05000336/LER-1980-011-03, Following Two Plant Trips & Shutdown,Daddle Clamp Bolts for Two Hangars Were Found Broken.Both Hangers Are Hydraulic Snubbers.Failures Caused by Combination of Fatigue & High Impact Loading: Difference between revisions

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{{Adams
#REDIRECT [[05000336/LER-1980-011-03, /03L-0:on 800313,following Full Power Plant Trip, Two Broken Saddle Clamp Bolts Were Found on Hydraulic Snubber Hanger 490008 on Ms Lead to HP Turbine.Caused by Fatigue Cracking Due to High Vibration & Shear on Trips]]
| number = ML19318C420
| issue date = 06/24/1980
| title = Following Two Plant Trips & Shutdown,Daddle Clamp Bolts for Two Hangars Were Found Broken.Both Hangers Are Hydraulic Snubbers.Failures Caused by Combination of Fatigue & High Impact Loading
| author name = Clement C
| author affiliation = NORTHEAST NUCLEAR ENERGY CO.
| addressee name =
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
| docket = 05000336
| license number =
| contact person =
| document report number = LER-80-011-03L, LER-80-11-3L, NUDOCS 8007010450
| package number = ML19318C413
| document type = LICENSEE EVENT REPORT (SEE ALSO AO RO), TEXT-SAFETY REPORT
| page count = 2
}}
{{LER
| Title = Following Two Plant Trips & Shutdown,Daddle Clamp Bolts for Two Hangars Were Found Broken.Both Hangers Are Hydraulic Snubbers.Failures Caused by Combination of Fatigue & High Impact Loading
| Plant =
| Reporting criterion =
| Power level =
| Mode =
| Docket = 05000336
| LER year = 1980
| LER number = 11
| LER revision = 3
| Event date =
| Report date =
| ENS =
| abstract =
}}
 
=text=
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s 60 61 OOCKET NUMBE9 68 69 EVE NT DATE 74 75 REPORT OATE 80 3
EVEN1 oESCRIPTioN ANo PRoBABt.E CoNSEQUENCCs Following a full power plant trip 13/80), 2 broken saddle clamp bolts l
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Following a se.cond trip (3/22/80), an additional p-
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Following a plant shutdown g
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Both hangers j
EI are hydraulic snubbers on the 28 inch steam leads downstream of the turbine control val ves. The' unit complied with Technical Specification 3.7.8.1 in each case.
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36 37 40 41 42 43 44 47 33 CAUSE oESCRIPTION ANo CORRECTIVE ACTIONS All failures were a combination of fat.igue and high impact loading.
The l
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stop valves were replaced with high strength bolts for high temperature ' service i,
( ASME A-193i Grade B7). The improved fatigue characteristics of this low-alloy p;-) l steel should prevent a recurrence.
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ATTACHMENT LER 80-11/3L-2 Millstone Unit 0 4
1 Docket No. 50-33c 1
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==EVENT DESCRIPTION==
1 During power ascension on 3/13/80 following a full power plant trip, two broken pipe saddle clamp bolts were found on hydraulic snubber hanger 490008. This hanger is located on a main steam lead prior to the HP turbine. The plant was at 30% power and the power ascension was halted until the broken bolts (1-1/2" UNF capscrews) were replaced. All other hangers on the HP turbine steam leads were inspected satisfactorily.
Following another full power trip, with the plant at 99% powe.r on 3/22/80, a broken saddle clamp bolt was found on hydraulic snubber hanger 490002.
The bolt (1-3/4" UNC machine bolt) was replaced and inspection revealed no other broken bolts on similar hangers. Both bolts were carbon steel.
Following a plant shutdown, including a turbine trip, on 5/08/80 the second saddle clamp bolt on hydraulic snubber hanger 490002 was found broken. At this time the carbon steel bolts on all similar saddle clamps were replaced with "1cw alloy steel bolting material for high temperature service" (ASME A-193, Grade 87).
These events resulted in declaring hangers 490008 and 490002 inoperable and the plant was operated in accordance with Technical Specification Action Statement 3.7.8.1 in each case.
CAUSE DESCRIPTION The bolt failures were caused by fatigue of the low carbon steel material.
In each case, the final failure was a result of the impact loading of the turbine stop and control valves tripping.
All saddle clamp bolts on similar hangers restraining the steam leads downstream of the turbine stop valves were replaced. The replacement bolting is low alloy steel bolting for high temperature service. (ASME A-193, Grade B7). The improved fatigue characteristics of this material should prevent recurrence.
There are no safety implications from these events in that these pipe supports are provided for a non-safety related purpose.
The or'iginal hydraulic snubber Technical Specification submittal included all snubbers in the plant. A change is pending to include only safety-related snubbers.
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Latest revision as of 03:06, 2 January 2025