ENS 41152: Difference between revisions

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| event date = 09/15/2004 09:11 CDT
| event date = 09/15/2004 09:11 CDT
| last update date = 10/27/2004
| last update date = 10/27/2004
| title = Invalid Actuation Of Containment Isolation Valves
| title = Invalid Actuation of Containment Isolation Valves
| event text = In accordance with the requirements and guidance of 10 CFR 50.73(a)(1), a telephonic report of an invalid signal affecting containment isolation valves in more than one system is being submitted.  This report is being made under 10 CFR 50.73(a)(2)(iv)(A), automatic actuation of a system listed in paragraph (a)(2)(iv)(B), in lieu of a written LER.
| event text = In accordance with the requirements and guidance of 10 CFR 50.73(a)(1), a telephonic report of an invalid signal affecting containment isolation valves in more than one system is being submitted.  This report is being made under 10 CFR 50.73(a)(2)(iv)(A), automatic actuation of a system listed in paragraph (a)(2)(iv)(B), in lieu of a written LER.
At 0911 hours, on 09/15/2004, while operating at full power, the plant experienced a loss of power to eight process radiation monitors.  The loss of power was caused by the failure of an internal radiation monitor system power supply, PS-100.  The affected radiation monitors actuated, where applicable, their associated safety and non-safety related components.  The safety related components affected included eight containment isolation valves and the plant's auxiliary building special ventilation system equipment.  The containment isolation valves were:
At 0911 hours, on 09/15/2004, while operating at full power, the plant experienced a loss of power to eight process radiation monitors.  The loss of power was caused by the failure of an internal radiation monitor system power supply, PS-100.  The affected radiation monitors actuated, where applicable, their associated safety and non-safety related components.  The safety related components affected included eight containment isolation valves and the plant's auxiliary building special ventilation system equipment.  The containment isolation valves were:

Latest revision as of 21:22, 1 March 2018

ENS 41152 +/-
Where
Kewaunee Dominion icon.png
Wisconsin (NRC Region 3)
Reporting
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation
Time - Person (Reporting Time:+1009.17 h42.049 days <br />6.007 weeks <br />1.382 months <br />)
Opened: Gary Harrington
15:21 Oct 27, 2004
NRC Officer: Bill Huffman
Last Updated: Oct 27, 2004
41152 - NRC Website
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