05000368/LER-1979-067-04, Auxiliary Bldg Radwaste Area Radiation Monitor 2RE-8542 Sample Pump Found to Have Broken Pump/Motor Coupling.Cause Unstated.Qualified Coupling Replacements Installed: Difference between revisions

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{{Adams
#REDIRECT [[05000368/LER-1979-067-04, /04L-0:on 790808,auxiliary Bldg Radwaste Area Radiation Monitor 2RE-E542 Sample Pump Found W/Broken Coupling.Cause Not Stated.Plastic Coupling Replaced W/Metal Coupling.Appropriate Grab Samples Taken]]
| number = ML19354C383
| issue date = 11/20/1980
| title = Auxiliary Bldg Radwaste Area Radiation Monitor 2RE-8542 Sample Pump Found to Have Broken Pump/Motor Coupling.Cause Unstated.Qualified Coupling Replacements Installed
| author name = Shively C
| author affiliation = ARKANSAS POWER & LIGHT CO.
| addressee name =
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
| docket = 05000368
| license number =
| contact person =
| document report number = LER-79-067-04X, LER-79-67-4X, NUDOCS 8012010340
| package number = ML19345B443
| document type = LICENSEE EVENT REPORT (SEE ALSO AO RO), TEXT-SAFETY REPORT
| page count = 1
}}
{{LER
| Title = Auxiliary Bldg Radwaste Area Radiation Monitor 2RE-8542 Sample Pump Found to Have Broken Pump/Motor Coupling.Cause Unstated.Qualified Coupling Replacements Installed
| Plant =
| Reporting criterion =
| Power level =
| Mode =
| Docket = 05000368
| LER year = 1979
| LER number = 67
| LER revision = 4
| Event date =
| Report date =
| ENS =
| abstract =
}}
 
=text=
{{#Wiki_filter:-
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[
REVISED REPORT - PREVIOUS REPORT DATE 9/5/79 NRC FrRep 3r4 U. S. NUCI E AR REGUL ATORY COMMISSION (7 77)
LICENSEE EVENT REPORT EXHIBIT A CONTROL SLOCs0 l l 1 l l l lh (PLE ASE PRINT OR T YPE ALL REQUIRED INFORMATIONI l AlR l Ai Nl012 lg 0l01 -l0 l0 l 0l O 0l-l0]O lg l1 l 1l1 l 1lg ; jg i
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H EVENT D ATE I4 iS M F POM F D A T E 80 EVENT DESC'41PT10N AND PROBASLE CONSEQUENCES h IT1rl I Durina Mode 1 operation, the Auxiliary Buildina Radwaste Area Radiation I t o l 21 LJ1onitor. 2RE-8542. samole oumo was_found to have a broken oumo/ motor i
G rrl Lcogling.
Gasesus releases which utilize the sub.iect monitor were I
in isi i manually sampled and analyzed.
Activity remained at less than minimum l
io nil detectable.
Similar to LER 50-368/79-057.
Reportable per E.T.S. 5.6.2.b>
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CAUSE OESCR PT.,)N AND CORRECHVE ACTIONS h I Annrnnriato grab samnloc worn taken while tho mnni tor was nut of servirn_1 i o t i li l I onro nor shif t as renuired by F_T.9.
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Fng'nopring evalhatinn I
lii2i l identified aualified couolino reolacements for tha ol.astic tyoe couclino 1 i'121 Llo uoorade the anolication for a more reliable coeration.
All affected I I Radiation Monitors were modi fied.
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,,o Chris N. Shively MU%bHB NAME OF PAEPARER
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}}
 
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Latest revision as of 00:00, 5 January 2025