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| {{Adams
| | #REDIRECT [[05000333/LER-1980-067-03, /03L-0:on 800805,while Conducting Instrument Surveillance Check,Steam Line Low Pressure Switches Found Set Higher than 100 Psig Limit.Caused by Instrument Drift. Instruments Calibr & Returned to Svc]] |
| | number = ML19331D406
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| | issue date = 08/29/1980
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| | title = LER 80-067/03L-0:on 800805,while Conducting Instrument Surveillance Check,Steam Line Low Pressure Switches Found Set Higher than 100 Psig Limit.Caused by Instrument Drift. Instruments Calibr & Returned to Svc
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| | author name = Childs W
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| | author affiliation = POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
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| | addressee name =
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| | addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
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| | docket = 05000333
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| | license number =
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| | contact person =
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| | document report number = LER-80-067-03L, LER-80-67-3L, NUDOCS 8009020359
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| | package number = ML19331D403
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| | document type = LICENSEE EVENT REPORT (SEE ALSO AO,RO), TEXT-SAFETY REPORT
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| | page count = 1
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| }}
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| | |
| =Text=
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| u a .iutan %.,- u n i _. .n m i LICENSEE EVENT REPORT (PLEASE PRINT OR TYFE ALL REQUIRED INFORMATION; CONTROL BLOCK: l l l l l l lh ,
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| EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h l o 121 l During normal shutdown, while conducting Instrument Surveilinnco Prncodiira 1: Tgp 19 I
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| [ol3l l and 12-1, HPCI and RCIC steam line low pressure switches 23-PS-68A and 13-PS-87R I 10141 I were found set 9.5 and 12.0 PSIC higher than the 100 PSIC limit of TR Tnbla 19' I
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| , io;3l l Redundant switches (6 total) were satisfactory preventing any loss of function. I l o is l l Reactor was shutdown and hazard was not significant. I I
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| 42 lNl@ lBl0l6l9lQ 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h lilo l l Cause is Instrument drift. Both instruments calibrated and returned to service I
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| [i [i j l in operable status later on the same day. No additional action is recuired. I I
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| J I n 171 1 I
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| % POWER CTHER STATUS DISCO RY DISCOVERY CESCRIPTION ST S NA l l i I 5 I [.C j@ l 0l 0 l 0l@l l lBl@l Surveillance ACTIVtTY CO TENT LOCATION OF RELEASE RELEASED OF RELE ASE AMOUNT CF ACTIVITY l l Ma l Ii le 8I 3L2J @ L2]@l 7 10 11 NA 44 45 80 PERSONNEL EXPCSUR(S NUMB E R l
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| l i l 7 l l O l 0 l O lhl Zl TYPE @l NA DESCRIPTION '
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| PERSONNd'iNJiES NeveER C ESCRIPTION l
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| li la 8l 101 7 9 O l 0 lhl12 11 NA 80 LOSS OF OR CAVAGE TO FACILITY TYPE DEM'iPTION l
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| l i l 9 l [,Z_j@l NA 80 7 8 9 10 PUBLICITY NRC USE CNLY DESCRIPTION I!!IllIIllll60{al$
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