05000321/LER-1981-016-03, During Review of Data Sheets for Refueling/Torus Mod Outage Determined That Valves Were Leaking.Caused by Debris &/Or Dirt on Valve Seats. Valves Lapped & Reseated & Successfully Retested: Difference between revisions

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{{Adams
#REDIRECT [[05000321/LER-1981-016-03, /03L-0:on 810306,review of Data Sheets from 810304 LLRT of Inboard MSIVs B21-F022A,B & C Determined That Valves Were Leaking in Excess of Tech Spec.Cause Unknown. Investigation Underway.Valves Will Be Repaired & Retested]]
| number = ML20010G320
| issue date = 09/03/1981
| title = During Review of Data Sheets for Refueling/Torus Mod Outage Determined That Valves Were Leaking.Caused by Debris &/Or Dirt on Valve Seats. Valves Lapped & Reseated & Successfully Retested
| author name = Coggin C
| author affiliation = GEORGIA POWER CO.
| addressee name =
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
| docket = 05000321
| license number =
| contact person =
| document report number = LER-81-016-03X, LER-81-16-3X, NUDOCS 8109150586
| package number = ML20010G310
| document type = LICENSEE EVENT REPORT (SEE ALSO AO RO), TEXT-SAFETY REPORT
| page count = 2
}}
{{LER
| Title = During Review of Data Sheets for Refueling/Torus Mod Outage Determined That Valves Were Leaking.Caused by Debris &/Or Dirt on Valve Seats. Valves Lapped & Reseated & Successfully Retested
| Plant =
| Reporting criterion =
| Power level =
| Mode =
| Docket = 05000321
| LER year = 1981
| LER number = 16
| LER revision = 3
| Event date =
| Report date =
| ENS =
| abstract =
}}
 
=text=
{{#Wiki_filter:_... -. - -.-
i
' idRC FORM D6 U. S. NUCLE AR REGULATORY COMMISSION (7-77 ).
LICENSEE EVENT REPORT Update Report Previous Report 1bte 3-26-81 CONTROL tiLOCK: l l
l l
l l lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6
Io I i l I cl Al El Il Hl 1)@l O l Ol -l 0 l O l O ! O l 0 l - l 0 l 0 l@l 4 l 1 l 1 l 1 l 1 l@[_i_.] @
1 7
8 9 LICENSdE CODE 14 15 LICENSE NUYBEM 25 26 LICENSE TYPE JO 5 7 CA T b6 CON'T IoIil Sllj'"C l_Lj@l0 is lo lo lo 1312 h l@l O I 310 I r,I a l 1 l@l019 l 0 l 3 l 8 l 1 l@
I 8
60 61 DOCKET NUMBER t4 69 EVENT DATE 74
.'S REPORT DATE
'to
[
EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h lo 121 I On 3-4-81. with Unit 1 shutdown for a refueling / torus modifiention nii t - 1 i
i O ta j l age, LLRTs of inboard MSIVs BM-F02?A. B. And C were performed.
On 3-1 loI.si L6-81, the data sheets were reviewed by the LLRT coordinator. and it was l' i
10151 1 determined that the valves were leaking in excess of the 11.5 scfh per I
r i l o 16 I i valve limit of Tech Specs 4. 7. A. 2.h (test volume would not nressurize). 1
* Io 121 1 This is a repetitive occurrence - refer to LER 50-366/1981-001.
There l
i o n i I were no effects on public health or safety due to this event.
I 80 i
7 8 9 DE CODE S BC DE COMPONENT CODE SUBC DE SU E
[ lit 9l l Cl Dl@ [Ej@ IX l@ lV l A lL IV lE lX l@ [F_j@ [ DJ @
7 8
9 10 11 12 13 18 19 20 SE QUENTI AL OCCURRENCE REPORT REVISION LER:RO EVENT YEAR REPORT NO.
CODE TYPE N O.
@ Ny,g 18l11
[. _]
101116l y
10131 Lx_j
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[.1.j a
_ 21 22 23 24 26 27 N
?3 30 31 32 t) A TO ON PL NT ME HOURS 22 S8 IT FORT 8.
SUPPLI MAN FACTURER K
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33 34 35 31 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h L'_l.o_j l Inspection of the valves showed that some debris and/or dirt had collectf litiiled on the valves' seats.
The valves were lapped and reseated and then I
liii2i lsuccessfu11y retested prior to startup.(as left leakages of 4.9 scfh). I llii3i l The unit is now in full compliance with the requirements of Tech Soecs I
ii pil4.7.A.2.h and no further reporting is required.
I 80 7
8 g 1
ST S
'4 POWER OTHER STATUS dis O RY DISCOVERY DESCRIPTION ll1 lsl[Gj@ l0l0l Q@l NA l
[B_J@l Performed LLRT l
A TIVITY CO TENT RELEASED OF RELE ASE AMOUNT OF ACTIVITY LOCATION OF RELEASE l2161 LZJ @ LZ_J@l NA l
l NA l
7 8 9 10 Il 44 45 80 PERSGNNEL E XPOSURES NUMBE R TYPE DESCRIPTION -
y l 0l 01 Ol@l Zl@l NA l
PERSONNE t imu'JiES i
NUMBER
 
==DESCRIPTION==
[Lbj l 0l 01 Of@l NA l
7 8 9 11 12 80 LOSS OF OR DAMAGE TO FACILITV TYPE
 
==DESCRIPTION==
l.tuj Lzj@l NA l
PususTY 8109150586 810903 DESCRIPTION @
PDR ADOCK 05000321 NRC USE ONLY iSSuEo@l uS PDR l
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2 o 68 69 80 %
7 8 9 10 C. L. Coggin - Supt. Plt. Eng. Serv.
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LER #:
50-321/198. J16, R1 Licensee:
Georgia Power Company Facility Name:
Edwin I. Hatch Docket #:
50-321 1
 
=Narrative=
Report for LER 50-321/1981-0,16, R1 On 3-4-81, with Unit I shutdown for a refueling / torus modific-ation outage, LLRTs of inboard main steam i solation valves B21-F022A, B,
and C were performed per procedure HNP-1-3952, " Primary Containment Periodic Type B - and Type C Leakage Tests".
On 3-6-81, the LLRT i
coordinator reviewed the data sheets, and it was determined that the 1
valves were leaking in excess of the 11.5 scfh per valve limit of Tech Specs 4.7. A.2. h (test volumes would not pressurize).
This is a i
repetitive occurrence - refer to LER 50-366/1981-001.
There were no effects on public health or safety.
An investigation conducted to determine the
 
==cause==
of the valves leaking showed that some debris had collected on the valve's seats.
The valves were lapped and reseated and then successfully retested-prior to startup (as left leakage of less than'4 scfh for B21-F022A; 4 scfh for B21-F022B; and 4.9 scfh for B21-F022C).
The unit is now in. full compliance with the requirements of Tech Specs 4.7. A.2.h and no further reporting is required.
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}}
 
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Latest revision as of 13:59, 23 December 2024