05000324/LER-1980-026-03, During HPCI Steamline High Differential Pressure Channel Calibr Check,Main Steamline Instrument 2E41-DPIS-N004 Found Out of Tolerance. Caused by Instrument Drift.Instrument Recalibr: Difference between revisions

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{{Adams
#REDIRECT [[05000324/LER-1980-026-03, /03L-0:on 800225,while Performing HPCI Steamline High Differential Pressure Channel Calibr and Functional Check,Main Streamline High Flow Instrument 2E41-DPIS-NOO4 Found Out of Tolerance.Caused by Setpoint Drift]]
| number = ML19323F339
| issue date = 05/12/1980
| title = During HPCI Steamline High Differential Pressure Channel Calibr Check,Main Steamline Instrument 2E41-DPIS-N004 Found Out of Tolerance. Caused by Instrument Drift.Instrument Recalibr
| author name = Tollison A
| author affiliation = CAROLINA POWER & LIGHT CO.
| addressee name =
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
| docket = 05000324
| license number =
| contact person =
| document report number = LER-80-026-03L, LER-80-26-3L, NUDOCS 8005280795
| package number = ML19323F335
| document type = LICENSEE EVENT REPORT (SEE ALSO AO RO), TEXT-SAFETY REPORT
| page count = 2
}}
{{LER
| Title = During HPCI Steamline High Differential Pressure Channel Calibr Check,Main Steamline Instrument 2E41-DPIS-N004 Found Out of Tolerance. Caused by Instrument Drift.Instrument Recalibr
| Plant =
| Reporting criterion =
| Power level =
| Mode =
| Docket = 05000324
| LER year = 1980
| LER number = 26
| LER revision = 3
| Event date =
| Report date =
| ENS =
| abstract =
}}
 
=text=
{{#Wiki_filter:NRC FOIM 366 U. S. NUCLE AR REGULATORY COMMISSION UPDATE REPORT:
PREVIOUS LICENSEE EVENT REPORT REPORT DATE 3-13-80 CONrROL etOC(: l l
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(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
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7 8 9 LICENSEE COGE 14 LICENSE NuvtsEH 26 26 LICENSE TYPE Jo 5 7 CA T $8 CON'T 10IiI 5ERCE I b hl 0 l 5 l 0 l-l 0 l 3 l 2 l4 @l 0 l 2 l 2 l 5 l 8 l 0 l@l 0l S l 1l 21 8 l 0 l 7
8 60 si DOCKET NUYSER 6a 63 EVENT DATE 14 75 REPORT QATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h ql While performing PT 2.1.lPC, HPCI Steamline High Differential Pressure Channel Cali-l bration and Functional Check, main steamline high flow instrument 2E41-DPIS-N004 was l gl gl found out of tolerance. The value found was 225 inches of water and the reportable l
g ; limit is greater than 219 inches of water (300% flow).
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'9 20 SEQUENTIAL OCCURRENCE RE# CAT REVISION LER Ro EVENT YE AR R EPORT No.
CCCE TYPE No.
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40 44 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS lilo l l The out of tolerance setpoint was attributed to instrument drift. The instrument was-l l
[i j i j j recalibrated and returned to service.
This is considered an isolated event and no l
,,,,,l further action is required. Although this is an isolated event on this instrument, i
it is scheduled to be replaced with an analog transmitter during a future outage.
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8 9 80 oT*ER STATUS @$iSEoNOY oiSCoVERY OESCRIPTION @
'^$IS" sPonER Sr Q [Ej@ l0l9l5l@l NAl l B l@] Periodic Test l
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A$TiviTY Co'0 TENT AuousTcF ACTIVITY @ l LOCATION CF RELE ASE f7T61 W @o or Rett *SElzl@l attEASE NA l
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7 8 9 10 11 44 45 80 PERSONNEL EupO5URES 1010 l o l@l z i@ DESCRIPTION NUMBER TYPE l
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NuunER l i l - l l 0 l 0 l 0 l@l NA l
7 8 9 11 12 80 LOSS OF CH DA*.' AGE to F ACILtTY T4PE DESCns e tiCN I W lzl@l NA l
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LER ATTACHMENT - RO NO. 2-80-26 Facility: BSEP Unit No. 2 Event Date: February 25, 1980 During the 1980 Unit No. 2 refueling outage, several instruments were scheduled to be replaced with more reliable analog-type instrumentation.
Prior to the refueling outage, Carolina Power & Light Company contacted other utilities which had already made this conversion to learn of any problems they experienced.
From these conversations, it was decided that a thorough bench-testing program should be implemented before actual installation.
During this bench testing, several problems were ider.tified which we feel make these Lastruments unsuit-able for operation at this time. Upon completion of correcting these problems and thorough testing, this new analog instrumentation will be installed.
6 A
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}}
 
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Latest revision as of 06:01, 2 January 2025