ML20004F069
| ML20004F069 | |
| Person / Time | |
|---|---|
| Site: | Farley |
| Issue date: | 06/01/1981 |
| From: | Hairston W ALABAMA POWER CO. |
| To: | |
| Shared Package | |
| ML20004F068 | List: |
| References | |
| NUDOCS 8106160464 | |
| Download: ML20004F069 (4) | |
Text
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O JOSEPH M. FARLEY NUCLEAR PLANT UNIT 1 NARRATIVE
SUMMARY
OF OPERATIONS MAY, 1981 In the month of May,1981, there were two (2) automatic unit shutdowns and one (1) power reduction.
The following safety-related maintenance was performed in May:
- 1. Performed miscellaneous maintenance.on diesel generators.
- 2. Replaced fiber optics lamp in the 'A' Train control room chlorine detector.
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8106160[l ..
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OPERATING DATA REPORT DOCKET NO. 50-348 DATE 6/1/81 COMPLETED BY W.G.Hairston, III TELEPHONE M 899-5156
_ OPERATING STATUS
- 1. Unit Na'me: .Ioseph M. Farley - Unit 1 Notes: (1) Cumulative data May, 1981 since 12/1/77, date of
- 2. Reporting Period:
2652 conunercial operation.
- 3. LicensedThermalPower(MWt):
- 4. Nameplate Rating (Gross MWe): 860 ,
S. Design Electrical Rating (Net MWe): 829
. 6. Maximum Dependable Capacity (Gross MWe): 844.6
- 7. Maximum Dependable Capacity (Net MWe): 803.6
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
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N/A .
- 9. Power Level To Which Restricted,1f Any (Net MWe): N/A
- 10. Reasons For Restrictions.lf Any: N/A ,
' ThisM nth Yr.-to.Date 'Cu'$mlatise
- 11. Hours In Reporting Period 744 3,623 30,671
- 12. Number Of Hours Reactor Was Critical 675.9 1,386.0 18,568.3
- 13. Reactor Reserve Shutdown Hours 68.1 364.9 2,811.7 i 14. Hours Generator On-Line 654.6 1,220.1 17,923.5 i 15. Unit Reserve Shutdown Hours 0 0 0
- 16. Gross Thermal Energy Generated (MWH) 1,639,347.6 2,773,783.1 44,763,674.9
- 17. Gross Electrical Energy Generated (MWH) 522,334 _,
883,270 14,302,678
- 18. Net Electrical Energy Generated (MWH) 495,612 805,772 13,413,522
- 19. Unit Service Factor 88.0 ,
33.7 58.4
- 20. Unit Availability Factor 88.0 ,
33.7 58.4
- 21. Unit Capacity Factor (Using MDC Net) - 82.9 27.7 54.4
- 22. Unit Capacity Factor (Using DER Net) 80.4 26.8 52.8
- 23. Unit Forced Outage Rate 12.0 20.2 8.0 l 24. Shutdowns Scheduled Over Next 6 Months (Type. Date.ar
- Duration of Each):
l N/A l
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- 25. If Shut Down At End Of Report Period. Estimated Date of Startup: N/A
- 26. Units In Test Status IPrior to Commercial Operation): Forecast Achiesed INITIAL CRITICALITY 8/6/77 8/9/77
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INITIA L ELECTRICITY 8/20/77 8/18/77 COMMERCIAL OPERATION 12/1/77 12/1/77 P00R BR K 1
Ayrmwr.uAII.T UNITPOWER I.IVEI. .
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.. DOCKETNO. 50-348 D ;
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DATE 6/1/a1 COMPU.TED SY W. G. Hairston, III TELEPHONE. (205)899-5156
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MONTH May, 1981 - .
t DAY AVERAGE DAILY POWER LEVEI.
- DAY AVERAGE DAILY POWER L.W.
i . (MWe Net) .
' (MWe Net) ~ ~ '
g, 802 g7 .
2 8d3 - gg .
l ^ '
I 3
800- g, 211' - - -
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4 811 -
23 611
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7 5
810 -
n'" ~0~
6 806 428 ' , y. .
. 22 _-
l 808 803 - .
t 7 23 . .
m.. .
810 801 8 24 .
l 9 811 . -.
.y. - - 804 .
10 809 ' . '.. .j, 803 --
=
Ig 812 -
27, .
799- - ~
813 - -
'798 -
12 .. . ... 3- . .
~~r.
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813 . 629 -
13 , 3 810
~ . - . 326 l'
!4 .
33
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.. gg 810 - ... .
778 -
s.
31 _
16 -
~811 . .
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INSTRUCHONS - - -
, On this formst.!ist the sver:te d.tily unit power levet in MWe Net for c:ch day in the reporting munth. Cocspute to the nearest whole met:wstt.
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UNITSilUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-348
- UNIT NAME J.M.Farlev-Unit 1 DATE 6/1/81 REPORT MONTil May. 1981 COMPLETED BY W.G.llairston. III TELEPif0NE (205)899-5156 1 "k -
a n ,5 m: 5 o E _e 8 g Ei 'f Licensee 5% Cause & Corrective No. Date g gg g ,, g e Event u5 Action to
- c5 6 5 j@* RcPort # NC b" g! Prevent Recurrence 013 810517 F 54.2 A 3 N/A CH VALVEX Unit tripped due to loss of instril-ment air to 1C feedwater regulating valve causing the valve to close.
Instrument air line break was repaired .
and Unit returned to service. -
014 810520 F 35.2 H 3 N/A EB CKTBKR Unit tripped due to Lo-Lo S/G level caused by trip of both S/G feed pumps, i
015 810529 S 0 B 4 N/A CH VALVEX Unit reduced to and held at 120 Mw te perform maintenance of IC feed i regulating valve. Control problems.
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i i 2 3 4 F: Forced Reason: Method: Exhibit G . instructions S: Scheduled A. Equipment Failuse(Explain) . l. Manual for l' reparation of Data U Maintenance of Test 2 Manual Scram. Entry Sheets for Licensee C Refueling 3 Automatic Scr m. Event lleport (LER) File (NUltEG-D Regulato y Restriction 4 Other (Explala) 0161)
E Operator Training & License Examination <
F-Administrative 5 i G Operational Error (Explain) Exhibit I . Same Source
- (9/77) Il Other (Explain)
)