ENS 43581: Difference between revisions

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| event date = 08/20/2007 10:53 CDT
| event date = 08/20/2007 10:53 CDT
| last update date = 08/20/2007
| last update date = 08/20/2007
| title = Electrical Breaker B4305 Unable To Function  
| title = Electrical Breaker B4305 Unable to Function  
| event text = During panel walk downs in the Main Control Room, an Operator discovered no light indication for V-AC-4, B RHR ROOM AIR COOLING UNIT.  Operator was dispatched to Breaker B4305 and 'B' RHR room to determine cause of loss of indicating light. The Operator determined that breaker B4305 (V-AC-4, 'B' RHR ROOM AIR COOLING UNIT 480V SUPPLY) was unable to function.  Division II RHR pumps, Division II CS pump, and associated low pressure injection systems were declared inoperable.  Tech Spec Actions 3.5.1.A, 3.5.1.B, and 3.5.1.M were entered resulting in entry into LCO 3.0.3 at 1053 on August 20, 2007.  At 1151 on August 20, 2007 power reduction was commenced using normal shutdown procedures.
| event text = During panel walk downs in the Main Control Room, an Operator discovered no light indication for V-AC-4, B RHR ROOM AIR COOLING UNIT.  Operator was dispatched to Breaker B4305 and 'B' RHR room to determine cause of loss of indicating light. The Operator determined that breaker B4305 (V-AC-4, 'B' RHR ROOM AIR COOLING UNIT 480V SUPPLY) was unable to function.  Division II RHR pumps, Division II CS pump, and associated low pressure injection systems were declared inoperable.  Tech Spec Actions 3.5.1.A, 3.5.1.B, and 3.5.1.M were entered resulting in entry into LCO 3.0.3 at 1053 on August 20, 2007.  At 1151 on August 20, 2007 power reduction was commenced using normal shutdown procedures.
Site Electricians determined that a line fuse had blown.  The fan motor was meggared and all three line fuses were replaced.  At 1230 on August 20, 2007, V-AC-4 was tested and returned to service.  Division II RHR pumps, Division II CS pump and associated low pressure injection systems were declared operable.  LCO 3.0.3 and T.S. Actions 3.5.1.A, 3.5.1.B, and 3.5.1.M were exited.  Power reduction was terminated at 98%.
Site Electricians determined that a line fuse had blown.  The fan motor was meggared and all three line fuses were replaced.  At 1230 on August 20, 2007, V-AC-4 was tested and returned to service.  Division II RHR pumps, Division II CS pump and associated low pressure injection systems were declared operable.  LCO 3.0.3 and T.S. Actions 3.5.1.A, 3.5.1.B, and 3.5.1.M were exited.  Power reduction was terminated at 98%.

Latest revision as of 21:16, 1 March 2018

ENS 43581 +/-
Where
Monticello Xcel Energy icon.png
Minnesota (NRC Region 3)
Reporting
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Time - Person (Reporting Time:+-1.3 h-0.0542 days <br />-0.00774 weeks <br />-0.00178 months <br />)
Opened: Randy Sandy
14:35 Aug 20, 2007
NRC Officer: John Knoke
Last Updated: Aug 20, 2007
43581 - NRC Website
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