigation of system operability. Based on the past operability evaluation, all four relays associated with PCIV functions on the HOA system would have performed their specific safety function of primary containment isolation, as required by the facility's technical specifications. Therefore, this event does not meet the threshold of an event or condition that would prevent fulfilment of a safety function. The loss of emergency preparedness and accident assessment capability previously reported under 10 CFR 50.72 (b)(3)(xiii) remains unchanged. The NRC Resident Inspector has been notified. Notified R3DO (Peterson).

ENS 5066310 December 2014 00:30:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionHigh Energy Line Break Door Found Closed

At 1830 (CST) on December 9, 2014 Door 410B, a HELB (High Energy Line Break) door between the east and west sides of the ground floor of the reactor building, was found closed. This door is one half of a pair of double doors that are normally open to provide a HELB energy and flooding release path to mitigate postulated HELB events. The closed HELB door has the potential to impact safe shutdown by exposing both divisions of safe shutdown components to unanalyzed environmental conditions. With the potential loss of both divisions of safe shutdown equipment, no safe shutdown path would exist. This condition is being reported as an unanalyzed condition as defined by (10 CFR) 50.72(b)(3)(ii)(B). The HELB door was immediately opened and returned to normal configuration. Door 410A remained open during the time that Door 410B was closed and provided an available, but not yet analyzed, release path that could have mitigated the consequences of this event. The health and safety of the general public was not impacted as a result of this condition. The NRC Resident Inspector has been notified.

  • * * RETRACTION FROM JON LAUDENBACH TO CHARLES TEAL ON 1/30/15 AT 1513 EST * * *

Further analysis has determined that the condition did not significantly degrade plant safety. Door 410B in the Reactor Building was found closed. This door is one half of a pair of double door (Doors 410A and 410B) that normally open to provide a High Energy Line Break (HELB) energy and flooding release path to mitigate postulated HELB events. The condition of one half of the double door closed was not previously analyzed. A subsequent completed engineering evaluation analyzed this condition, Door 410B being closed and Door 410A being open, for the following environmental conditions: peak compartment temperatures, block wall differential pressure, radiation dose, and flooding. The environmental conditions found the Reactor Building in response to Door 410B being closed with 410A being open does not affect the operability of safety related equipment housed within the Reactor Building or the ability to safely shut-down the plant and maintain the plant shutdown condition following a HELB event. The NRC Resident Inspector has been notified. Notified R3DO (Dickson).

ENS 5070529 December 2014 02:23:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Two Inoperable Emergency Diesel GeneratorsWhile the 12 Emergency Diesel Generator (EDG) was inoperable for performance of the monthly surveillance, adjustments were inadvertently made to 11 EDG which made it inoperable. As a result, Technical Specification (TS) 3.8.1 Condition E, for both EDG's inoperable was entered. Monticello has subsequently restored 12 EDG to an operable status within the 2 hour TS LCO (Limiting Condition for Operation) completion timer requirement. The station remained in a safe condition during this discovery with 12 EDG available at all times. The plant continues to operate in a normal condition with no initiating events present. The health and safety of the public was not impacted as a result of this condition. The NRC Resident Inspector has been notified. EDG 12 was restored to operable status at 2214 CST and EDG 11 will remain inoperable until a surveillance test is performed to start the EDG and restore the local governor control idle speed to the correct setting. The licensee will be notifying the Minnesota State Duty Officer.