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| {{Adams
| | #REDIRECT [[05000366/LER-1981-054-03, /03L-0:on 810613,drywell & Torus hydrogen-oxygen Analyzer recorder,2P33-P001B,found to Be Inoperative.Caused by Analyzer Drift.Analyzer Recalibr]] |
| | number = ML20009F740
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| | issue date = 06/30/1981
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| | title = LER 81-054/03L-0:on 810613,drywell & Torus hydrogen-oxygen Analyzer recorder,2P33-P001B,found to Be Inoperative.Caused by Analyzer Drift.Analyzer Recalibr
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| | author name = Coggin C
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| | author affiliation = GEORGIA POWER CO.
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| | addressee name =
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| | addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
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| | docket = 05000366
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| | license number =
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| | contact person =
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| | document report number = LER-81-054-03L-01, LER-81-54-3L-1, NUDOCS 8107310484
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| | package number = ML20009F736
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| | document type = LICENSEE EVENT REPORT (SEE ALSO AO,RO), TEXT-SAFETY REPORT
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| | page count = 2
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| }}
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| =Text=
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| {{#Wiki_filter:U. S. NUCLEAR REGULATORY' COMMISSION NRC FOPf1366 (7-77 )
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| o LICENSEE EVENT REPORT (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
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| CONTROL BLOCK: l i
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| l l l l l lh e
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| lo lil8 l9 G l A 7
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| l E I I l H l 2 l@l 0 IO l- LICENSE LICENCEE CODE 14 15 1010NuM8ER l01010 l- 1010 l@l4 25 26 LICENSE ll Il Jol@l5 7 CAl T $8l@
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| ll Il TYPE CON'T lol11 7 8 S$RC"' 60 I L l@l 0 D3CKET 61 l 51010101316 NUMlER 68 l6 69 l@l016EVENT DATE Il 131311 l@l01613 74 75 REPORT DATE l 018 80 l1 l@
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| EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h lol2l IWhile operating at 2255 MWt, 2P33-P001B, drywell and torus H2-02 analyz-l lol3]jer recorder, was found to be inoperative.
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| Tech Soecs section 3.3.6.4-1 l 10141 leponi ron both channels to be noprativo during oower nopration. The i lo isl iplant was placed in a 30-day LCO. The health and safety of the public I 10161 Iwa s not affected. This is a repetitive event as last reported on LER I I
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| lo171 150-366/1981-033.
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| l l o la i I 80 C DE CODE EUBCO E COMPONENT CODE SL8C DE SU E 10191 7 8 I s l E l@ LLl@ W@ l xl xl xl x1 xl xi@ I Z I@ I Z I@
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| 9 10 11 12 13 18 19 20 OCCURF.ENCE REPORT REVISION SE QUENTI AL EVENT YEAR REPORT NO. COCE TYPE N O.
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| LER RO
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| @ 0uf.g E 1811 l l-l !0 l5 14 l l/l 1013 l ll l l-l l01 24 26 27 28 29 30 3' 32
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| _ 21 22 23 AKE A T ON ON PL NT ET HOURS 22 S GMI D FC i B. SLP LIE MAN FACTURER l33E l@l34 El@ LZ_j@ l36Zl@ l01010101 37 40 lyl@
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| 43 Llij@
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| 42 l xl@ l 01019 I 61@
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| 43 44 47 35 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS li101IThe cause of this evert has been attributed to analyzer drift. The I I
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| l i l i l Lav a l y z e r w a s recalibrated and returned to service.
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| I l i 121 I l
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| li t al i I
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| li14i I 7 8 9
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| '6 POWER OTHER STATUS I O RY DIECJVERY DESCRIPTION STA S I1 15l W @ l0l9l1i@l NA l lAl@lOperatorObservation l AC nVITY CO' TENT AMOUNT OF ACTIVITY LOCATION OF RELEASE AELEASED OF RELEASE NA l I 1 I6 l l Z l @ [Z_j@l NA l l PERSONNEL EXPOS ES Nuv8E R TYPE oeSCRiPriON O l NA l i l 71 10l O l O l@l Z l@l "
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| ' PERSONNE t iN;u' RIES NUV8ER DESCRIPTION NA l
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| [1h] 8l 9Ol 01 Ol@l 7 11 12 80 LOSS OF OR OAMAGE TO FACILtTY h TYPE DESCRIPTION v l
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| lilollZl@l 7 8 9 10 NA .
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| 80 NRC USE ONLY ,
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| issue 8107310484 810630 llllll]lll lll 12 I o f l N f@DESCRIPTIONO 7 8 9 l
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| 10 PDR ADOCK 05000 b
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| l 68 69 80 5
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| - , c s ., c.,* pu rnn e- .- 912-367-7851 2
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| a r
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| LER #: 50-366/1981-054 Licensee: Georgia Power Company Facility Name: Edwin I. Hatch Docket #: 50-366 Narrative Report for LER 50-366/1981-054 On 6-13-81, while operating at 91% power 2P33-P001B, drywell and torus H -02 analyzer recorder was found to be inoper-ative. Tech2 Specs section 3.3.6.4-i requires both channels to be operative during power operation. The plant was placed in a 30-day LCO. This is a repetitive event as last reported on LER 50-365/1981-033.
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| The cause of this ev e.nt has been attributed to analyzer drift. The analyzer, 2P33-P001B, was recalibrated per Comsip Delphi K-IV Hydrogen and Oxygen Analyzer procedure, HNP 3882. The analyzer was declared operable and returned to service.
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| Plant operation was not affected as a result of this event.
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| The health and safety of the public was not affected.
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| A generic ceview revealed no inherent drift problems. Unit 1 does not v.tilize this type of analyzer.
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| . _ _ _ _ _ .}}
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