05000313/LER-1980-013-03, High Pressure Injection (HPI) Was Manually Initiated & CV-1227 (HPI Valve,Loop B) Failed to Open on Demand.Caused by Stuck Manual Engaging Lever.Personnel Freed Lever: Difference between revisions

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{{Adams
#REDIRECT [[05000313/LER-1980-013-03, /03L-0:on 800407,during Reactor Trip of Offsite Power,High Pressure Injection Was Manually Initiated & CV-1227 High Pressure Injection Valve,Loop B Failed to Open on Demand.Caused by Stuck Engaging Lever]]
| number = ML20010F939
| issue date = 08/13/1981
| title = High Pressure Injection (HPI) Was Manually Initiated & CV-1227 (HPI Valve,Loop B) Failed to Open on Demand.Caused by Stuck Manual Engaging Lever.Personnel Freed Lever
| author name = Shively C
| author affiliation = ARKANSAS POWER & LIGHT CO.
| addressee name =
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
| docket = 05000313
| license number =
| contact person =
| document report number = LER-80-013-03X, LER-80-13-3X, NUDOCS 8109150133
| package number = ML20010F935
| document type = LICENSEE EVENT REPORT (SEE ALSO AO RO), TEXT-SAFETY REPORT
| page count = 1
}}
{{LER
| Title = High Pressure Injection (HPI) Was Manually Initiated & CV-1227 (HPI Valve,Loop B) Failed to Open on Demand.Caused by Stuck Manual Engaging Lever.Personnel Freed Lever
| Plant =
| Reporting criterion =
| Power level =
| Mode =
| Docket = 05000313
| LER year = 1980
| LER number = 13
| LER revision = 3
| Event date =
| Report date =
| ENS =
| abstract =
}}
 
=text=
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REVISED REPORT - PREVIOUS REPORT DATE 5/5/80 NRC FORM y,6 U. 5. NUCLE AR REGULATORY COMMISSsOes (777)
LICENSEE EVENT REPORT EXHIBIT A CONTROL BLOCK: l l l l l l lh (PLE ASE PRINT OR TYPE ALL REQUIRED INFORMATIOM i
6 l AlR l Al Nl O l 1 Ig[ 0 l0 l -l0 l0 l 0l 0l 0 l-l 0 l0 lgl4 l l1l1l1lgl l lg o i 7
e 9 L*CENstE Co0E I4 h
uCENst NvMsEn 26 26 ucEN>E e vrE Jo ti CAT se CCad*T "l,u% [L_J@LO I s p 10 i 0 is i 113 i@i0 i 410 17 i 810 l@l0 i 811 I a l 811 l@
pS 60 68 DOCK ET Nuuggn to 69 EVENT DATE 74 iS HEPoHfDATE 80 ROB AGLE CONSEQUENCES Oio EVENT DESCRIP flON AND rJl During a reactor trip on loss of offsite power Hiah Pressare In.iection i e i was manually initiated and CV-1227 (HPI Valve, Loop B) failed to open qn_J o. i demand.
HPI valves CV-1228, CV-1219, and CV-1220 +:are available and usedi gto maintain RCS pressure and inventory. There have been no similar I
o s o. i occurrences.
Reportable per T.S.
6.12.3.2.b.
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3J 34 35 36 JJ 40 41 42 43 44 op CAUSE DESCR.PTION AND CORRECflVE ACTIONS 27 l The/ manual enoaoina lever was found / stuck in the manual enaaaed Dosition. !
s o i This type valve operator is designed to automatically disengage the valvet 1 operator from the manual enoaaed aosition when operated electrically.
I i 2 g l Maintenance personnel investigated the failure & [ freed the manual enaaqine Ilever. The valve was operated electrically several times with no malfunctions.
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8 9 10 64 r9 no NAME OF PREPARER PHON E:
8109150133 810813 PDR ADOCK 05000313 S
PDR
}}
 
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