ML15160A608: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
Line 1: Line 1:
{{Adams
#REDIRECT [[RC-15-0085, LER 15-002-00 for V.C. Summer, Unit 1, Regarding Low Oil Level Trip Renders Chillers Non-Functional and a Train of Charging System Inoperable]]
| number = ML15160A608
| issue date = 06/08/2015
| title = LER 15-002-00 for V.C. Summer, Unit 1, Regarding Low Oil Level Trip Renders Chillers Non-Functional and a Train of Charging System Inoperable
| author name = Gatlin T D
| author affiliation = South Carolina Electric & Gas Co
| addressee name =
| addressee affiliation = NRC/Document Control Desk, NRC/NRR
| docket = 05000395
| license number = NPF-012
| contact person =
| case reference number = 818.07, CR-13-02694, CR-13-03952, RC-15-0085
| document report number = LER 15-002-00
| document type = Letter, Licensee Event Report (LER)
| page count = 5
}}
 
=Text=
{{#Wiki_filter:Thomas D. Gatlin Vice President, Nuclear Operations 803.345.4342 A SCANA COMPANY June 8, 2015 Document Control Desk U. S. Nuclear Regulatory Commission Washington, DC 20555
 
==Dear Sir / Madam:==
 
==Subject:==
VIRGIL C. SUMMER NUCLEAR STATION (VCSNS), UNIT 1 DOCKET NO. 50-395 OPERATING LICENSE NO. NPF-12 LICENSEE EVENT REPORT (LER 2015-002-00)
LOW OIL LEVEL TRIP RENDERS CHILLER NON-FUNCTIONAL AND "A" TRAIN OF CHARGING SYSTEM INOPERABLE Attached is Licensee Event Report (LER) 2015-002-00, for the Virgil C. Summer Nuclear Station (VCSNS). This report describes a condition that rendered the "A" Chiller non-functional.
This report is submitted in accordance with 10 CFR 50.73(a)(2)(i)(B).
Should you have any questions, please call Mr. Bruce Thompson at (803) 931-5042.Very truly yours Thomas D. Gatlin WLTFTDG/ts Attachment c: K. B. Marsh S. A. Byrne J. B. Archie N. S. Carns J. H. Hamilton J. W. Williams W. M. Cherry V. M. McCree S. A. Williams NRC Resident Inspector QA Manager -L. W. Harris Paulette Ledbetter J. C. Mellette ICES Coordinator K. M. Sutton INPO Records Center Marsh USA, Inc.Maintenance Rule Engineer NSRC RTS (CR-13-02694/CR-13-03952)
File (818.07)PRSF (RC-15-0085)
£9-(%~44 V. C. Summer Nuclear Station -P. O. Box 88 .Jenkinsville, SC .29065. F (803) 941-9776 NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 01/31/2017 (02-2014)
Estimated burden per response to comply with this mandatory collection request: 80 hours.Reported lessons learned are incorporated into the licensing process and fed back to industry.Send comments regarding burden estimate to the FOIA, Privacy and Information Collections SL SE EBranch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by LICENSEE EVENT REPORT (LER) intemet e-mail to lnfocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and (See Page 2 for required number of Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB digits/characters for each block) control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
: 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE V.C. Summer Nuclear Station, Unit 1 05000 395 1 OF 4 4. TITLE LOW OIL LEVEL TRIP RENDERS CHILLER NON-FUNCTIONAL AND "A" TRAIN OF CHARGING SYSTEM INOPERABLE
: 5. EVENT DATE 6. LER NUMBER 7. REPORT DATE 8. OTHER FACILITIES INVOLVED MONT YEAR YEAR SEQUENTIAL REV FACILITY NAME DOCKET NUMBER NUMBER NO MONTH DAY YEAR 05000 FACILITY NAME DOCKET NUMBER 4 9 2015 2015 -002 00 6 8 2015 05000 9. OPERATING MODE 11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check all that apply)El 20.2201(b)
[ 20.2203(a)(3)(i)
[] 50.73(a)(2)(i)(C)
[] 50.73(a)(2)(vii)
[] 20.2201(d)
E] 20.2203(a)(3)(ii)
[] 50.73(a)(2)(ii)(A)
[ 50.73(a)(2)(viii)(A)
[] 20.2203(a)(1)
F] 20.2203(a)(4)
[] 50.73(a)(2)(ii)(B)
[ 50.73(a)(2)(viii)(B)
[] 20.2203(a)(2)(i)
[ 50.36(c)(1)(i)(A) 50.73(a)(2)(iii)
[ 50.73(a)(2)(ix)(A)
: 10. POWER LEVEL [] 20.2203(a)(2)(ii)
[ 50.36(c)(1)(ii)(A) 50.73(a)(2)(iv)(A)
[ 50.73(a)(2)(x)
El 20.2203(a)(2)(iii)
[ 50.36(c)(2) 50.73(a)(2)(v)(A)
[ 73.71(a)(4) 100 El 20.2203(a)(2)(iv)
[ 50.46(a)(3)(ii) 50.73(a)(2)(v)(B)
[ 73.71(a)(5)
El 20.2203(a)(2)(v)
El 50.73(a)(2)(i)(A)
El 50.73(a)(2)(v)(C)
El OTHER El 20.2203(a)(2)(vi)
[ 50.73(a)(2)(i)(B)
El 50.73(a)(2)(v)(D)
Specifyoin Abstract below or in 12. LICENSEE CONTACT FOR THIS LER LICENSEE CONTACT TELEPHONE NUMBER (Include Area Code)Bruce Thompson, Manager Nuclear Licensing (803) 931-5042 13. COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT MANU- REPORTABLE CYMANU- REPORTABLE CAUSE SYSTEM COMPONENT FACTURER TO EPIX CAUSE SYSTEM COMPONENT FACTURER TO EPIX B KM CHU N418 A 14. SUPPLEMENTAL REPORT EXPECTED 15. EXPECTED MONTH DAY YEAR El YES (If yes, complete 15. EXPECTED SUBMISSION DATE) El NO SUBMISSION I ~ DATEI ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines)A past operability review determined that HVAC System Mechanical Water Chiller (XHXOOOIA) had been non-functional during the month of July 2013 due to a vulnerability with component operation resulting in a low oil level condition.
The event impacts the operability requirements of the Chilled Water (VU) System and the area room coolers the system supports per TS 3/4.7.9, "Area Temperature Monitoring." On September 25, 2013, XHXOOO1A tripped on low oil level following surveillance testing. The "Circuit 2 Low Oil Level" fault occurred due to the compressor oil level dropping below the low oil level indicator switch set point for 60 seconds which initiates shutdown of the component.
The cause was low superheat, causing liquid floodback to the compressor and a low evaporator heat load that was insufficient to promote proper oil return in the evaporator.
The chiller unit was intermittently operated as the only chiller on the"A" VU train in July 2013. Due to this vulnerable condition the non-functional chiller impacted the operability of the "A" train components served by the "A" train VU system.On April 9, 2015, the station determined this event was reportable and is being submitted in accordance with 10 CFR 50.73(a)(2)(i)(B).
NRC FORM 366 (02-2014)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 01/31/2017 (02-2014)
Estimated burden per response to comply with this mandatory collection request: 80 hours.Reported lessons learned are incorporated into the licensing process and fed back to industry."Send comments regarding burden estimate to the FOIA, Privacy and Information Collections
-LICENSEE EVENT REPORT (LER) Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by interaet e-mail to Infocotlects.Resource@nrc.gov, and to the Desk Officer, Office of Information CONTINUATION SHEET and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
: 1. FACILITY NAME 2. DOCKET 6. LER NUMBER 3. PAGE SEQUENTIAL REV YEAR NME O V.C. Summer Nuclear Station, Unit 1 NUMBER NO.05000 395 2 OF 4 2015 -002 -00 NARRATIVE EVENT DESCRIPTION A past operability review determined that HVAC System Mechanical Water Chiller (XHX0001IA) had been non-functional during the month of July 2013 due to a vulnerability with component operation resulting in a low oil level condition.
On September 25, 2013 XHX0001A had tripped on low oil level following surveillance testing. The "Circuit 2 Low Oil Level" fault occurred due to the compressor oil level dropping below the low oil level indicator switch (ILI-19039A-VU) set point for 60 seconds which initiates an alarm and chiller unit shutdown.
Data collected from the event indicates XHX000IA was started when the chilled water at the inlet of the component was 60 degrees Fahrenheit and the alarm came after Compressor 2 shut off as the "lag" circuit. The lag circuit shutdown occurs when the chilled water outlet temperature is below 43.5 degrees Fahrenheit and combined compressor amps are below 250 amps for greater than 120 seconds. After the lag circuit permissive was satisfied, Circuit 2 was signaled to shut off and the"Circuit 2 Low Oil Level" fault was received resulting in shutdown of the chiller.EVENT ANALYSIS XHX1OOOIA was installed on August 5, 2011 and is one of three chiller units that provide chilled water to the VU System.XHX0001A is a different design than XHXOOO1B and XHX0001C.
XHX0001A is a 280-ton three tier chiller skid that has 2 equal capacity circuits that are independently controlled via a Triconex Programmable Logic Controller.
The VU System has two trains and is designed to provide safety related cooling to various areas and equipment as discussed in FSAR 9.4.7.2.4.
XHX0001C is used as a swing component that is powered from either train of Safeguards Power.The VU System provides cooling to safety related areas (TS Table 3.7-7) as an attendant cooling system and supports the comfort requirements for the Control Room Emergency Filtration Systems (CREFS). The VU System is needed to ensure equipment located within these areas can withstand the environmental effects of a postulated FSAR chapter 15 event. With a non-functional chiller unit, the VU system will become inoperable therefore affecting room temperatures and the reliability of associated equipment within the safety related area. The most limiting area for temperature limits has been identified as the Charging Pump Rooms. Per TS 3/4.5.2, one Charging Pump has to be operable per train of Emergency Core Cooling System (ECCS).TS 3/4.7.6, "Control Room Emergency Filtration Systems (CREFS)" states that two CREFS trains shall be operable.
The surveillance requirements under TS 3/4.7.6 require each CREFS train to be demonstrated operable through verification that the control room air temperature is less than or equal to 85 degrees Fahrenheit.
TS 3/4.7.9, "Area Temperature Monitoring", and associated Table 3.7-7 describe the area temperature limits during normal operation due to cooling provided by the VU System. If the chiller cooling a chilled water loop is not running, room temperatures will rise over time. If the temperature in a given area exceeds the limit shown in TS Table 3.7-7 for eight hours a Special Report detailing past basis for continued operability must be submitted to the NRC. If the technical specifications limit for a given area is exceeded by thirty degrees for four hours, the equipment in the associated area must be declared inoperable.
NRC FORM 366A (02-2014)
NRCFORM2 3 LICENSEE EVENT REPORT (LER) U.S. NUCLEAR REGULATORY COMMISSION (02-2014)LIESEEETRP T E)CONTINUATION SHEET 1. FACILITY NAME 2. DOCKET 6. LER NUMBER 3. PAGE YEAR SEQUENTIAL REV V.C. Summer Nuclear Station, Unit 1 -NUMBER NO.05000 395 3 OF 4 2015 -002 -00 NARRATIVE LER 2013-003-00 dated August 21, 2013 [ML 13235A3 11] reported that XHX0001A had been inoperable/non functional since installation through June 2013 due to skid mounted molded case circuit breaker trip setpoint being set too low. That LER discussed the safety significance of the nonfunctional chiller during that time period.Investigation after the September 25, 2013 event found that XHXOOO1A has been also vulnerable to the low oil level condition since original installation on August 5, 2011 and was therefore non-functional since installation.
The past operability review determined that from July 5 through July 27, 2013, X-X0001A was intermittently operating as the only chiller on "A" train while being vulnerable to the low oil level condition during the following tinieframes:
Placed In Service 07/05/2013 at 18:30 07/11/2013 at 02:27 07/20/2013 at 03:06 Removed From Service 07/07/2013 at 17:03 07/20/2013 at 02:12 07/27/2013 at 09:54 Total Time 46.6 hours 215.8 hours 174.8 hours The second and third listed timefranmes represent times where "A" VU train was unavailable for greater than 72 hours which exceeds the TS 3/4.5.2 action requirements for XHXOOO IA.The September 25, 2013 trip was attributed to low superheat causing liquid floodback to the compressor and a low evaporator heat load that was insufficient to promote proper oil return in the evaporator.
The plant was operating at 100 percent power at the time of the event.SAFETY SIGNIFICANCE The safety significance of this event was minimal. The VU system function of cooling plant areas and equipment is not modeled in the Probabilistic Risk Analysis (PRA) model. The VU backup function to supply alternate cooling to Charging pump gear box is also not credited in the PRA model.The Final Safety Analysis Report (FSAR) 9.4.7.2.4 describes the Safety Class Chilled Water System. This section states that continuous operation of one of the three chillers and chilled water pumps is required during normal and emergency periods to provide 45 degrees Fahrenheit water to the chilled water coils. Use of three chillers and three chilled water pumps permits one unit to undergo extended maintenance.
When all three chillers and pump sets are available, one is designated as a spare and its breaker(s) is racked out. All chillers may also be started locally.During the periods of time in July 2013 when XHX0001A was the only operating chiller on "A" VU train, XHX00011B was operable and aligned to "B" VU train.If the XHX0001A tripped, XHXOOO1C would have been aligned to the "A" VU train per Annunciator Response Procedure before the temperatures became excessive.
NRC FORM 366A (02-2014)
NRC FORM 366A LICENSEE EVENT REPORT (LER) U.S. NUCLEAR REGULATORY COMMISSION (02-2014)CONTINUATION SHEET 1. FACILITY NAME 2. DOCKET 6. LER NUMBER 3. PAGE YEAR SEQUENTIAL REV V.C. Summer Nuclear Station, Unit 1 NUMBER NO.05000 395 4 OF 4 2015 -002 -00 NARRATIVE PREVIOUS OCCURRENCE XHX0001A tripped on Circuit 2 Low Oil Level on January 11, 2013, under similar circumstances.
Troubleshooting identified that the hot gas bypass valve on Circuit 2 was leaking by. The valve leak-by influenced Circuit 2 suction pressure and superheat values which resulted in excess liquid refrigerant being admitted to the compressor.
The hot gas bypass valve was repaired and XHX0001A was returned to service. In retrospect, this trip may have been as a result of low superheat causing liquid floodback to the compressor and low evaporator heat load to promote proper oil return in the evaporator.
LER 2013-003-00 dated August 21, 2013 [ML13235A3 11] reported that XHXOOO1A had been inoperable since installation through June 2013 due to skid mounted molded case circuit breaker trip setpoint being set too low.CORRECTIVE ACTIONS To resolve the liquid floodback failure mechanisms the suction piping on Circuit 2 of XHXOOOA was buffed to allow the thermal expansion valves (TXV) sensing bulb to be installed flush with the suction piping per the manufacturers' installation recommendations, software changes to prevent the lagging circuit from starting if the lead compressor has enough capacity to cool down the VU loop were implemented, XHXO00 IA TXVs were adjusted to ensure optimal superheat, and the initial 20% open position for the Service Water Motor Operated Valves was revised to 15% initial position in order to enhance compressor discharge pressure control.The corrective actions for the below minimum heat load failure mechanism include implementing software changes to improve chiller operation, modifying hot gas bypass function during dual circuit operation, reducing hot gas delay time from 30 seconds to 5 seconds, limiting minimum compressor unloading to 140 amps, and revising the logic permissive for securing the lag compressor to reduce the time the lag compressor runs at minimum loads during transients when two compressors are required.NRC FORM 366A (02-2014)}}

Revision as of 05:23, 13 July 2018