05000327/LER-1980-028-01, /01T-0:on 800411,main Steam Header Pressure Transmitters 1-PT-1-2B,-9A,-9B,-20A,-20B & -27B Found to Lack Environ Qualification to Substantiate long-term post-high Energy Line Break Operation.Replacement Ordered: Difference between revisions

From kanterella
Jump to navigation Jump to search
StriderTol Bot insert
 
StriderTol Bot change
 
Line 1: Line 1:
{{Adams
#REDIRECT [[05000327/LER-1980-028-01, Main Steam Header Pressure Transmitters 1-PT-1-2B,-9A,-9B,-20A,-20B & 27B Found to Lack Environ Qualification.Caused by Design Error]]
| number = ML19309F352
| issue date = 04/24/1980
| title = /01T-0:on 800411,main Steam Header Pressure Transmitters 1-PT-1-2B,-9A,-9B,-20A,-20B & -27B Found to Lack Environ Qualification to Substantiate long-term post-high Energy Line Break Operation.Replacement Ordered
| author name = Hereford J
| author affiliation = TENNESSEE VALLEY AUTHORITY
| addressee name =
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
| docket = 05000327
| license number =
| contact person =
| document report number = LER-80-028-01T, LER-80-28-1T, NUDOCS 8004290316
| package number = ML19309F351
| document type = LICENSEE EVENT REPORT (SEE ALSO AO RO), TEXT-SAFETY REPORT
| page count = 2
}}
{{LER
| Title = /01T-0:on 800411,main Steam Header Pressure Transmitters 1-PT-1-2B,-9A,-9B,-20A,-20B & -27B Found to Lack Environ Qualification to Substantiate long-term post-high Energy Line Break Operation.Replacement Ordered
| Plant =
| Reporting criterion =
| Power level =
| Mode =
| Docket = 05000327
| LER year = 1980
| LER number = 28
| LER revision = 1
| Event date =
| Report date =
| ENS =
| abstract =
}}
 
=text=
{{#Wiki_filter:.
1 C'&
8004280 NitC F ORM N G U. S. NUCLE AR RcCUL ATC AY CCY'.il5%iOf4 (7 77) 1.ICENCEE EVEfJT REPORT EXHIBIT A CC: din 0L DLCC.C: l ! l l l l.lh (PLE ASE PRINT CR TYPE ALL CEQUIREO IN70n'.' ATIC*41 [TTTlITlNISINlPlll@ul 0!O I -l 010101010 l-l0 i O f@l 4 l 11111 11 [@!! l@
u...... w t
..a.. v.. :.. -
.. u s.
...t,,,4 u
CO*4*T
,"CU g.,j@l 015 010 ! O t3 ! 2 l 7 t@t 014 11111810 !@l 01 412 l 4l 8101@
j iolii J
44 61
;;,;n t T N,*/6t e 6e 6J t v t'.T pai t de it utpGitTGAit sJ PTION AND PaCf ase! CO*.stCt:E'vCES h EVENT QESCn TTTF1i Main steam header pressure transmitters 1-PT-1-23, -9A, -9B, -20A, -203, t
g i and -27B-1.tch env' iron = ental' qualification Io s'ubstan'tiate" their required
~
10641l lone tem enernef en fn11ou4 e s hfch annve.. liep h e n n te.
l l
l 0 j 's l l ITTTl 1 I
l lots l 1 I
ITTI'l i 4s SV5f tV CAZ E CAL 51 C o*/
* v4Lvt C004 cc;t St.3;;;4 CC'/7C':t%f Coot suscCct swsccst t,s.LJ.
.l 1 IB 18 LB._J@ !,A, JG I IIN I s ! TI n1 u !@ L,TJ@ LzJ @
n n
o i
u st Cut NTial OCCt'* eta.CE mtsomt navis:ov CVt%TvtaR PE*Cmf NO.
CCQt TYFt
* O.
G,'('g n og IS !0 !
l-]
l _0 l 218 I lf_J [0 ! 1I LT.J 1,. -!
Loj
.'.?,";...
u u
.u u
u u
u u
Y s.,!*t,t k
ITG O P A T
McVe$
$3 f FC
*t 3
*/A F
b8tm i
l1JSil.!@
LZJ@
LEJ@
1010 to i a [1.j@
t;LJ@
LEJ@
lFl'il8IO!Q 3J e4 49 e4 3d 43 44 42 43 44 gy CAU51 DESCRIPTICf4 /sNO CCM EC ftVE ACTICN3 Il g l Per FSAR table 3.11-2, the expected temperature can reach 290 decrees F g
g j while the instruments are qualified for 130 degrees F operation. Replace t 1 the existing transmitters with codel capable of withstanding the accident
, 7 l ri11 environment in main steam valve rooms.
TTTTl !
I i
n
@ N EoE$ N oiscovenv ossCnieriov @
's*[A''iE[
s eov.cn or-r e s taiv:
li !*. i L Bl@ 10!0 ! 0!GI N/A I ID_JO! Notification from Engineering Des.1 i
'drisity CcLest Ast h 4+/ov :t es ACrivity @ l Locariou or cct ITTil tz_] @o os a.csc4wLZi@l N/A '
nu e.v.t
[ N/A Id II 44 43 EJ Ptn'Q*eNtt f aPo%sitt c:co.erios -
r.g s,.
~
%s....... t".m
,no. @ N/ A o r. Cm l
l01010191 i
n",
64 c J i f.*.* CF ';n D A'ca t.c.# 71 t o r Acat :i f.
14.-(
f E ' t..'re f 3 8 Lz_1T L N/A I
^
..t.s.,
I5] []L@............,,.O
,. n e. w,.,
('
N/A l [tfII!'88113 I t,a s
a,
o J. M. Hereford
,,,o,,g. 615-84 2-02 0 5 l
~
N AY(' Of PetLP,WLH L
 
s Tannessas Vallsy Authority Szquoyah Nuclear Plant LER SUPPLEMENTAL INFOP3!ATION SQRO 327/8028 Technical rpecification Involved None Reported Under Technical Specificaticn 6.9.1.12.1 Date of Occurrence: 4/11/80 Time of Occurrence: 0750 EST Identification and Description of Occurrence:
The following Westin'ghouse Class lE pressure transmitters (Foxboro EllGM-HSAE1) located outside containment in the main steam valve rooms do not have the necessary environmental qualifications to substantiate their required long-term operation following a high energy line break:
TVA Tag Nos. PT-1-23, 9A, 93, 20A, 203, and 27B (W Nos. 515, 524, 525, 534, 535, and 545).
NOTE: PT-1-12 and 23 are deleted from this report (they were included in the telecopy of this occurrence transmitted 4/14/80).
Since these instruments are located in a separate roo= and not in the valve roo=s as originally reported.
Conditions Prior to Occurrence:
Unit in Mode 5 with all fuel loaded.
Action specified in the Technical Specification Surveillance Requirements met due to inoperabic eauipment. Describe.
4 N/A Apparent Cause of Occurrence:
As shown in FSAR table 3.11-2 the expected temperature can reach greater than 290 F while the instruments are qualified for 1300 F operation.
Analysis of Occurrence:
Should a high energy line break in the =ain steam valve room, the main steam pressure transmitters possibly would not be capable of performing their intended post accident functions.
There was,no ha:ard to public health and safety.
CorrectiveAction$
Subject transmitters are to be replaced with those capable of withstanding the accident environment in main steam valve rooms. This will be completed prior to entry into Mode 3.
Failure Data:
N/A
}}
 
{{LER-Nav}}

Latest revision as of 13:36, 26 May 2025