ENS 42446: Difference between revisions

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| event date = 03/23/2006 12:50 EST
| event date = 03/23/2006 12:50 EST
| last update date = 04/04/2006
| last update date = 04/04/2006
| title = 24-Hour Condition Of License Report Due To Thermal Power Potentially Exceeding Licensed Limit
| title = 24-Hour Condition of License Report Due to Thermal Power Potentially Exceeding Licensed Limit
| event text = McGuire Unit 1 and Unit 2 may have been operating greater than design thermal power limits of 3411 MW [Megawatt] by approximately 0.08% due to discovery of non-conservative thermal power calculations.  Preliminary evaluation of Steam Generator Blow Down inputs into the thermal power calorimetric indicates a non-conservative error resulting in indicated total thermal power being approximately 0.08% lower than actual.  Additional evaluations to confirm indicated power are ongoing.  Power was reduced as soon as the on duty shift was made aware of the error and both Unit 1 and Unit 2 indicated thermal power is being limited to less than 99.85% to ensure actual reactor power remains less than 3411 MW.
| event text = McGuire Unit 1 and Unit 2 may have been operating greater than design thermal power limits of 3411 MW [Megawatt] by approximately 0.08% due to discovery of non-conservative thermal power calculations.  Preliminary evaluation of Steam Generator Blow Down inputs into the thermal power calorimetric indicates a non-conservative error resulting in indicated total thermal power being approximately 0.08% lower than actual.  Additional evaluations to confirm indicated power are ongoing.  Power was reduced as soon as the on duty shift was made aware of the error and both Unit 1 and Unit 2 indicated thermal power is being limited to less than 99.85% to ensure actual reactor power remains less than 3411 MW.
This notification is being made pursuant to the McGuire Facility Operating License Condition 2.C.(1) Maximum Power Level.
This notification is being made pursuant to the McGuire Facility Operating License Condition 2.C.(1) Maximum Power Level.

Latest revision as of 21:19, 1 March 2018

ENS 42446 +/-
Where
McGuire 
North Carolina (NRC Region 2)
Reporting
Other Unspec Reqmnt
Time - Person (Reporting Time:+0.5 h0.0208 days <br />0.00298 weeks <br />6.849e-4 months <br />)
Opened: Fred Kirk
18:20 Mar 23, 2006
NRC Officer: Steve Sandin
Last Updated: Apr 4, 2006
42446 - NRC Website
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