05000261/LER-2010-001-01, Regarding Emergency Diesel Generator Inoperable in Excess of Technical Specifications Allowed Completion Time: Difference between revisions

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#REDIRECT [[05000261/LER-2010-001, For H.B. Robinson, Unit 2, Regarding Emergency Diesel Generator Inoperable in Excess of Technical Specifications Completion Time Due to Output Breaker Failure]]
| number = ML101590222
| issue date = 06/01/2010
| title = Regarding Emergency Diesel Generator Inoperable in Excess of Technical Specifications Allowed Completion Time
| author name = Saunders W
| author affiliation = Progress Energy Carolinas, Inc
| addressee name =
| addressee affiliation = NRC/Document Control Desk, NRC/NRR
| docket = 05000261
| license number = DPR-023
| contact person =
| case reference number = RNP-RA/10-0049
| document report number = LER 10-001-01
| document type = Letter, Licensee Event Report (LER)
| page count = 7
}}
{{LER
| Title = Regarding Emergency Diesel Generator Inoperable in Excess of Technical Specifications Allowed Completion Time
| Plant =
| Reporting criterion = 10 CFR 50.73(a)(2)(i), 10 CFR 50.73(a)(2)(vii), 10 CFR 50.73(a)(2)(ii)(A), 10 CFR 50.73(a)(2)(viii)(A), 10 CFR 50.73(a)(2)(ii)(B), 10 CFR 50.73(a)(2)(viii)(B), 10 CFR 50.73(a)(2)(iii), 10 CFR 50.73(a)(2)(ix)(A), 10 CFR 50.73(a)(2)(iv)(A), 10 CFR 50.73(a)(2)(x), 10 CFR 50.73(a)(2)(v)(A), 10 CFR 50.73(a)(2)(v)(B), 10 CFR 50.73(a)(2)(i)(A), 10 CFR 50.73(a)(2)(v), 10 CFR 50.73(a)(2)(i)(B)
| Power level =
| Mode =
| Docket = 05000261
| LER year = 2010
| LER number = 1
| LER revision = 1
| Event date =
| Report date =
| ENS =
| abstract =
}}
 
=text=
{{#Wiki_filter:10 CFR 50.73 9 Progress Energy Serial: RNP-RA/10-0049 JUN 0 1 2010 Attn: Document Control Desk United States Nuclear Regulatory Commission Washington, DC 20555-0001 H. B. ROBINSON STEAM ELECTRIC PLANT, UNIT NO. 2 DOCKET NO. 50-261/LICENSE NO. DPR-23 LICENSEE EVENT REPORT NO. 2010-001-01 EMERGENCY DIESEL GENERATOR INOPERABLE IN EXCESS OF TECHNICAL SPECIFICATIONS COMPLETION TIME DUE TO OUTPUT BREAKER FAILURE Ladies and Gentlemen:
The attached Licensee Event Report (LER) is provided to correct editorial errors in the labels for blocks 5 and 6 and reflects the revised completion date for Refueling Outage 26. LER 2010-001-00 was submitted to the Nuclear Regulatory Commission on April 22, 2010. Should you have any questions regarding this matter, please contact Mr. C. A. Castell at (843) 857-1626.
Sincerely, W. Scott Saunders Plant General Manager H. B. Robinson Steam Electric Plant, Unit No. 2 WSS/ahv Attachment c:
L. A. Reyes, NRC, Region II T. J. Orf, NRC, NRR NRC Resident Inspector Progress Energy Carolinas, Inc.
Robinson NuJLclear Plant 3581 West Entrance Road Hartsville, SC 29550 A912 -
 
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES 08131/2010 (9-2007)
Estimated burden per response to comply with this mandatory collection request: 80 hours. Reported lessons learned are incorporated into the licensing process and LICENSEE EVENT REPORT (LER) fed back to industry.
Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, (See reverse for required number of Washington. DC 20555-0001, or by internet e-mail to infocollects@nrc.gov, and to digits/characters for each block) the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to I respond to, the information collection.
: 3. PAGE H. B. Robinson Steam Electric Plant, Unit No. 2 05000261 1 OF 6
: 4. TITLE Emergency Diesel Generator Inoperable in Excess of Technical Specifications Allowed Completion Time
: 5. EVENT DATE
: 6. LER NUMBER
: 7. REPORT DATE
: 8. OTHER FACILITIES INVOLVED FACILITY NAME DOCKET NUMBER MONTH DAY YEAR YEAR SEQUENTIAL REV NUMBER NO MONTH DAY YEAR 05000 FACILITY NAME DOCKET NUMBER 02 22 2010 2010-001 01 06 10 2010 1
05000
: 11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check all that apply)
: 9. OPERATING MODE 11 20.2201(b)
El 20.2203(a)(3)(i)
[E 50.73(a)(2)(i)(C)
El 50.73(a)(2)(vii)
E]
20.2201(d)
El 20.2203(a)(3)(ii)
El 50.73(a)(2)(ii)(A)
E] 50.73(a)(2)(viii)(A) 1 El 20.2203(a)(1)
El 20.2203(a)(4)
El 50.73(a)(2)(ii)(B)
[I 50.73(a)(2)(viii)(B)
El 20.2203(a)(2)(i)
El 50.36(c)(1)(i)(A)
[1 50.73(a)(2)(iii)
El 50.73(a)(2)(ix)(A)
: 10. POWER LEVEL El 20.2203(a)(2)(ii)
El 50.36(c)(1)(ii)(A)
El 50.73(a)(2)(iv)(A)
El 50.73(a)(2)(x)
C]
20.2203(a)(2)(iii)
El 50.36(c)(2)
El 50.73(a)(2)(v)(A) 0i 73.71 (a)(4) 99%
El 20.2203(a)(2)(iv)
El 50.46(a)(3)(ii)
El 50.73(a)(2)(v)(B)
E] 73.71(a)(5)
El 20.2203(a)(2)(v)
El 50.73(a)(2)(i)(A)
El 50.73(a)(2)(v)(C)
El OTHER Specify in Abstract below or
_ El 20.2203(a)(2)(vi) 0 50.73(a)(2)(i)(B) 0 50.73(a)(2)(v)(D) in II.
 
==CAUSE OF EVENT==
The cause of the event was determined to be a vendor workmanship error, which allowed use of a defective Shunt Trip Attachment (STA) movable core in the breaker.
The STA is a solenoid-operated device designed for remote breaker electrical tripping.
The shunt trip is designed for intermittent service and the circuit must be opened by an auxiliary switch contact.
The STA consists of a metal frame, coil, moving and stationary core, and trip lever.
A trip signal to the STA energizes a coil on the STA, thereby causing its moving core to be pulled into the stationary core. The moving core can either rotate a trip lever to lift the trip bar or pull a trip paddle on the trip shaft, thereby rotating the trip shaft counter-clockwise (looking down the trip shaft on a DB-75/DB-100 breaker from the right side) to trip the breaker.
As the breaker trips open, its auxiliary switch contact, in series with the STA coil, opens and de-energizes the coil.
With the coil deenergized, the STA return.spring pushes the moving core out of the stationary core to the reset position.
During the investigation HBRSEP, Unit No. 2, personnel and Westinghouse personnel disassembled the defective STA in an attempt to isolate the binding issue.
The STA internal assembly was removed from the core as one complete unit.
The internal STA assembly consists of the movable core, the stationary core, brass sleeve, guide pin, return spring, and anti-freeze washer.
The internal STA assembly was dissembled into its individual components and each component was inspected and verified against Westinghouse design drawing requirements.
The inspection of the movable core disclosed that the leading edge of the core was not chamfered to the required 1/32 inch.
The leading edge was specified by Westinghouse manufacturing prints to have an outside diameter of 1.485 inches to 1.490 inches.
On the leading edge of the core the diameter measured at a maximum of 1.494 inches.
The moving core slides within the brass sleeve on the STA.
The brass sleeve inside diameter was to be machined to a minimum of 1.492 inches and a maximum of 1.500 inches.
These values are acceptable per the Westinghouse design print for the STA.
The investigation revealed that internal binding of the movable STA occurred when the 1.492 inches inside diameter area of the brass sleeve aligned with the 1.494 inches outside diameter area of the movable core.
When the two areas were not aligned the STA would operate properly; however, once the movable core rotated in such a way that the areas were aligned, then binding occurred and the STA would not operate as designed.
This explains why the EDG 'B' output breaker, 52/27B, was able to successfully cycle 12 times over a period of 10 months because the internal binding condition of the STA is intermittent and had not occurred.
This vendor workmanship error resulted in the internal binding condition that prevented the STA from releasing the trip bar, resulting in the trip bar remaining in the "trip condition" and preventing the output breaker from closing.
 
III.
 
==ANALYSIS OF EVENT==
The conditions described in this Licensee Event Report are reportable in accordance with 10 CFR 50.73(a)(2)(i)(B), "Any operation or condition which was prohibited by plant's Technical Specifications," and 10 CFR 50.73(a)(2)(v)(D),
"Any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident."
This event was investigated using the HBRSEP, Unit No. 2, Corrective Action Program (CAP) and documented in Significant Adverse Nuclear Condition Report 382604.
This reportable event and the associated significant adverse condition investigation was reviewed by the Plant Nuclear Safety Committee on April 7, 2010.
The investigation for the inoperability of EDG 'B' due to breaker 52/27B failure to close determined that the STA contained internal binding that prevented the STA from releasing the trip bar, preventing the breaker from closing.
Additionally, the investigation determined that EDG 'B' was not able to fulfill its safety related function from January 28, 2010, to February 24, 2010.
January 28, 2010, was the date breaker 52/27B was last successfully operated and the most likely time that the internal alignment of the STA caused it to become bound.
Operations personnel declared the EDG 'B' operable February 24, 2010, after completion of repairs and testing.
This resulted in approximately 27 days of inoperability and the TS Required Actions and Completion Times not being met.
During this time period, EDG 'A' was declared inoperable for 6 hours and 53 minutes for scheduled maintenance.
The combined inoperability of EDG 'A' and 'B' could have prevented the fulfillment of a safety function.
During the investigation, an extent of condition was performed.
Fourteen circuit breakers were identified as DB-75 and DB-100 currently in service and one spare DB-100 breaker.
Of those fourteen breakers, six breakers are safety-related.
The six safety-related breakers are 52/17B (EDG 'A' output breaker to Emergency Bus 1 [El]), 52/18B (Station Service Transformer 2F to El), 52/22B (El supply to Safety Injection [SI] Pump 'B'), 52/27B (EDG 'B' output breaker to Emergency Bus 2 [E2]), 52/28B (Station Service Transformer 2G to E2), and 52/29B (E2 supply to SI Pump 'B').
While the SI Pump 'B' is not in service, breakers 52/22B and 52/29B are not required for operability.
Caution tags are in place on 52/22B and 52/29B to verify the STA is in the correct position, in the event the breakers are closed.
Breakers 52/18B and 52/28B are currently in the closed position.
These breakers do not have a safety-related function to close.
 
Scenarios were evaluated to consider a Loss of Power Event.
Immediately following a loss of normal offsite electrical AC power, the control room operators would enter procedure PATH-i.
PATH-1 requires the verification of either El and/or E2 energized.
As previously stated, even if the EDG 'B' output breaker 52/27B failed to close, EDG 'A' would have been capable of providing power to the necessary equipment, except during the approximately 7 hour period on February 8, 2010, when EDG 'A' was also inoperable.
If it is assumed that EDG 'A' had failed to operate, PATH-1 directs the start of End Path Procedure (EPP),
EPP-1, "Loss of All AC Power."
EPP-l directs the control room to dispatch an operator to start and load the Dedicated Shutdown Diesel Generator (DSDG) to restore AC power.
If the DSDG operates, sufficient equipment can be operated to safely shutdown the plant.
EPP-1 then directs restoration of AC power to energize El and E2.
Assuming EDG 'A,'
EDG 'B,'
and DSDG fail to operate, the control room would request assistance from Maintenance in restoring AC power.
As a result of steps performed in EPP-i, it would be determined that 52/27B failed to close, and maintenance could use the following repair options:
: 1. Perform a localized inspection of the 52/27B, EDG 'B' output breaker.
This inspection would reveal that the STA has positioned the trip bar in such a way which will not allow the breaker to close.
Maintenance would then manually manipulate the trip bar allowing the breaker to close.
The estimated time of completion for this evolution is approximately one hour.
: 2.
EDG 'B' output breaker 52/27B could be replaced with EDG 'A' output breaker 52/17B.
The estimated time of completion for this evolution is approximately one hour.
: 3.
Manual closure of 52/27B in accordance with EPP-22, "Energizing Plant Equipment Using Dedicated Shutdown Diesel Generator," Attachment 2.
The estimated time of completion for this evolution is approximately two hours.
: 4. Retrieval of spare DB-IO0 breaker from stock and installing the spare breaker into the 52/27B cubicle.
The estimated time of completion for this evolution is approximately four hours.
IV.
 
==CORRECTIVE ACTIONS==
Completed Corrective Actions:
* EDG output breaker, 52/27B, was replaced including a new STA assembly.
* Instructions were added to work requests for EDG 'A' and EDG 'B' to perform a visual inspection of the STA to ensure proper orientation following each operation.
* Work requests were initiated to inspect STA assemblies on the 'A' train during Refueling Outage 26, currently scheduled to end on June 25, 2010.
 
==Planned Corrective Actions==
0 Applicable EDG operating procedures are scheduled to be revised by July 10, 2010, to include instructions to visually inspect DB-IO circuit breakers for the correct STA orientation after completion of the test and with the breaker in the open position.
* Procedure, PM-402, "Inspection and Testing of Circuit Breakers for 480 Volt Bus El,"
is scheduled to be revised by.July 10, 2010, to include instructions to physically inspect the internal binding of the STA on DB-75 and DB-100 circuit breakers.
* Procedure, PM-163, "Inspection and Testing of Circuit Breakers for 480 Volt Bus E2,"
is scheduled to be revised by July 10, 2010, to include instructions to physically inspect for internal binding of the STA on DB-75 and DB-100 circuit breakers.
* Procedure, SPP-032, "Breaker Receipt Inspection for New and Refurbished Breakers," is scheduled to be revised by July 10, 2010, to include instructions to physically inspect for internal binding of the STA on DB-75 and DB-100 circuit breakers.
 
==V. ADDITIONAL INFORMATION==
Previous Similar Events:
Licensee Event Reports (LERs) for HBRSEP, Unit No. 2, were reviewed from the past 10 years.
The following event was identified as being similar to the event described in this LER:
LER 2009-001-00, Emergency Diesel Generator Inoperable in Excess of Technical Specifications Allowed Completion Time.
This event was a failure to meet the required actions associated with TS LCO 3.8.1, "AC Sources - Operating," due to the cotter pin used to retain the relay's mechanical lift linkage had rotated to a position that prevented complete return of the lift linkage to its normal position.
The lift linkage maintained the control relay trip pin engaged and maintained the control circuits open preventing the breaker from closing.
This event is relatable to the event described in LER 2010-001-00.
Both events were attributed to vendor error.
}}
 
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Latest revision as of 05:29, 14 January 2025