ML061840312: Difference between revisions

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{{#Wiki_filter:Intormation inlthis recor       us inaccordance with the FreedI°Of FOIA-efl Act,        .
{{#Wiki_filter:Intormation inl this recor us in accordance with the FreedI° Of Act, efl FOIA-


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.F~egion III On November 30, staff at the Braidwood Nuclear Generating Station informed the NRC resident inspectors of higher than expected tritium levels (-58,000 picocuries per liter)
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      'S measured in on-site monitoring wells at the northern edge of the owner-controlled area.
.F~egion III
The licensee's staff attributed the higher levels of tritium to historical vacuum breaker valve leakage in the circulating water blowdown line to the Kankakee River that occurred
'S On November 30, staff at the Braidwood Nuclear Generating Station informed the NRC resident inspectors of higher than expected tritium levels (-58,000 picocuries per liter) measured in on-site monitoring wells at the northern edge of the owner-controlled area.
                                                                                                        )  I in 1998 and 2000. The licensee uses the blowdown line to perform liquid eftent               I releases to the river. Region III dispatched a senior radiation specialist to assist the resident inspector in reviewing the licensee's sampling results, evaluation, and mitigative actions. The State of Illinois was notified, and the onsite Illinois Inspector is observing the NRC's inspection.
The licensee's staff attributed the higher levels of tritium to historical vacuum breaker valve leakage in the circulating water blowdown line to the Kankakee River that occurred in 1998 and 2000. The licensee uses the blowdown line to perform liquid eftent releases to the river. Region III dispatched a senior radiation specialist to assist the resident inspector in reviewing the licensee's sampling results, evaluation, and mitigative actions. The State of Illinois was notified, and the onsite Illinois Inspector is observing the NRC's inspection.
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Latest revision as of 08:11, 15 January 2025

EDO Daily Notes for December 2, 2005 and One-Week Look Ahead
ML061840312
Person / Time
Site: Braidwood  
Issue date: 12/02/2005
From:
NRC/EDO
To:
References
FOIA/PA-2006-0115
Download: ML061840312 (2)


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Intormation inl this recor us in accordance with the FreedI° Of Act, efl FOIA-

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.F~egion III

'S On November 30, staff at the Braidwood Nuclear Generating Station informed the NRC resident inspectors of higher than expected tritium levels (-58,000 picocuries per liter) measured in on-site monitoring wells at the northern edge of the owner-controlled area.

The licensee's staff attributed the higher levels of tritium to historical vacuum breaker valve leakage in the circulating water blowdown line to the Kankakee River that occurred in 1998 and 2000. The licensee uses the blowdown line to perform liquid eftent releases to the river. Region III dispatched a senior radiation specialist to assist the resident inspector in reviewing the licensee's sampling results, evaluation, and mitigative actions. The State of Illinois was notified, and the onsite Illinois Inspector is observing the NRC's inspection.

I INTE RNAL ONLY - NOT R PUBLIC Dl 3