ENS 43329: Difference between revisions

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| event date = 04/30/2007 15:02 EDT
| event date = 04/30/2007 15:02 EDT
| last update date = 04/30/2007
| last update date = 04/30/2007
| title = Reactor Trip Due To Grass Intrusion Into Circulating Water Intake Structure
| title = Reactor Trip Due to Grass Intrusion Into Circulating Water Intake Structure
| event text = A manual trip of Salem Unit 1 was initiated due to a loss of the circulators from heavy grassing at the circulating water intake structure.  All rods fully inserted on the trip and all systems responded as designed, with decay heat being removed via the atmospheric relief valves and subsequently the steam dump system.  All Auxiliary Feedwater pumps auto started as expected on low steam generator levels from the trip.  Salem Unit 1 had entered the abnormal operating procedure for circulating water due to two (2) circulators being out of service; one circulator previously emergency tripped due to excessive traveling water screen [differential pressure] and a second circulator emergency tripped soon thereafter.  The procedure provides guidance to trip the plant if less than three (3) circulators are in service and power is above ten (10) percent.  Two (2) of the remaining four (4) in-service circulators emergency tripped due to excessive traveling water screen differential pressure.  At this point the manual reactor trip was initiated.  The crew entered emergency operating procedures and stabilized the plant at no load conditions.
| event text = A manual trip of Salem Unit 1 was initiated due to a loss of the circulators from heavy grassing at the circulating water intake structure.  All rods fully inserted on the trip and all systems responded as designed, with decay heat being removed via the atmospheric relief valves and subsequently the steam dump system.  All Auxiliary Feedwater pumps auto started as expected on low steam generator levels from the trip.  Salem Unit 1 had entered the abnormal operating procedure for circulating water due to two (2) circulators being out of service; one circulator previously emergency tripped due to excessive traveling water screen [differential pressure] and a second circulator emergency tripped soon thereafter.  The procedure provides guidance to trip the plant if less than three (3) circulators are in service and power is above ten (10) percent.  Two (2) of the remaining four (4) in-service circulators emergency tripped due to excessive traveling water screen differential pressure.  At this point the manual reactor trip was initiated.  The crew entered emergency operating procedures and stabilized the plant at no load conditions.
No personnel injuries have occurred as a result of the trip. Salem Unit 2 was not affected and is operating at 100% power.
No personnel injuries have occurred as a result of the trip. Salem Unit 2 was not affected and is operating at 100% power.

Latest revision as of 22:16, 1 March 2018

ENS 43329 +/-
Where
Salem PSEG icon.png
New Jersey (NRC Region 1)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation
Time - Person (Reporting Time:+-2.22 h-0.0925 days <br />-0.0132 weeks <br />-0.00304 months <br />)
Opened: Richard Desanctis
16:49 Apr 30, 2007
NRC Officer: Pete Snyder
Last Updated: Apr 30, 2007
43329 - NRC Website
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