ML17229A090: Difference between revisions
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{{#Wiki_filter:CATEGORY1REGUL' | {{#Wiki_filter:CATEGORY1REGUL'ATINFORMATION DISTRIBUTIOtSTEM (RIDE)ACCESSION NBR:961,0280062 DOC.DATE: | ||
96/10/24NOTARIZED: | |||
NODOCKETgFACIL:50-335 St.LuciePlant,Unit1,FloridaPower&LightCo.05000335AUTH.NAMEAUTHORAFFILIATION STALL,"J.A. | |||
FloridaPower6LightCo.RECIP.NAME RECIPIENT AFFILIATION DocumentControlBranch(Document ControlDesk) | |||
==SUBJECT:== | ==SUBJECT:== | ||
Forwardsencldemonstrating thatallsignificant parameters ofDraftRegGuide,Steame Generator TubeIntegrity,met for14monthsofoperation, whiletoplevelcriterion remainslessthan0.05for15monthperiodofoperation. | |||
~yeslJ1 S;.LucieUnit1DocketNo,50-335L-96-273Page2Insummary, | DISTRIBUTION CODE:AOOIDCOPIESRECEIVED:LTR JENCLISIZE:+ZTITLE:ORSubmittal: | ||
GeneralDistribution NOTES:RECIPIENT IDCODE/NAME PD2-3LA.WIENSFL. | |||
COPIESLTTRENCL1111RECIPIENT IDCODE/NAME PD2-3PDCOPIESLTTRENCL11RINTERNAL: | |||
ACRSNRR/DE/EMCB NRR/DSSA/SPLB NUDOCS-ABSTRACT EXTERNAL: | |||
NOAC1~111111111NRR/DRCH/HICB NRR/DSSA/SRXB OGC/HDS3NRCPDR1111111011D0UNNOTETOALLNRIDS"RECIPIENTS: | |||
PLEASEHELPUSTOREDUCEWASTE.TOHAVEYOURNAMEORORGANIZATION REMOVEDFROMDISTRIBUTION LISTSORREDUCETHENUMBEROFCOPIESRECEIVEDBYYOUORYOURORGANIZATION, CONTACTTHEDOCUMENTCONTROLDESK(DCD)ONEXTENSION 415-2083TOTALNUMBEROFCOPIESREQUIRED: | |||
LTTR13ENCL12 FloridaPower8tLightCompany,P.O.Box128,FortPierce,FL34854-0128 October24,1996L-96-27310CFR50.4U.S.Ihluclear Regulatory Commission Attn:DocumentControlDeskWashington, D.C.20555RE:St.LucieUnit1DocketNo.50-335SteamGenerator RunTimeAnalsisforCcle14DuringaJuly3,1996,meetingwiththeNRC,FloridaPowerandLightCompany(FPL)committed toprovidetheresultsoftheSt.LucieUnit1steamgenerator runtimeanalysistotheNRCwithin90daysofthestartupfromthe1996refueling outage(SL1-14). | |||
FPLplanstooperatetheUnit1steamgenerators forfifteen(15)monthsthroughOctober23,1997.Theruntimeanalysisisaphysically basedanalysisusingtheguidancecontained inDraftRegulatory Guide(RG)1.121,GenericLetter95-05,andtheDraftRegulatory Guide,SteamGenerator TubeIntegrity. | |||
Thefifteen(15)monthoperating cyclerepresents aseven(7)monthreduction intheoriginally scheduled cycleoftwenty-two (22)months.Thisrevisedoperating cyclelengthwillpermitthesafeoperation ofthesteamgenerators untiltheearliestdatefortheinstallation ofthereplacement steamgenerators. | |||
Enclosure 1istheSt.LucieUnit1SteamGenerator RunTimeAnalysisforCycle14.Thisruntimeanalysisincludestheresponses totheNRCrequestsforadditional information datedJuly26,1996.Enclosures 2,3,and4areFPLcontractor reportswhicharereferenced inthesteamgenerator runtimeanalysis. | |||
Enclosure 2isAPTECHEngineering ServicesReport,AES96052749-1-1, datedOctober1996,AnalysisofODSCC/IGA atTubesheet andTubeSupportLocations atSt.LucieUnitl.Enclosure 3isScientific Applications International Corporation (SAIC)Report,SAIC05-5049-05-6734-500, datedSeptember 1996,SteamGenerator Degradation SpecificManagement (SGDSM)LeakageLimitCalculation forSt.LucieUnit1.Enclosure 4isABBCombustion Engineering Report,00000-OSW-16 Revision0,In-situPressureTestResultsforSt.LucieUnit1Spring1996Outage.Theenclosures demonstrate thatallofthesignificant parameters-of theDraftRegulatory Guide,SteamGenerator TubeIntegrity, havebeenmetforfourteen(14)monthsofoperation, whilethetoplevelcriterion (probability ofburst(POB)atmainsteamlinebreakconditions) remainslessthan0.05forthefifteen(15)monthperiodofoperation. | |||
Aprobabilistic safetyassessment (PSA)demonstrates thatoperation fortheadditional monthdoesnotincreasethecoredamagefrequency (CDF)intothesafetysignificant category. | |||
Theinclusion oftheEPRIprimarytosecondary leakguidelines inplantoperating procedures andincreased trainingofthelicensedoperators, asdocumented intheenclosures, providesFPL'scommitment torespondtopossibletubeleakevents.Anadditional benchmark oftheplannedcyclelengthisprovidedbytheendofCycle13in-situpressuretesting.Thistestingdemonstrated thatsteamgenerator tubeswithrepresentative worstcasedefectsmettherequirements ofDraftRG1.121r~R()gpf'ter13.9effective fullpowermonths(EFPM)ofoperation. | |||
r96i0280062 96i024PDRprrADGCK | |||
: 05000335, O'""'DR | |||
~yeslJ1 S;.LucieUnit1DocketNo,50-335L-96-273Page2Insummary,FPLconsiders thatsafeoperation oftheSt.LucieUnit1steamgenerators forfifteen(15)monthsthroughOctober23,1997,issupported bytheenclosedruntimeanalysis, theendofCycle13repairsandin-situpressuretesting,theincorporation ofmorerestrictive operational tubeleakagelimits,andtheenhancedoperatortraining. | |||
Asdiscussed attheJuly3,1996meeting,FPLispreparedtomeetwiththeNRCtodiscusstheresultsoftheanalysesoncetheNRCStaffhashadanopportunity toreviewthismaterial. | |||
VetyoursJ.A.StallVicePresident St.LuciePlantJAS/GRMEnclosures (4)cc:StewartD.Ebneter,RegionalAdministrator, RegionII,USNRCSeniorResidentInspector, USNRC,St.LuciePlant | |||
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Revision as of 14:49, 29 June 2018
| ML17229A090 | |
| Person / Time | |
|---|---|
| Site: | Saint Lucie |
| Issue date: | 10/24/1996 |
| From: | STALL J A FLORIDA POWER & LIGHT CO. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| Shared Package | |
| ML17229A091 | List: |
| References | |
| L-96-273, NUDOCS 9610280062 | |
| Download: ML17229A090 (5) | |
Text
CATEGORY1REGUL'ATINFORMATION DISTRIBUTIOtSTEM (RIDE)ACCESSION NBR:961,0280062 DOC.DATE:
96/10/24NOTARIZED:
NODOCKETgFACIL:50-335 St.LuciePlant,Unit1,FloridaPower&LightCo.05000335AUTH.NAMEAUTHORAFFILIATION STALL,"J.A.
FloridaPower6LightCo.RECIP.NAME RECIPIENT AFFILIATION DocumentControlBranch(Document ControlDesk)
SUBJECT:
Forwardsencldemonstrating thatallsignificant parameters ofDraftRegGuide,Steame Generator TubeIntegrity,met for14monthsofoperation, whiletoplevelcriterion remainslessthan0.05for15monthperiodofoperation.
DISTRIBUTION CODE:AOOIDCOPIESRECEIVED:LTR JENCLISIZE:+ZTITLE:ORSubmittal:
GeneralDistribution NOTES:RECIPIENT IDCODE/NAME PD2-3LA.WIENSFL.
COPIESLTTRENCL1111RECIPIENT IDCODE/NAME PD2-3PDCOPIESLTTRENCL11RINTERNAL:
ACRSNRR/DE/EMCB NRR/DSSA/SPLB NUDOCS-ABSTRACT EXTERNAL:
NOAC1~111111111NRR/DRCH/HICB NRR/DSSA/SRXB OGC/HDS3NRCPDR1111111011D0UNNOTETOALLNRIDS"RECIPIENTS:
PLEASEHELPUSTOREDUCEWASTE.TOHAVEYOURNAMEORORGANIZATION REMOVEDFROMDISTRIBUTION LISTSORREDUCETHENUMBEROFCOPIESRECEIVEDBYYOUORYOURORGANIZATION, CONTACTTHEDOCUMENTCONTROLDESK(DCD)ONEXTENSION 415-2083TOTALNUMBEROFCOPIESREQUIRED:
LTTR13ENCL12 FloridaPower8tLightCompany,P.O.Box128,FortPierce,FL34854-0128 October24,1996L-96-27310CFR50.4U.S.Ihluclear Regulatory Commission Attn:DocumentControlDeskWashington, D.C.20555RE:St.LucieUnit1DocketNo.50-335SteamGenerator RunTimeAnalsisforCcle14DuringaJuly3,1996,meetingwiththeNRC,FloridaPowerandLightCompany(FPL)committed toprovidetheresultsoftheSt.LucieUnit1steamgenerator runtimeanalysistotheNRCwithin90daysofthestartupfromthe1996refueling outage(SL1-14).
FPLplanstooperatetheUnit1steamgenerators forfifteen(15)monthsthroughOctober23,1997.Theruntimeanalysisisaphysically basedanalysisusingtheguidancecontained inDraftRegulatory Guide(RG)1.121,GenericLetter95-05,andtheDraftRegulatory Guide,SteamGenerator TubeIntegrity.
Thefifteen(15)monthoperating cyclerepresents aseven(7)monthreduction intheoriginally scheduled cycleoftwenty-two (22)months.Thisrevisedoperating cyclelengthwillpermitthesafeoperation ofthesteamgenerators untiltheearliestdatefortheinstallation ofthereplacement steamgenerators.
Enclosure 1istheSt.LucieUnit1SteamGenerator RunTimeAnalysisforCycle14.Thisruntimeanalysisincludestheresponses totheNRCrequestsforadditional information datedJuly26,1996.Enclosures 2,3,and4areFPLcontractor reportswhicharereferenced inthesteamgenerator runtimeanalysis.
Enclosure 2isAPTECHEngineering ServicesReport,AES96052749-1-1, datedOctober1996,AnalysisofODSCC/IGA atTubesheet andTubeSupportLocations atSt.LucieUnitl.Enclosure 3isScientific Applications International Corporation (SAIC)Report,SAIC05-5049-05-6734-500, datedSeptember 1996,SteamGenerator Degradation SpecificManagement (SGDSM)LeakageLimitCalculation forSt.LucieUnit1.Enclosure 4isABBCombustion Engineering Report,00000-OSW-16 Revision0,In-situPressureTestResultsforSt.LucieUnit1Spring1996Outage.Theenclosures demonstrate thatallofthesignificant parameters-of theDraftRegulatory Guide,SteamGenerator TubeIntegrity, havebeenmetforfourteen(14)monthsofoperation, whilethetoplevelcriterion (probability ofburst(POB)atmainsteamlinebreakconditions) remainslessthan0.05forthefifteen(15)monthperiodofoperation.
Aprobabilistic safetyassessment (PSA)demonstrates thatoperation fortheadditional monthdoesnotincreasethecoredamagefrequency (CDF)intothesafetysignificant category.
Theinclusion oftheEPRIprimarytosecondary leakguidelines inplantoperating procedures andincreased trainingofthelicensedoperators, asdocumented intheenclosures, providesFPL'scommitment torespondtopossibletubeleakevents.Anadditional benchmark oftheplannedcyclelengthisprovidedbytheendofCycle13in-situpressuretesting.Thistestingdemonstrated thatsteamgenerator tubeswithrepresentative worstcasedefectsmettherequirements ofDraftRG1.121r~R()gpf'ter13.9effective fullpowermonths(EFPM)ofoperation.
r96i0280062 96i024PDRprrADGCK
- 05000335, O'""'DR
~yeslJ1 S;.LucieUnit1DocketNo,50-335L-96-273Page2Insummary,FPLconsiders thatsafeoperation oftheSt.LucieUnit1steamgenerators forfifteen(15)monthsthroughOctober23,1997,issupported bytheenclosedruntimeanalysis, theendofCycle13repairsandin-situpressuretesting,theincorporation ofmorerestrictive operational tubeleakagelimits,andtheenhancedoperatortraining.
Asdiscussed attheJuly3,1996meeting,FPLispreparedtomeetwiththeNRCtodiscusstheresultsoftheanalysesoncetheNRCStaffhashadanopportunity toreviewthismaterial.
VetyoursJ.A.StallVicePresident St.LuciePlantJAS/GRMEnclosures (4)cc:StewartD.Ebneter,RegionalAdministrator, RegionII,USNRCSeniorResidentInspector, USNRC,St.LuciePlant
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