ML20054G340
ML20054G340 | |
Person / Time | |
---|---|
Site: | |
Issue date: | 06/07/1982 |
From: | Frahm R Public Service Enterprise Group |
To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
Shared Package | |
ML20054G330 | List: |
References | |
LER-82-034-03L-01, LER-82-34-3L-1, NUDOCS 8206210460 | |
Download: ML20054G340 (1) | |
Text
NRC FZM 366 U, S. NUCLE AO REIULATZ.Y COMMISSION (7 77)
.* LICENSEE EVENT REPORT CONTCOL 8LOCX: l i
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(PLEASE PRINT CD TYPE ALL CE~UIRE31NFU MATIZNI ,
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$7 C A T 58 l@
8 8 9 LICENSEE CQQE CON'T I0l1l ["cg l Lhl 0l 5] 0l0 lol217l2@l0l5lll0] 8l 2@l 0 l 6 l 0l 7l 8l 2l@ 68 69 EVENT OATE 7# 75 REPORT DATE 80 e 60 91 oOcxET NuMSER EVENT OESCRIPTION AND PROBABLE CONSEQUENCES h
,o,;;jon May 10, 1982 during routine operation, the Control Room Operator noticed the l gg 3, gN o. 14 Steam Generator Wide Range Level indication had failed low. The channel was l
- o,,j[leclared inoperable at 0415 hours0.0048 days <br />0.115 hours <br />6.861772e-4 weeks <br />1.579075e-4 months <br />, and Limiting Condition for Operation 3.3.3.7 l lo;5l l Action 1 was entered. This occurrence constituted operation in a degraded mode in l l0161 pccordance with Technical Specification 6.9.1.9.b. (82-025) 1 -
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I l o la I f 80 8 ,
SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUSCODE COMPONENT CODE SU8 CODE SUBCQQE l0l9l 7 8 lI l E lh {h l Z lh lIl Nl S l Tl Rl Ulh Wh J h 9 to it 12 13 18 19 20 REVislON
_ SE QUENTI AL OCCURPENCE REPORT EVENTYEAR REPORT NO. CODE TYPE NO.
LER 80 O ,ag' ,,,21l e l 222 l l-l 23 1013l4l 24 26
[d 27 1013J 28 '9 ltl 30 l-l 31 Lo_]
32 AX N A T ON O PLANT MET MOURS S8 i FOR 8. SUPPLI MANUFACTURER lE l 23 lJ4 Zl@ l Zlh l36Z lh l70l0l0l0l 35 3 40 Wh 41 l Nlh l3L lh 42 4 l44H l 0 l 2 l 47 1l@
CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l i l 0 l lThe failure of No. 14 Steam Generator Wide Rance Level Tnstrument was due to a loose l I i l i l ifiise in the power supply. The loose fuse was nronerly tichrennd. nna Wo i n e-n* I gi;2) Fas satisfactorily tested. At 0450 hours0.00521 days <br />0.125 hours <br />7.440476e-4 weeks <br />1.71225e-4 months <br />, No. 14 Steam Generator Wide Rance Level l g l Instrument was declared operable, and Limitino Condition for Onaration 3.3.3.7 l g ] Action 1 was terminated. 80 l
7 8 g S % POWE R OTHE R STATUS DIS RY DISCOVERY DESCRIPTION lt l5l h l 0l 9l 8lhl N/A l l A lhl Operator Observation l ACTivlTY CO TENT TELE ASED OF RELE ASE AMOUNT OF ACTIVITY LOCATION OF RELEASE N/A l l N/A l
[1 l68 9l l Zl @ Whlt1 7 10 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE D E SCRIPTION N/A !
ITITl l 0l 0 l O l@l Zlhl' PERSONNE L INJURIES NUM8tR DESCRIPTION l
7 1 a 8 9 l0l0l0l@l 11 12 N/A 80 LOSS OF OR DAMAGE TO FACILITY TvPE DESCRIPTION 7 8 9 h 10 N/A 80 PU8uCITY NRC USE ONLY iS$utD DESCRIPTION 5 W Whl N/A J lllIllIIlllI!I 7 8 9 to 68 69 80 S NAME OF PREPARER L Frahm PHONE:
8206210460 920607 ~ ' ~ " - ~~~
PDR A
ADOCK 05000298 pnp