ENS 47582: Difference between revisions

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| event date = 01/10/2012 04:36 EST
| event date = 01/10/2012 04:36 EST
| last update date = 02/15/2012
| last update date = 02/15/2012
| title = Excessive Leakage From Rcp Seal Return  
| title = Excessive Leakage from Rcp Seal Return  
| event text = Plant shutdown from 100% due to increased leakage from 21 RCP [Reactor Coolant Pump] seal return was commenced at 0100 EST. A manual reactor trip was actuated in accordance with plant procedures at 25% power.  Auxiliary feedwater pump was placed in service prior to the reactor trip, per plant procedures. Decay heat is being removed via the condenser steam dumps. All offsite power sources are available. All equipment operated as expected.
| event text = Plant shutdown from 100% due to increased leakage from 21 RCP [Reactor Coolant Pump] seal return was commenced at 0100 EST. A manual reactor trip was actuated in accordance with plant procedures at 25% power.  Auxiliary feedwater pump was placed in service prior to the reactor trip, per plant procedures. Decay heat is being removed via the condenser steam dumps. All offsite power sources are available. All equipment operated as expected.
The licensee has notified the NRC Resident Inspector and other government agencies.
The licensee has notified the NRC Resident Inspector and other government agencies.

Latest revision as of 21:04, 1 March 2018

ENS 47582 +/- *RETRACTED*
Where
Indian Point 
New York (NRC Region 1)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation
Time - Person (Reporting Time:+-4.78 h-0.199 days <br />-0.0285 weeks <br />-0.00655 months <br />)
Opened: Russ Long
04:49 Jan 10, 2012
NRC Officer: John Knoke
Last Updated: Feb 15, 2012
47582 - NRC Website
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